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23
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nameWellbore
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26 values
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1 value
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stringlengths
25
25
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stringlengths
25
25
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stringclasses
1 value
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stringclasses
183 values
wellAlias
dict
wellboreAlias
listlengths
2
2
wellboreInfo
listlengths
1
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statusInfo
listlengths
1
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fluid
listlengths
0
6
porePressure
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surveyStation
listlengths
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7
15_9_F_4_2008_03_21
NO 15/9-F-4
NO 15/9-F-4
name
2008-03-20T00:00:00+01:00
2008-03-21T00:00:00+01:00
normal
2018-05-03T13:52:53+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "10.5", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-03-21T00:00:00+01:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "WOW for pulling drilling riser.Perform general maintenance. Nipple down BOP and diverter. ", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "74", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "WOW. Performed general maintenance.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-03-20T22:00:00+01:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "3508", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-03-21T00:00:00+01:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "WOW. Serviced and inspected the TDS.\n", "dTimEnd": "2008-03-20T03:00:00+01:00", "dTimStart": "2008-03-20T00:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW. Changed out the wash pipe.\n", "dTimEnd": "2008-03-20T05:00:00+01:00", "dTimStart": "2008-03-20T03:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW. Cleaned and cleared the rig floor\n", "dTimEnd": "2008-03-20T06:00:00+01:00", "dTimStart": "2008-03-20T05:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW. Cleaned and cleared the rig floor. \n", "dTimEnd": "2008-03-20T07:15:00+01:00", "dTimStart": "2008-03-20T06:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW. Performed general maintenance. Cleaned kill manifold. Had derrick inspection. Serviced Carrier rollers, spinner and tracks on aft Roughneck.\n", "dTimEnd": "2008-03-20T19:00:00+01:00", "dTimStart": "2008-03-20T07:15:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW. Cleaned rig floor. Cleaned pit # 7. Performed maintenance on the aft PRS and the TDS.\n", "dTimEnd": "2008-03-21T00:00:00+01:00", "dTimStart": "2008-03-20T19:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_03_22
NO 15/9-F-4
NO 15/9-F-4
name
2008-03-21T00:00:00+01:00
2008-03-22T00:00:00+01:00
normal
2018-05-03T13:52:53+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "11.4", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-03-22T00:00:00+01:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "WOW to be able to nipple down Diverter and BOP. Nipple down the Diverter, BOP and the HPDR.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "75", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "WOW prior to retrieve the HP drilling riser. Meanwhile cleaned stand pipe/Choke line manifold. Changed oil on the TDS. Performed general maintenance and PM's. Changed out the cathead wire. Prepared tools and lifting equipment, for nippling down the Diverter, BOP and the HPDR. Commenced installation of flood light in derrick.\n\n", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-03-21T15:00:00+01:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "3508", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-03-22T00:00:00+01:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "WOW. Greased the UPR track on the PRS beam. Functioned main flow line valve 1250 psi. Transported 6 flood light to the finger board level in the derrick. \n", "dTimEnd": "2008-03-21T06:00:00+01:00", "dTimStart": "2008-03-21T00:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW prior to retrieve the HP drilling riser. Meanwhile cleaned stand pipe/Choke line manifold. Changed oil on the TDS. Performed general maintenance and PM's. Changed out the cathead wire.", "dTimEnd": "2008-03-21T19:00:00+01:00", "dTimStart": "2008-03-21T06:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW prior to retrieve the HP drilling riser. Meanwhile prepared tools and lifting equipment, for nippling down the Diverter,BOP and the HPDR. Commenced installation of flood light in derrick.\n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg\n22:00 41/47 30° 6.1/9.7 360°\n23:00 42/47 30° 6.2/9.8 10°\n00:00 43/48 30° 6.1/9.7 360°\n", "dTimEnd": "2008-03-22T00:00:00+01:00", "dTimStart": "2008-03-21T19:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_03_23
NO 15/9-F-4
NO 15/9-F-4
name
2008-03-22T00:00:00+01:00
2008-03-23T00:00:00+01:00
normal
2018-05-03T13:52:53+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "12.4", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-03-23T00:00:00+01:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "WOW to be able to nipple down Diverter and BOP. Nipple down the Diverter, BOP and the HPDR.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "76", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "WOW prior to retrieve the HP riser. Performed general maintenance and PM's. Commenced changing out the seal assy of BOP door. Installed flood light in derrick. Cleaned pit # 6,8,9,10 & 11.\n", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-03-22T15:00:00+01:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3508", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-03-23T00:00:00+01:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "WOW prior to retrieve the HP drilling riser. Continued installation of flood light in derrick.\n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg\n00:30 40/45 30° 6.4/10.1 360°\n02:00 42/47 30° 6.1/9.6 10°\n03:00 39/43 30° 6.0/9.6 10°\n04:30 37/41 20° 5.6/8.8 360°\n05:00 35/41 30° 5.3/8.4 10°\n06:00 34/38 20° 4.9/7.9 10°\n", "dTimEnd": "2008-03-22T06:00:00+01:00", "dTimStart": "2008-03-22T00:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW prior to retrieve the HP riser. Meanwhile installed flood light in derrick. Commenced changing out the seal assy of BOP door. Cleaned pit # 9 & 11. Performed general maintenance and PM's.\nMoved CTS funnel from F-9 to F-1. Installed cover in CTS funnel. \n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg\n07:00 24/30 30° 4.4/10 10°\n09:00 18/26 28° 4/10.4 30°\n11:00 14/20 24° 3.7/7.8 40°\n13:00 9/15 7° 3/9.4 340°\n15:00 15/21 300° 2.8/9.8 225°\n17:00 20/23 315° 2.9/8.9 250°\n19:00 19/22 320° 2.6/4.1 340°\n", "dTimEnd": "2008-03-22T19:00:00+01:00", "dTimStart": "2008-03-22T06:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW prior to retrieve the HP riser. Installed flood light in derrick. Cleaned pit # 6,8 & 10.\n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg\n21:00 18/22 320° 2.6/4.2 320°\n23:00 20/23 340° 2.5/4 340°\n", "dTimEnd": "2008-03-23T00:00:00+01:00", "dTimStart": "2008-03-22T19:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_03_24
NO 15/9-F-4
NO 15/9-F-4
name
2008-03-23T00:00:00+01:00
2008-03-24T00:00:00+01:00
normal
2018-05-03T13:52:53+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "13.3", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-03-24T00:00:00+01:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "WOW to be able to nipple down Diverter and BOP. Nipple down the Diverter, BOP and the HPDR.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "77", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "WOW prior to retrieve the HP riser. Performed general maintenance and PM's. Changed out of BOP door seal assy, greased manuel valves on choke/kill line. Cleaned pit. Performed general maintenance and PM's. Not able to work at rig floor, due to exhaust fumes. Installed CRI check valve on to F-14. Attempted to inject in to F-12 annulus.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-03-23T15:00:00+01:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3508", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-03-24T00:00:00+01:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "WOW prior to retrieve the HP riser. Completed installation of the flood light in the derrick. House keeping in the moon pool.\n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg\n01:00 7/9 360° 2.7/3.9 340°\n03:00 11/15 340° 2.4/4.1 340°\n05:00 15/18 350° 2.7/4.3 340°\n07:00 12/14 350° 2.9/4.6 340°\n", "dTimEnd": "2008-03-23T06:00:00+01:00", "dTimStart": "2008-03-23T00:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW prior to retrieve the HP riser. Changed out of BOP door seal assy, greased manual valves on choke/kill line. Cleaned pit. Performed general maintenance and PM's. \n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg\n08:00 17/23 330° 2.6/4.1 350°\n10:00 2.3/3.6 \n12:00 1.6/2.6 \n14:00 1.3/2.1 \n16:00 21/24 350° 1.8/2.9 330°\n18:00 23/26 340° 3.1/5.0 340°\n\n14:30-19:00 Not able to work at rig floor, due to exhaust fumes.", "dTimEnd": "2008-03-23T19:00:00+01:00", "dTimStart": "2008-03-23T06:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW prior to retrieve the HP riser. Not able to work at rig floor, due to exhaust fumes. Performed general maintenance and PM's. Greased valves on BOP. Disconnected the CRI hose from F-12 and removed the check valve. Connected up the CRI hose again and opened to annulus, annulus pressure 52 bars. Attempted to inject seawater into F-12, stopped pumping at 190 bars.\n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg\n20:00 18/28 330° 3.7/5.9 350°\n22:00 22/26 330° 3.6/5.7 340°\n00:00 26/32 320° 3.3/5.7 340°\n", "dTimEnd": "2008-03-24T00:00:00+01:00", "dTimStart": "2008-03-23T19:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_03_25
NO 15/9-F-4
NO 15/9-F-4
name
2008-03-24T00:00:00+01:00
2008-03-25T00:00:00+01:00
normal
2018-05-03T13:52:53+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "14.3", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-03-25T00:00:00+01:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "WOW to be able to nipple down Diverter and BOP. Nipple down the Diverter, BOP and the HPDR.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "78", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "WOW prior to retrieve the HP riser. No access to rig floor, due to exhaust fumes. RIH with test plug, attempted to test against plug. Performed general maintenance and PM's. Re-ran in hole with test plug with polypack seals. Pressure tested plug to 25/345 bars 5/10 min. ", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-03-24T15:00:00+01:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3508", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-03-25T00:00:00+01:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "WOW prior to retrieve the HP riser. Not able to work at rig floor, due to exhaust fumes. Installed CRI check valve on to F-14. Greased valves on BOP. House keeping in the moon pool. \n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg\n02:00 17/20 320° 3.6/5.8 340°\n04:00 30/34 320° 3.1/5.8 340°\n06:00 15/18 340° 2.7/4.3 340°\n07:00 29/33 350° 3.6/5.8 340°\n", "dTimEnd": "2008-03-24T06:00:00+01:00", "dTimStart": "2008-03-24T00:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW prior to retrieve the HP riser. Performed general maintenance and PM's. \n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg\n08:00 15/17 340° 4.2/6.7 340°\n10:00 25/28 340° 3.9/6.3 340° \n12:00 26/30 340° 3.6/5.8 340° \n14:00 3.7/5.9 350° \n\n07:00-10:30 No access to rig floor, due to exhaust fumes.\n12:45-14:00 No access to rig floor, due to exhaust fumes\n", "dTimEnd": "2008-03-24T14:00:00+01:00", "dTimStart": "2008-03-24T06:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW prior to retrieve the HP riser. Meanwhile RIH with test plug and landed of in sub sea WH. Attempted to pressure test against plug. POOH with test plug. \n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg\n16:00 23/26 330° 3.9/6.2 330°\n18:00 23/27 360° 3.9/6.2 340°\n\n16:30-19:00 No access to rig floor, due to exhaust fumes\n", "dTimEnd": "2008-03-24T19:00:00+01:00", "dTimStart": "2008-03-24T14:00:00+01:00", "md": "139", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW prior to retrieve the HP riser. Not able to work at rig floor, due to exhaust fumes. Performed general maintenance and PM's. \n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg\n20:00 3.8/6.1 340°\n22:00 20/24 320° 4.0/6.3 340°\n00:00 17/22 320° 3.9/6.3 340°\n", "dTimEnd": "2008-03-25T00:00:00+01:00", "dTimStart": "2008-03-24T19:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_03_26
NO 15/9-F-4
NO 15/9-F-4
name
2008-03-25T00:00:00+01:00
2008-03-26T00:00:00+01:00
normal
2018-05-03T13:52:53+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "15.2", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-03-26T00:00:00+01:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "WOW to be able to retrieve the HPDR. Retrieve the HPDR. WOW to be able to run PR.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "79", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "WOW prior to retrieve the HP riser. No access to rig floor, due to exhaust fumes. Pressure tested BOP and TDS 20/345 bars 5/10 min. Performed derrick inspection. N/D diverter and BOP. Installed Claxton tool and made up same.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-03-25T15:00:00+01:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3508", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-03-26T00:00:00+01:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "WOW prior to retrieve the HP riser. Not able to work at rig floor, due to exhaust fumes. Performed general maintenance and PM's. \n", "dTimEnd": "2008-03-25T04:00:00+01:00", "dTimStart": "2008-03-25T00:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW prior to retrieve the HP riser. Meanwhile re-RIH with test plug with polypack seals and landed of in sub sea WH. Pressure tested plug to 25/345 bars 5/10 min.", "dTimEnd": "2008-03-25T06:00:00+01:00", "dTimStart": "2008-03-25T04:00:00+01:00", "md": "139", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW prior to retrieve the HP riser. Pressure tested BOP and TDS 20/345 bars 5/10 min. Performed derrick inspection. \n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg\n12:30 27/32 320° 4.5/7.2 340°\n14:30 24/30 320° 4.6/7.3 340° \n16:30 23/25 340° 4.6/7.4 340° \n18:30 23/27 340° 4.2/6.6 340° \n\n14:45-15:30 No access to rig floor, due to exhaust fumes\n", "dTimEnd": "2008-03-25T15:30:00+01:00", "dTimStart": "2008-03-25T06:00:00+01:00", "md": "139", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW prior to retrieve the HP riser. POOH with the test plug assy. Racked back string in derrick and laid out the test plug.\n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg\n16:30 23/25 340° 4.6/7.4 340° \n18:30 23/27 340° 4.2/6.6 340° \n\n16:30-18:30 No access to rig floor, due to exhaust fumes\n", "dTimEnd": "2008-03-25T19:00:00+01:00", "dTimStart": "2008-03-25T15:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW prior to retrieve the HP riser. Prepared for N/D diverter. Checked tool for making up the Claxton tool.\n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg\n21:00 17/19 330° 4.2/6.7 340°\n22:30 15/17 330° 3.5/5.5 340°\n23:15 15/17 350° 3.1/5.0 340°\n\n19:00-20:30 No access to rig floor, due to exhaust fumes\n23:00-00:00 No access to rig floor, due to exhaust fumes\n", "dTimEnd": "2008-03-26T00:00:00+01:00", "dTimStart": "2008-03-25T19:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_03_27
NO 15/9-F-4
NO 15/9-F-4
name
2008-03-26T00:00:00+01:00
2008-03-27T00:00:00+01:00
normal
2018-05-03T13:52:53+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "15.6", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-03-27T00:00:00+01:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Pull HPDR. WOW for running production Riser.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "80", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "WOW prior to pull HPDR. Shut in F12 production. Prepared for/disconnected and pulled HPDR.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-03-26T15:00:00+01:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3508", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-03-27T00:00:00+01:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "WOW prior to retrieve the HP riser. No access to rig floor, due to exhaust fumes.\n", "dTimEnd": "2008-03-26T00:30:00+01:00", "dTimStart": "2008-03-26T00:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk and N/D diverter and BOP. Had gas turbines shut down at 01:25 due to exhaust fumes blowing into the rig floor.", "dTimEnd": "2008-03-26T03:00:00+01:00", "dTimStart": "2008-03-26T00:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to M/U the Claxton tool.", "dTimEnd": "2008-03-26T03:15:00+01:00", "dTimStart": "2008-03-26T03:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Landed the Claxton tool on to the HPDR. Made Claxton tool to 1300 ft-lbs.", "dTimEnd": "2008-03-26T06:00:00+01:00", "dTimStart": "2008-03-26T03:15:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW prior to retrieve the HP riser. \n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg\n06:30 22/25 350° 3,4/5,4 340°\n", "dTimEnd": "2008-03-26T07:00:00+01:00", "dTimStart": "2008-03-26T06:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Shut in F-12 for production. Simultaneously prepared for retrieving HPDR BOP joint. Moved CRI hose line from F-12 to F-14. Installed hot stab, for releasing of riser TBC.\n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg\n08:30 13/15 020° 3,5/5,5 340° \n", "dTimEnd": "2008-03-26T11:00:00+01:00", "dTimStart": "2008-03-26T07:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Loosen BOP/Tension joint flange. At 11:15 confirmed production shut in.\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg \n11:30 6/11 030* 2,6/4,1 340° \n13:30 4/10 050° 2,2/3,4 340° \n15:00 1/3 110° 2,1/3,4 350° \n", "dTimEnd": "2008-03-26T15:00:00+01:00", "dTimStart": "2008-03-26T11:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed horizontal tension support for riser in the moon pool.\n", "dTimEnd": "2008-03-26T15:30:00+01:00", "dTimStart": "2008-03-26T15:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Loosen the remaining 4 bolts on BOP/tension joint flange.", "dTimEnd": "2008-03-26T16:00:00+01:00", "dTimStart": "2008-03-26T15:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up the BOP joint and racked back one DP stand.\n", "dTimEnd": "2008-03-26T16:45:00+01:00", "dTimStart": "2008-03-26T16:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/U elevator on slings to allow, for laying out the Claxton tool with pup joint attached. Removed master bushing and outer ring.\n", "dTimEnd": "2008-03-26T17:30:00+01:00", "dTimStart": "2008-03-26T16:45:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled the BOP joint above the RT. Installed outer ring and the master bushing. Preserved the BOP joint flange. Laid out the BOP joint.\n", "dTimEnd": "2008-03-26T18:15:00+01:00", "dTimStart": "2008-03-26T17:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/D slings on elevator.\n", "dTimEnd": "2008-03-26T18:30:00+01:00", "dTimStart": "2008-03-26T18:15:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up riser lifting sub on one DP std.\n", "dTimEnd": "2008-03-26T19:00:00+01:00", "dTimStart": "2008-03-26T18:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk and RIH with C-type lifting sub and made up same to Tension joint. Simultaneously disconnected the Claxton tool from the BOP joint.", "dTimEnd": "2008-03-26T20:45:00+01:00", "dTimStart": "2008-03-26T19:00:00+01:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed Spider.\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg \n21:30 4/8 160° 1,7/2,7 350° \n", "dTimEnd": "2008-03-26T21:45:00+01:00", "dTimStart": "2008-03-26T20:45:00+01:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk and applied 130 MT on to the string. Commenced to remove tension cylinders.\n", "dTimEnd": "2008-03-27T00:00:00+01:00", "dTimStart": "2008-03-26T21:45:00+01:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_03_28
NO 15/9-F-4
NO 15/9-F-4
name
2008-03-27T00:00:00+01:00
2008-03-28T00:00:00+01:00
normal
2018-05-03T13:52:53+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "15.5", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-03-28T00:00:00+01:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "WOW. Meanwile transfer F-4 flowline/hose from drillfloor to XMT deck. Transfer 4 ea tension cylinders for F-14 to Centralizer deck. Run production riser; TBC, stress joint and two riser doubles. WOW.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "81", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Pulled HPDR from 140 m to surface. Laid doubles in horizontal storage rack. Prepared singles for backload.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-03-27T17:00:00+01:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3508", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-03-28T00:00:00+01:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Continued rigging down the tension system.\n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg \n00:20 7/12 160° 1,3/2,1 360° \n", "dTimEnd": "2008-03-27T01:45:00+01:00", "dTimStart": "2008-03-27T00:00:00+01:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk and slacked of to 110 MT on the string. Released TBC as per Vetco procedure.\n", "dTimEnd": "2008-03-27T03:00:00+01:00", "dTimStart": "2008-03-27T01:45:00+01:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled HPDR tensinon joint and landed of in Spider. Racked back stand in derrick. Made up HPDR lifting sub. Pulled back first double HPDR with tension joint on top and landed of in Spider.", "dTimEnd": "2008-03-27T04:30:00+01:00", "dTimStart": "2008-03-27T03:00:00+01:00", "md": "95", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Disconnected flange bolt on HPDR flange and picked up double.\n\nTime Wind speed Wind direction Sea Wave direction\n Knots deg m deg \n05:00 11/15 170° 1,5/2,4 360°", "dTimEnd": "2008-03-27T06:00:00+01:00", "dTimStart": "2008-03-27T04:30:00+01:00", "md": "95", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up handling flange type C to HPDR double B in rotary.", "dTimEnd": "2008-03-27T08:00:00+01:00", "dTimStart": "2008-03-27T06:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Landed double A on HTS cradle with simultaneous lift by deck crane and block. Re-slung double A and lifted to horizontal storage rack using deck crane.", "dTimEnd": "2008-03-27T09:00:00+01:00", "dTimStart": "2008-03-27T08:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled HPDR double B through rotary and placed coupling in working height above riser spider. Removed fairrings.", "dTimEnd": "2008-03-27T10:00:00+01:00", "dTimStart": "2008-03-27T09:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Landed off double B in riser spider. Broke bolts on flange. Inspected and preserved seal surfaces on flanges. Made up handling flange flange type C to double C.", "dTimEnd": "2008-03-27T14:15:00+01:00", "dTimStart": "2008-03-27T10:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Landed double B on HTS cradle with simultaneous lift by deck crane and block. Re-slung double B and lifted to horizontal storage rack using deck crane.", "dTimEnd": "2008-03-27T15:00:00+01:00", "dTimStart": "2008-03-27T14:15:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled HPDR double C through rotary and placed coupling in working height above riser spider. Removed fairrings.", "dTimEnd": "2008-03-27T16:00:00+01:00", "dTimStart": "2008-03-27T15:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Landed off double C in riser spider. Broke bolts on flange. Lifted off double C. Inspected and preserved seal surfaces on flanges. Made up handling flange type C to standard joint #1. Meanwhile ROV brushed wellhead seal area and installed VXG ring.", "dTimEnd": "2008-03-27T18:15:00+01:00", "dTimStart": "2008-03-27T16:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Landed double C on HTS cradle with simultaneous lift with deck crane and block. Re-slung double C and lifted to horizontal storage rack using deck crane.", "dTimEnd": "2008-03-27T19:15:00+01:00", "dTimStart": "2008-03-27T18:15:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled HPDR standard joint #1 and placed coupling in working height above riser spider. Removed \nfairrings. Landed off HPDR standard joint #1 in riser spider. Broke bolts on flange. Observed loose skirt on TBC connector, bolts partly unscrewd and 2 bolts missing. Thightended bolts on TBC skirt.", "dTimEnd": "2008-03-27T21:30:00+01:00", "dTimStart": "2008-03-27T19:15:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up handling flange type C to HPDR lower pup joint.", "dTimEnd": "2008-03-27T22:15:00+01:00", "dTimStart": "2008-03-27T21:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Landed HPDR standard joint #1 on HTS cradle with simultaneous lift by deck crane and block. Re-slung double HPDR standard joint #1 and lifted to basket on main deck.", "dTimEnd": "2008-03-27T22:30:00+01:00", "dTimStart": "2008-03-27T22:15:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled HPDR lower pup joint and placed coupling in working height above riser spider. Removed fairrings. Landed off HPDR standard joint #1 in riser spider. Meanwhile installed debris cap on F-4 using ROV and tugger assist.", "dTimEnd": "2008-03-28T00:00:00+01:00", "dTimStart": "2008-03-27T22:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_03_29
NO 15/9-F-4
NO 15/9-F-4
name
2008-03-28T00:00:00+01:00
2008-03-29T00:00:00+01:00
normal
2018-05-03T13:52:54+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "16.3", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-03-29T00:00:00+01:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Waiting on weather. Meanwhile test BOP. Prepare for running production riser.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "82", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Waited on weather for running production riser. Meanwhile brought flexible hose to XMT deck and hooked up same. Landed BOP on test stump. Attempted to test BOP to 15 K. Had leakage on test stump. Changed gasket on test stump. LIfted F-4 XMT to moonpool. Transferred tension cylinders to XMT deck.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[ { "dTim": "2008-03-29T00:00:00+01:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Broke bolts on flange between lower pup and stress joint.", "dTimEnd": "2008-03-28T01:30:00+01:00", "dTimStart": "2008-03-28T00:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Due to findings made by production department, halted operation for inspection in wellhead area. A support bracket on the F-12 flowline/piping was found to be ripped off. Mærsk rig management decided not to start production due to the circumstances. Further investigation/assessment needed before starting production.", "dTimEnd": "2008-03-28T02:30:00+01:00", "dTimStart": "2008-03-28T01:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- wait", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Landed HPDR lower pup joint on HTS cradle with simultaneous lift by deck crane and block. Removed handling flange. Re-slung HPDR lower pup joint and lifted to basket on main deck.", "dTimEnd": "2008-03-28T03:30:00+01:00", "dTimStart": "2008-03-28T02:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed handling flange type C on TBC joint. Pulled out TBC joint and laid down on HTS cradle with simultaneous lift by block and deck crane. Removed handling flange. Lifted TBC joint to basket on main deck.", "dTimEnd": "2008-03-28T05:15:00+01:00", "dTimStart": "2008-03-28T03:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "WOW for running production riser. \n\nMeanwhile: Cleared and tidied rigfloor. Brought F-4 flexible hose onto HTS. Held toolbox talk prior to transferring flexible hose to XMT deck.", "dTimEnd": "2008-03-28T06:00:00+01:00", "dTimStart": "2008-03-28T05:15:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited on weather.\n\nMeanwhile :\n-Cleared XMT deck for reception of F-4 flexible hose\n-Transferred F-4 flexible hose to XMT deck\n-Suspended flexibel hose in roof and jacked to position for hook up\n-Landed BOP on test stump and made up NT-2 connector\n-Tested door seal on BOP\n\n", "dTimEnd": "2008-03-28T19:00:00+01:00", "dTimStart": "2008-03-28T06:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited on weather.\n\nMeanwhile :\n-Worked on hooking up flexible hose\n-Assisted production in equalizing across DHSV\n", "dTimEnd": "2008-03-29T00:00:00+01:00", "dTimStart": "2008-03-28T19:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_03_30
NO 15/9-F-4
NO 15/9-F-4
name
2008-03-29T00:00:00+01:00
2008-03-30T00:00:00+01:00
normal
2018-05-03T13:52:54+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "17.3", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-03-30T00:00:00+01:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Waiting on weather. Run production riser.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3448", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "83", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Waited on weather to obtain conditions for running production riser. Meanwhile tested BOP to 15 K. Lifted TBC to drillfloor and performed pre-operational checks. Laid out 10 3/4\" casing. Installed vinyl guides and tenison ring in wellhead module decks.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-03-29T13:00:00+01:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3508", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-03-30T00:00:00+01:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Waited on weather.\n\nMeanwhile :\n-Worked on hooking up flexible hose\n-Tested BOP - 6 month 15 K test - had lekage on test stump\n-Changed gasket on test stump and made up NT-2 connector\n-Lifted F-4 XMT to moonpool\n-Transferred tension cylinders for F-14 to XMT deck\n", "dTimEnd": "2008-03-29T06:00:00+01:00", "dTimStart": "2008-03-29T00:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited on weather for running production riser.\n\nMeanwhile :\n-Performed 6 month BOP test to 15 K\n-Repaired 10 MT tugger in moonopol\n-Moved guide funnel to F-4 and installed debris cover\n-Performed derrick inspection", "dTimEnd": "2008-03-29T20:00:00+01:00", "dTimStart": "2008-03-29T06:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited on weather for running production riser.\n\nMeanwhile :\n-Performed repair of BX elevator\n-Lifted TBC joint to drillfllor\n-Performed pre-operational checks on TBC", "dTimEnd": "2008-03-30T00:00:00+01:00", "dTimStart": "2008-03-29T20:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_03_31
NO 15/9-F-4
NO 15/9-F-4
name
2008-03-30T00:00:00+01:00
2008-03-31T00:00:00+02:00
normal
2018-05-03T13:52:54+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "17.4", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-03-31T00:00:00+02:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Lock TBC according to Vetco procedure. Test production riser against GTV plug. Pump inhibitor in TBC. Install tensioner assembly and centralizers in wellhhead module. Transfer load from block to tensioner assembly. Disconnect riser flange and retrieve DP. Prepare for cutting tensioner joint.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3448", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "84", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "WOW for running production riser. Shut down F-12 production and ran production riser. Landed TBC on top of wellhead. Ran hot stab and minireel hose along guidewire.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-03-30T13:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3508", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-03-31T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[]
[]
15_9_F_4_2008_04_01
NO 15/9-F-4
NO 15/9-F-4
name
2008-03-31T00:00:00+02:00
2008-04-01T00:00:00+02:00
normal
2018-05-03T13:52:54+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "16.8", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-01T00:00:00+02:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Install surface WH and test BT seals. Install surface riser. N/U BOP and diverter. Install bowl protector in surface wellhead.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3448", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "85", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Locked TBC connector to subsea wellhead. Performed overpull test. Pumped hydraulic fluid / corrosion inhibitor in TBC cavities. Tested riser to 200 bar against GTV plug. Installed tensioning assembly on Centralizer deck and transferred load from block to tension cylinders. Installed centralizers in wellhead decks. Cut riser and made 45 deg bevel in riser circumference.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-03-31T13:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3508", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-01T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Held toolbox talk prior to lifting in tension joint. Removed BX-elevator. Installed 2 wire slings between bails and elevator. Picked up tension joint with deck crane and laid same on HTS cradle. Hooked up aft sling in tugger to get further in on drillfloor. Latched BX elevator around lift sub below 3 m pup joint. Lifted tension joint to upright position with simultaneous lift on deck crane and block.", "dTimEnd": "2008-03-31T01:00:00+02:00", "dTimStart": "2008-03-31T00:00:00+02:00", "md": "101", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed handling flange type F. Installed guide pins and landed tension joint on 3rd PR double. Made up connection using bolt tensioner tools. Pressure tested connection through test port 5 min / 345 bar using hand pump. Installed bolt protector caps. Installed fairrings.", "dTimEnd": "2008-03-31T02:30:00+02:00", "dTimStart": "2008-03-31T01:00:00+02:00", "md": "101", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Released BX elevator and removed slings. Installed BX elevator in bails. Re-latched tension joint. Removed spider and installed master bushing. RIH with tensioner joint, installed bowl and hung off riser on 3 m 5 1/2\" pup joint.", "dTimEnd": "2008-03-31T04:00:00+02:00", "dTimStart": "2008-03-31T02:30:00+02:00", "md": "120", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up 5 1/2\" landing stand. RIH with production riser on 5 1/2\" DP. Guided TBC into guide funnel while observing with ROV. Used ROV C-guide for stabbing TBC. Positioned ROV with manipulator camera pointing upwards in guide funnel cut out window. Observed TBC relative to VX ring and top wellhead while comming down with production riser. Stopped riser motion when ~10 cm TBC swallow was obtained.", "dTimEnd": "2008-03-31T04:45:00+02:00", "dTimStart": "2008-03-31T04:00:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Detached lift sling on two points on each side of the hinge of the guide funnel. Unlocked hinge bolts and split guide funnel. Removed guide funnel by means of ROV and tuggers.", "dTimEnd": "2008-03-31T05:45:00+02:00", "dTimStart": "2008-03-31T04:45:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with production riser and landed TBC on top of wellhead. Set down 10 MT. Ran hotstab and minireel hose along guidewire.", "dTimEnd": "2008-03-31T06:00:00+02:00", "dTimStart": "2008-03-31T05:45:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Established hot stab in port A and set valves on ROV lock panel to \"lock\". Verified TBC fully landed. Locked TBC by pressuring up through minireel to 3000 psi. Observed movement of indicator rods as prescribed. Maintained pressure for 15 mins. Set valves on ROV lock panel to parking position. Meanwhile assissted production in equalising across F-12 DHSV using cement unit.", "dTimEnd": "2008-03-31T07:00:00+02:00", "dTimStart": "2008-03-31T06:00:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed overpull test to 116 MT hookload / 20 MT overpull.", "dTimEnd": "2008-03-31T07:15:00+02:00", "dTimStart": "2008-03-31T07:00:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed hotstab and installed dummy stab. Moved hotstab to receptacle on panel B. Set valves to lower dog flush and injected hydraulic fluid / corrosion inhibitor through minireel.", "dTimEnd": "2008-03-31T08:30:00+02:00", "dTimStart": "2008-03-31T07:15:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed bleeder valve on top of tension joint running flange to prepare for pressure test.", "dTimEnd": "2008-03-31T09:00:00+02:00", "dTimStart": "2008-03-31T08:30:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Flushed and filled riser while venting air through valve on top of tension joint running flange. Closed valve. Lined up cement unit to standpipe and verified line-up by putting 15 bar on IBOP and opening same.", "dTimEnd": "2008-03-31T10:00:00+02:00", "dTimStart": "2008-03-31T09:00:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressure tested production riser to 20/200 bar 5/10 min - ok. Pumped 680 liter and got full return when bleeding back. Observed for leaks around TBC with ROV - ok. Maintained 20 MT overpull on TBC while performing pressure test.", "dTimEnd": "2008-03-31T11:00:00+02:00", "dTimStart": "2008-03-31T10:00:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Reduced hookload to 107 MT / 10 MT overpull on TBC. Took measurement for contact ring relative to Centralizer deck. Meanwhile pumped corrosion inhibitor in TBC upper piston cavity through hotstab port B.", "dTimEnd": "2008-03-31T11:45:00+02:00", "dTimStart": "2008-03-31T11:00:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Unstabbed hotstab and installed dummy stab in receptacle B. Landed riser guide funnel on F-5 using ROV and tugger support. Installed hatches on all levels in wellhead module for slot F-3 and F-5.", "dTimEnd": "2008-03-31T13:45:00+02:00", "dTimStart": "2008-03-31T11:45:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk prior to installing tensioner assembly.", "dTimEnd": "2008-03-31T14:15:00+02:00", "dTimStart": "2008-03-31T13:45:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Hoisted tension ring and removed nylon guide in Centralizer deck. Installed centralizer and boat collision stool in Centralizer deck. Placed wooden beams on boat collision stool and landed tension ring on top. Installed contact ring below mark on riser contact grooves. Installed and assembled tension assy half hubs with shimms and made up tension ring lock plates. Connected 2 tension cylinders. Elevated tension assembly with tension cylinders and checked contact ring allignement. Made up contact ring. Connected 2 tension cylinders.", "dTimEnd": "2008-03-31T21:30:00+02:00", "dTimStart": "2008-03-31T14:15:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressured up on tension cylinders to 4 x 90 bar (150 MT) and transferred tension from block to tension cylinders on Centralizer deck. Slacked off drillstring to obtain marginal overpull (~1 MT) at cutting height.", "dTimEnd": "2008-03-31T22:15:00+02:00", "dTimStart": "2008-03-31T21:30:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed centralizer assembly in Tensioner deck.", "dTimEnd": "2008-03-31T23:00:00+02:00", "dTimStart": "2008-03-31T22:15:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed Norse cutting equipment on riser. Barriered off Centralizer deck.", "dTimEnd": "2008-04-01T00:00:00+02:00", "dTimStart": "2008-03-31T23:00:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_02
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-01T00:00:00+02:00
2008-04-02T00:00:00+02:00
normal
2018-05-03T13:52:54+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "16.6", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-02T00:00:00+02:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Retrieve annulus isolation sleeve in 10 3/4\" hanger. Retrieve bowl protector and wash multibowl. Run 10 3/4\" tie-back casing and land same on spear. Make up tie-back casing to tie-back adapter. Run adjustment sub running tool and engage same, retract adjustment sub.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3448", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "86", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Installed surface wellhead and tested same. Ran BOP riser joint. Nippled up BOP. Installed diverter and slickjoint. Tested BOP connection and annulus valves against test plug to 345 bar. Made up bowl protector RT.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-01T13:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3508", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-02T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Installed Norse cutting equipment on riser.\n", "dTimEnd": "2008-04-01T00:30:00+02:00", "dTimStart": "2008-04-01T00:00:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cut riser according to Norse procedure. \n\nMeanwhile : \n-Installed flood lights in derrick\n-Varco checked both PRS's with focus on falling objects\n-Painted tuggerchains and control panels on drillfloor\n-Tested Gray valve and FOSVs to 345 bar\n-Brought wellhead to drillfloor", "dTimEnd": "2008-04-01T04:30:00+02:00", "dTimStart": "2008-04-01T00:30:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Released top part of riser when cut obtained. Re-configuered cutting jig with 45 deg blades for machining bevel. Put protective ball on top of cut to avoid swarf falling into well.", "dTimEnd": "2008-04-01T05:15:00+02:00", "dTimStart": "2008-04-01T04:30:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cut 45 deg bevel on riser circumference.", "dTimEnd": "2008-04-01T06:00:00+02:00", "dTimStart": "2008-04-01T05:15:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged down Norse cutting equipment. Removed swarf and smoothed down cut. Marked deck for wellhead orientation.", "dTimEnd": "2008-04-01T07:15:00+02:00", "dTimStart": "2008-04-01T06:00:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Packed and removed cutting equipment. Cleared and tidied wellhead decks.", "dTimEnd": "2008-04-01T08:15:00+02:00", "dTimStart": "2008-04-01T07:15:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled landing stand and laid out handling flange and riser cut off.", "dTimEnd": "2008-04-01T09:00:00+02:00", "dTimStart": "2008-04-01T08:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk prior to lowering WH with dual lift.", "dTimEnd": "2008-04-01T09:15:00+02:00", "dTimStart": "2008-04-01T09:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lowered WH to tensioner deck and landed same on top of riser.", "dTimEnd": "2008-04-01T10:00:00+02:00", "dTimStart": "2008-04-01T09:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Orientated WH with valve stack pointing 45 deg relative to PORT/FWD. Pressure tested BT-seals to 35 bar - ok. Energized plastic in upper annd lower BT seal. Tested seals to 207 bar / 10 min - ok. Locked in 1000 psi after test. Energized slips with cap srews according to Vetco procedure. Pull tested WH with tugger - ok. Installed valves on A and B annulus outlets. Meanwhile loosended bolts on BOP NT-2 connector on stump. Made preparations to run BOP riser joint.", "dTimEnd": "2008-04-01T16:30:00+02:00", "dTimStart": "2008-04-01T10:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk prior to installing BOP riser joint.", "dTimEnd": "2008-04-01T16:45:00+02:00", "dTimStart": "2008-04-01T16:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Ran BOP riser joint using block and dedicated slings and landed on wellhead. Made up NT-2 connector. Retrieved lift slings.", "dTimEnd": "2008-04-01T17:45:00+02:00", "dTimStart": "2008-04-01T16:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk prior to nippling BOP.", "dTimEnd": "2008-04-01T18:00:00+02:00", "dTimStart": "2008-04-01T17:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Nippled up BOP. Meanwhile prepared for installing diverter.", "dTimEnd": "2008-04-01T22:30:00+02:00", "dTimStart": "2008-04-01T18:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk prior to installing slick joint and diverter.", "dTimEnd": "2008-04-01T22:45:00+02:00", "dTimStart": "2008-04-01T22:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed diverter in housing.", "dTimEnd": "2008-04-02T00:00:00+02:00", "dTimStart": "2008-04-01T22:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_03
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-02T00:00:00+02:00
2008-04-03T00:00:00+02:00
normal
2018-05-03T13:52:54+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "16.7", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-03T00:00:00+02:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Run 10 3/4\" tie-back casing. Latch tie-back adapter. Activate adjustment sub. Test upper tie-back with straddle cup tester. Install MS-seal and test same. Pull GTV plug. Rig up for running completion.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3448", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "87", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Installed bowl protector. Retrieved annulus insert in 10 3/4\" hanger. Displaced well to 1,03 sg packer fluid. Made extra washing run to clean tie-back adapter. Retrieved bowl protector. Rig up for running 10 3/4\" tie-back casing.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-02T15:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3508", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-03T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Installed diverter in housing.", "dTimEnd": "2008-04-02T00:30:00+02:00", "dTimStart": "2008-04-02T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Ran slickjoint and landed same on top of BOP. Removed running slings from bails and installed elevator.", "dTimEnd": "2008-04-02T02:15:00+02:00", "dTimStart": "2008-04-02T00:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Function tested BOP shear ram - ok. RIH with test plug for testing BOP connection. Function tested BOP rams and annular - ok. Landed test plug in surface wellhead. Performed line test and verified line up by opening HCR with 35 bar - ok.", "dTimEnd": "2008-04-02T03:30:00+02:00", "dTimStart": "2008-04-02T02:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop activities", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressured up to 35 bar using cement unit - mismatch pumped vs theoretical volume. Suspected pressuring up against GT plug. Opened B-annulus valves to vent underneath plug and pressure dropped immediatly. Leakage observed across test plug despite steady pressure 35 bar indicating that plug did not vent into pipe when doing pressure test. Discussed situation - decided to re-attempt test while keeping B-annulus valves open.", "dTimEnd": "2008-04-02T04:15:00+02:00", "dTimStart": "2008-04-02T03:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Increased pumprate to 50 lpm and put 100 bar differential across plug, leakage decreased and pressure curve indicated that plug was sealing. Achieved steady pressure curve at 100 bar. Bled off pressure to 35 bar and held test for 5 mins (1,7 bar drop / 5 min). Steady fluid returns observed from B-annulus. Pressured up to 345 bar and tested connectors + inner A annulus valve for 10 min - 1,3 bar drop - ok. Shifted valves on A annulus. Held pressure and pressure tested outer A annulus valve for 10 min - 0,7 bar drop - ok. Pumped and bled back 43 liter (35=>345 bar). Still minor fluid returns from B-annulus outlet but gradually decreasing.", "dTimEnd": "2008-04-02T05:15:00+02:00", "dTimStart": "2008-04-02T04:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop activities", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with 5 1/2\" DP stand and test plug. Observed dirt/mud residues plug. Found pieces of steel in the mud residues. Strapped pipe and found landing point 20,45 m vs theoretical 20,81 m - but likely that plug landed too shallow.", "dTimEnd": "2008-04-02T05:30:00+02:00", "dTimStart": "2008-04-02T05:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop activities", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up bowl protector to running tool and made up to stand of 5 1/2\" DP. Meanwhile hooked up tension cylinders on BOP.", "dTimEnd": "2008-04-02T06:00:00+02:00", "dTimStart": "2008-04-02T05:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed bowl protector according to Vetco instructions. POOH with 5 1/2\" DP stand and laid down RT. Meanwhile hooked up BOP tension cylinerders in moonpool.", "dTimEnd": "2008-04-02T08:30:00+02:00", "dTimStart": "2008-04-02T06:00:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk prior to retrieving annulus insert.", "dTimEnd": "2008-04-02T09:00:00+02:00", "dTimStart": "2008-04-02T08:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Checked equipment prior to RIH.", "dTimEnd": "2008-04-02T09:30:00+02:00", "dTimStart": "2008-04-02T09:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up and made up annulus insert J-slot retrieval tool.", "dTimEnd": "2008-04-02T10:30:00+02:00", "dTimStart": "2008-04-02T09:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with retrieval tool on 5 1/2\" HWDP landing string from surface to 76 m MD.", "dTimEnd": "2008-04-02T10:45:00+02:00", "dTimStart": "2008-04-02T10:30:00+02:00", "md": "76", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Mærsk crewchange. Held toolbox talk prior to continuing operation.", "dTimEnd": "2008-04-02T11:00:00+02:00", "dTimStart": "2008-04-02T10:45:00+02:00", "md": "76", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with retrieval tool on 5 1/2\" HWDP landing string from 76 m to 120 m MD. Made up TDS and took torque readings wiith annular closed (200 psi on strip bottle). Torque 0,3-0,6 kNm at 5 rpm.", "dTimEnd": "2008-04-02T12:00:00+02:00", "dTimStart": "2008-04-02T11:00:00+02:00", "md": "120", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Tagged annulus insert at 139,68 m MD. Engaged J-slot and confirmed with 1 MT overpull.", "dTimEnd": "2008-04-02T13:30:00+02:00", "dTimStart": "2008-04-02T12:00:00+02:00", "md": "139.7", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Closed annnular and backed out insert with 3 lefthand turns. Max torque 5 kNm. Observed for pressure build up - none obeserved. Continued backing out annular insert with another 3 lefthand turns - observed 6\" travel - ok.", "dTimEnd": "2008-04-02T14:15:00+02:00", "dTimStart": "2008-04-02T13:30:00+02:00", "md": "139.7", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Opened annular. Attempted to pull free - had 18 MT overpull. Continued rotating left and came free with annular insert.", "dTimEnd": "2008-04-02T14:30:00+02:00", "dTimStart": "2008-04-02T14:15:00+02:00", "md": "139.7", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Flowchecked well - well static.", "dTimEnd": "2008-04-02T15:00:00+02:00", "dTimStart": "2008-04-02T14:30:00+02:00", "md": "138", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Emptied trip tanks. Displaced well to 1,03 sg completion fluid at 1000 lpm. Pumped a total of 26 m3.", "dTimEnd": "2008-04-02T15:45:00+02:00", "dTimStart": "2008-04-02T15:00:00+02:00", "md": "138", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke out TDS. POOH with annular insert on 5 1/2\" HWDP landing string from 138 m MD to surface.", "dTimEnd": "2008-04-02T16:45:00+02:00", "dTimStart": "2008-04-02T15:45:00+02:00", "md": "138", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke out annular insert RT. Worked to free annular insert free from J-slot running tool due to debris jamming the sleeve.", "dTimEnd": "2008-04-02T17:00:00+02:00", "dTimStart": "2008-04-02T16:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk prior to making up Smith 10 3/4\" spear.", "dTimEnd": "2008-04-02T17:15:00+02:00", "dTimStart": "2008-04-02T17:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up spear to 5 1/2\" HWDP (LS-1), checked serial no - ok. Broke spear and inserted 9,632\" nominal grapple. Made up spear using rig tongs.", "dTimEnd": "2008-04-02T18:15:00+02:00", "dTimStart": "2008-04-02T17:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up adjustment sub setting tool to stand of 5 1/2\" HWDP (LS-2), checked serial no - ok.", "dTimEnd": "2008-04-02T19:45:00+02:00", "dTimStart": "2008-04-02T18:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed extra washing trip in order to clean tie-back adapter. Made up bullnose/jet sub. RIH on 5 1/2\" DP from surface to 140 m MD. Stepped up pumps to 3500 lpm / SPP 68 bar. Passed tie-back adapter and pulled back while pumping and rotating with 5 rpm. Pumped a total of 25 m3. Took returns to separate pit. POOH with jet sub.", "dTimEnd": "2008-04-02T21:30:00+02:00", "dTimStart": "2008-04-02T19:45:00+02:00", "md": "140.5", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up bowl protector RT and RIH on stand of 5 1/2\" DP to 20 m. Caught bowl portector and POOH.", "dTimEnd": "2008-04-02T22:00:00+02:00", "dTimStart": "2008-04-02T21:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk prior to rig up 10 3/4\" casing running equipment.", "dTimEnd": "2008-04-02T22:15:00+02:00", "dTimStart": "2008-04-02T22:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cleared and tidied drillfloor prior to bringing in casing running equipment.", "dTimEnd": "2008-04-02T23:15:00+02:00", "dTimStart": "2008-04-02T22:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed BX-3 elevator, changed inserts and function tested same.", "dTimEnd": "2008-04-03T00:00:00+02:00", "dTimStart": "2008-04-02T23:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_04
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-03T00:00:00+02:00
2008-04-04T00:00:00+02:00
normal
2018-05-03T13:52:54+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "17.4", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-04T00:00:00+02:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Activate adjustment sub. Test adjustment sub and tie-back adapter to 380 bar. Test surface tie-back casing to 380 bar. Set MS-seal in casing hanger. Set secondary bowl protector. Drift 10 3/4\" surface casing. Pull GTV plug.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3448", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "88", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Troublehot Mærsk casing tong. Changed to Odfjell casing tong. Troubleshot Odfjell casing tong. Made up and RIH with 10 3/4\" surface tie-back casing. Made up adjustment sub and 10 3/4\" hanger. Engaged spear. Troubleshot TDS torque wrench. RIH and made several attempts to land. Achieved satifactory datum on 4th attempt. Made up tie-back adapter to 10 000 Nm. POOH with spear. Rigged down casing tong and PS-30 slips. ", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[ { "dTim": "2008-04-04T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Moved Mærsk casing tong from drawwork deck storage and moved in front of IR.", "dTimEnd": "2008-04-03T02:00:00+02:00", "dTimStart": "2008-04-03T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Hooked up casing tong. Changed head on PDM to accommodate 10 3/4\" casing. Moved HTS rollers from FWD to AFT end of cantilever. Dressed PS-30 casing with 10 3/4\" inserts/dies. Removed masterbushing and installed PS-30 in rotary. Hooked up PS-30 slip. Programmed and tested casing tong - negative.", "dTimEnd": "2008-04-03T05:00:00+02:00", "dTimStart": "2008-04-03T02:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Troubleshot casing tong / programming.", "dTimEnd": "2008-04-03T05:30:00+02:00", "dTimStart": "2008-04-03T05:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Function tested casing tong - ok.", "dTimEnd": "2008-04-03T06:00:00+02:00", "dTimStart": "2008-04-03T05:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up tie-back adapter and checked seals and acme thread. Installed tie-back adapter in slips. Secured same with dogcollar.", "dTimEnd": "2008-04-03T07:00:00+02:00", "dTimStart": "2008-04-03T06:00:00+02:00", "md": "3", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up first 10 3/4\" joint and stabbed on to tie-back adapter. Had problems with Mærsk casing tong. Not able to get torque/turn curves on computer.", "dTimEnd": "2008-04-03T08:00:00+02:00", "dTimStart": "2008-04-03T07:00:00+02:00", "md": "3", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Investigated problem with casing tong.", "dTimEnd": "2008-04-03T09:00:00+02:00", "dTimStart": "2008-04-03T08:00:00+02:00", "md": "3", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Laid out tie-back adapter. Picked up joint #18 and #17 to test make up with Mærsk casing tong.", "dTimEnd": "2008-04-03T09:30:00+02:00", "dTimStart": "2008-04-03T09:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Attempted to make up connection, investigated missing torque reading on Mærsk system. Traced fault to be load cell or load cell amplifier.", "dTimEnd": "2008-04-03T11:45:00+02:00", "dTimStart": "2008-04-03T09:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Laid out jont #18 and #17 due to overtorque.", "dTimEnd": "2008-04-03T12:15:00+02:00", "dTimStart": "2008-04-03T11:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Rigged down Mærsk casing tong and frame.", "dTimEnd": "2008-04-03T14:00:00+02:00", "dTimStart": "2008-04-03T12:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Rigged up Odfjell casing tong and installed in rails in front of IR. Meanwhile held tollbox talk for re-installing safety net on FWD PRS.", "dTimEnd": "2008-04-03T15:45:00+02:00", "dTimStart": "2008-04-03T14:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Re-installed safety net around FWD PRS.", "dTimEnd": "2008-04-03T18:15:00+02:00", "dTimStart": "2008-04-03T15:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Powered up OWS casing tong. Installed travle cylinder.", "dTimEnd": "2008-04-03T19:15:00+02:00", "dTimStart": "2008-04-03T18:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Picked up tie-back connector and installed same in slips. Picked up 1 st joint and attempted to make up to tie-back adapter - not able to get torque/turn curve on Odfjell computer. Trouble shot situation. Changed gauges and valve on Odfjell tong.", "dTimEnd": "2008-04-03T21:00:00+02:00", "dTimStart": "2008-04-03T19:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "RIH with 10 3/4\" tie-back casing from surface to 108 m MD according to tally.", "dTimEnd": "2008-04-03T23:00:00+02:00", "dTimStart": "2008-04-03T21:00:00+02:00", "md": "108", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up and made up 10 3/4\" hanger / adjustable sub assy. Landed hanger in slips. Broke off casing hanger handling tool. Checked casing hanger. Changed from BX3 to 5 1/2\" BX elevator.", "dTimEnd": "2008-04-04T00:00:00+02:00", "dTimStart": "2008-04-03T23:00:00+02:00", "md": "119", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_05
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-04T00:00:00+02:00
2008-04-05T00:00:00+02:00
normal
2018-05-03T13:52:54+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "17.9", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-05T00:00:00+02:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Set 10 3/4 MS seal.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3448", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "89", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Changed die holders in TDS. Ran adjustment sub activation tool and retracted adjustment sub. Tested metal seal in adjustment sub to 380 bar. Rigged up casing running equipment to run hanger RT. Observed dropped object on drilfloor - suspended operations for investigation and repair work on aft PRS. RIH with hanger RT on 10 3/4\" casing.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[ { "dTim": "2008-04-05T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Picked up pre-made 5 1/2\" HWDP (LS-1) with 10 3/4\" Itco spear with PRS. Attempted to make up stand to TDS - negative - slipped in TDS back up dies.", "dTimEnd": "2008-04-04T00:15:00+02:00", "dTimStart": "2008-04-04T00:00:00+02:00", "md": "119", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke off TDS from stand. Set down stand in PRS. Lowered TDS and inspected torque wrench dies, removed swarf from dies. Re-attempted make up to stand in TDS - ok.", "dTimEnd": "2008-04-04T01:15:00+02:00", "dTimStart": "2008-04-04T00:15:00+02:00", "md": "119", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Ran 10 3/4\" Itco spear 3 m into 10 3/4\" tie-back casing and latched same. Took up/down weight 82/79 MT. RIH with tie-back casing on 5 1/2\" HWDP (LS-1). Put meter marks from casing hanger landing shoulder. Tagged with 4 MT at ~139,4 m, i.e. 30-40 cm shallow - no colour marks observed in WH B-annulus outlet. Re-attempted tag - same depth.", "dTimEnd": "2008-04-04T01:30:00+02:00", "dTimStart": "2008-04-04T01:15:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Evaluated situation. Checked drawings for potential hang-ups. Checked tally and joints left on deck - ok. Made two attempt to index pipe before tagging again - same depth. Sudden overpull of 14 MT observed after pulling some 30 cm above tag depth.", "dTimEnd": "2008-04-04T02:30:00+02:00", "dTimStart": "2008-04-04T01:30:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Decided to attempt to screw in 1-2 turn in order to verify tie-back adapter depth. RIH and tagged approx 10 cm deeper than earlier. Observed lower orange and white band in B-annulus outlet. Measured required distance for adjustment sub travel (15\") and decieded to continue according to plan.", "dTimEnd": "2008-04-04T03:15:00+02:00", "dTimStart": "2008-04-04T02:30:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Set torqe limit to 2700 Nm. Made 3 attempts to enter tie-back adapter. Entered tie-back adapter on 4th attempt and observed weight increasing about 3-4 MT for each turn. Slacked off to neutral (80 MT) for each turn achieved. String stalled out at 2700 Nm after 5+ turns achieved. Took 10 MT overpull. Rotated at 1 rpm. Attempted make up to 10 000 Nm (optimum torque) - spear started to slip at 5500 Nm. Re-engaged spear. Adjusted torque setting to minimum torque 6600 Nm -spear started to slip at 5500 Nm. Re-enaged spear. Set torque limit to 10 000 Nm, increased rotation to 3 RPM. String stalled out on 10 000 NM (optimum torque) - ok.", "dTimEnd": "2008-04-04T04:15:00+02:00", "dTimStart": "2008-04-04T03:15:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Took 30 MT overpull to check pre-tension in casing towards datum. Streched pipe approx 2\" and observed lower white band through B-annulus outlet.", "dTimEnd": "2008-04-04T04:45:00+02:00", "dTimStart": "2008-04-04T04:15:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged down Odfjell casing tong and removed PS-30 slips. Installed masterbushing and bowl.", "dTimEnd": "2008-04-04T06:00:00+02:00", "dTimStart": "2008-04-04T04:45:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Jammed torque wrench on TDS. Inspected equipment and found that wrong die-holders had been installed. Changed die-holders.", "dTimEnd": "2008-04-04T09:00:00+02:00", "dTimStart": "2008-04-04T06:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Held toolbox talk prior to picking up adjustment sub activation tool.", "dTimEnd": "2008-04-04T09:15:00+02:00", "dTimStart": "2008-04-04T09:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with adjustment sub and located same at 28,4 m MD. Checked serial numbers on pipe. Made up TDS.", "dTimEnd": "2008-04-04T10:15:00+02:00", "dTimStart": "2008-04-04T09:15:00+02:00", "md": "28", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressured up on drillpipe to 140 bar to activate horizontal dogs. Pulled back 0,4 m and confirmed engaged in vertical dog profile by 9 MT overpull. Rotated string with 22 righthand turns. Observed colored band through B-annulus outlet to confirm adjustment sub collapsing. Increased overpull to 30 MT and continued rotating until TDS stalled out on 9 kNm and overpull reduced. Slacked off string to 28,4 m MD mark and waited for 2 min. Bleed off pressure on DP. Obtained a total of 17\" travel on adjustment sub.", "dTimEnd": "2008-04-04T11:00:00+02:00", "dTimStart": "2008-04-04T10:15:00+02:00", "md": "28", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with adjustment sub activation tool and racked back in derrick.", "dTimEnd": "2008-04-04T11:45:00+02:00", "dTimStart": "2008-04-04T11:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up Drillquip straddle cup tester.", "dTimEnd": "2008-04-04T12:00:00+02:00", "dTimStart": "2008-04-04T11:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with straddle cup tester and located same at 28,4 m MD across metal seal in adjustment sub. Meanwhile held toolbox talk for pressure testing.", "dTimEnd": "2008-04-04T12:30:00+02:00", "dTimStart": "2008-04-04T12:00:00+02:00", "md": "28", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up cement unit on standpipe. Performed line test to 380 bar.", "dTimEnd": "2008-04-04T13:00:00+02:00", "dTimStart": "2008-04-04T12:30:00+02:00", "md": "28", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressure tested adjustment sub (metal seal) to 380 bar / 10 min - ok. Kept B-annulus open throughout test.", "dTimEnd": "2008-04-04T14:30:00+02:00", "dTimStart": "2008-04-04T13:00:00+02:00", "md": "28", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with straddle cup tester from 28,4 m and located same across tie-back adpater at 140,5 m MD.", "dTimEnd": "2008-04-04T15:00:00+02:00", "dTimStart": "2008-04-04T14:30:00+02:00", "md": "140.5", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Filled pipe with approx 1,8 m3 packer fluid prior to testing. Pressured up to 380 bar - observed leakage from B-annulus outlet - not able to obtain test.", "dTimEnd": "2008-04-04T16:00:00+02:00", "dTimStart": "2008-04-04T15:00:00+02:00", "md": "140.5", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled back 10 m to put cuptester in blank pipe to test tool. Pressured up - not able to obtain test - straddle cup test leaking.", "dTimEnd": "2008-04-04T16:15:00+02:00", "dTimStart": "2008-04-04T16:00:00+02:00", "md": "130.5", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with straddle cup tester from 130,5 m MD to surface. Laid out cup tester and inspected same. Found no tears or flaws, but OD reduced significantly (9,85\"/9,70\" vs originally 10,13\")", "dTimEnd": "2008-04-04T17:30:00+02:00", "dTimStart": "2008-04-04T16:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk prior to rigging casing running equipment.", "dTimEnd": "2008-04-04T17:45:00+02:00", "dTimStart": "2008-04-04T17:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged up casing running equipment. Found a yellow sheared allen bolt on walkway along drillfloor. Suspended operation and evaluated situation.", "dTimEnd": "2008-04-04T18:00:00+02:00", "dTimStart": "2008-04-04T17:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Isolated aft PRS and TDS and inspected same with manrider. Found origin of bolthead to be from backside of aft PRS upper grip head.", "dTimEnd": "2008-04-04T20:00:00+02:00", "dTimStart": "2008-04-04T18:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Parked aft PRS for repair. Performed repair work on aft PRS. Broke out and re-thightended in total 24 allen/hex bolts with prescribed momentum (600 ft lbs). Replaced broken bolt. \n\nMeanwhile :\n-Installed BX3 elevator in bails\n-Brought Vetco/BOT equipment to cantilever", "dTimEnd": "2008-04-05T00:00:00+02:00", "dTimStart": "2008-04-04T20:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" } ]
[]
15_9_F_4_2008_04_06
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-05T00:00:00+02:00
2008-04-06T00:00:00+02:00
normal
2018-05-03T13:52:54+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "18.8", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-06T00:00:00+02:00", "dTimDiaHoleStart": "2008-03-19T21:00:00+01:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Run bowl protector in surface WH. Drift 10 3/4\" casing to 600 m MD. Pull GTV plug at 615 m MD. Pull bowl protector. Prepare for running completion.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3448", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "90", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Landed 10 3/4\" casing hanger running tool. Pressure tested upper tie-back casing against GTV plug to 380 bar - ok. Suspended operations due to exhaust fumes on drillfloor. Meanwhile cleaned in drilling areas. Shut down gas turbines. Pulled 10 3/4\" casing hanger RT. Rigged down casing running equipment. Dropped object on drillfloor - suspended operations. Secured and isolated aft PRS. Resumed operations. Made up MS-seal running tool. Function tested tool.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-05T16:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "3510", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-06T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Repaired aft PRS. Meanwhile prepared for rigging casing running equipment.", "dTimEnd": "2008-04-05T02:30:00+02:00", "dTimStart": "2008-04-05T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Rigged up Odfjell casing tong adn PS-30 slips dressed for 10 3/4\" casing.", "dTimEnd": "2008-04-05T03:45:00+02:00", "dTimStart": "2008-04-05T02:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk for running 10 3/4\" hanger running tool on 10 3/4\" casing.", "dTimEnd": "2008-04-05T04:00:00+02:00", "dTimStart": "2008-04-05T03:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up 10 3/4\" x 1502 swedge to 8 m 10 3/4\" casing joint. Laid out casing joint.", "dTimEnd": "2008-04-05T05:00:00+02:00", "dTimStart": "2008-04-05T04:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Suspended operation due to reported fumes. Wind direction 330. Assessed situation. Decided to resume operation.", "dTimEnd": "2008-04-05T05:30:00+02:00", "dTimStart": "2008-04-05T05:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up 10 3/4\" casing hanger RT and hung off in slips. Picked up joint of 10 3/4\" casing and made up to RT. Picked up joint with pre-made swedge.", "dTimEnd": "2008-04-05T06:00:00+02:00", "dTimStart": "2008-04-05T05:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up pup joint with pre-made 1502 swedge. RIH and landed casing hanger RT at 20 m MD. Set of weight of landing string. Entered hanger RT threads using chain tong. Made up RT with 9 lefthand turns using casing tong.", "dTimEnd": "2008-04-05T07:00:00+02:00", "dTimStart": "2008-04-05T06:00:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk prior to pressure testing.", "dTimEnd": "2008-04-05T07:15:00+02:00", "dTimStart": "2008-04-05T07:00:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged up 1502 chicksan from swedge to cement hose hub on drillfloor.", "dTimEnd": "2008-04-05T08:00:00+02:00", "dTimStart": "2008-04-05T07:15:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up to cement pump and flushed lines. Performed line test to 380 bar - ok. Exhaust fumes detected on drillfloor.", "dTimEnd": "2008-04-05T08:45:00+02:00", "dTimStart": "2008-04-05T08:00:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressured up on cement unit and tested upper tie-back/adjustment sub/tie-back adapter to 380 bar /10 min - ok. Pumped and bled back 587 litres.", "dTimEnd": "2008-04-05T09:30:00+02:00", "dTimStart": "2008-04-05T08:45:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Exhaust fumes on drillfoor and drillers cabin. Suspended drillfloor operations. Checked wind and conditions every 30 min. Monitored well from shaker control room.\n\nMeanwhile :\n-Cleaned and tidied in moonpool\n-Cleaned and tidied in wellhead module\n-Housekeeping in heavy tool store\n\n21:30 - shut down gas turbines to get working conditions on drillfloor.", "dTimEnd": "2008-04-05T21:30:00+02:00", "dTimStart": "2008-04-05T09:30:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Resumed work on drillfloor. Broke out casing hanger RT with 10 turns. Unable to latch elevator on 10 3/4\" casing, had to use singel joint elevator and tugger. Pulled 10 3/4\" landing string. Broke out RT. Broke out 1502 swedge.", "dTimEnd": "2008-04-05T23:45:00+02:00", "dTimStart": "2008-04-05T21:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged down casing tong.", "dTimEnd": "2008-04-06T00:00:00+02:00", "dTimStart": "2008-04-05T23:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_07
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-06T00:00:00+02:00
2008-04-07T00:00:00+02:00
normal
2018-05-03T13:52:54+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "19.4", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-07T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-06T09:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "RIH to 615 m MD and pull GTV plug, POOH. Pull bowl protector. Prepare for running 7\" tubing. Run 7\" tubing.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3448", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "91", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Set and tested MS seal - ok. Ran bowl protector in WH. Troubleshot PDM. Ran drift to 580 m MD using DP singles. Dropped object on drillfloor simmer/lock ring. Investigated and found source to be Cherrypicker. RIH with GTV pulling tool to 130 m MD using DP singles.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-06T16:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "3510", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-07T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Rigged down casing tong. Removed PS-30 slips. Observed dropped object on drillfloor - hex/allen bolt head from aft PRS. Suspended operations for investigation. Fenced off drillfloor.", "dTimEnd": "2008-04-06T00:30:00+02:00", "dTimStart": "2008-04-06T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Inspected aft PRS. Discussed way forward. Parked and isolated aft PRS. Secured backside of aft PRS gripper head with cover and trailer straps for dropped object prevention.", "dTimEnd": "2008-04-06T03:00:00+02:00", "dTimStart": "2008-04-06T00:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Resumed operations. Removed BX3 elevator and installed 5 1/2\" DP elevator. Cleared drillfloor from casing handing equipment.", "dTimEnd": "2008-04-06T03:45:00+02:00", "dTimStart": "2008-04-06T03:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Ran 2 x 5 1/2\" DP singels and made up to MS-seal running tool. Meanwhile laid out DP singels on deck to cater for continued operations.", "dTimEnd": "2008-04-06T04:45:00+02:00", "dTimStart": "2008-04-06T03:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up control lines to MS-seal RT. Function tested and adjusted dogs and stroke on MS seal RT.", "dTimEnd": "2008-04-06T06:00:00+02:00", "dTimStart": "2008-04-06T04:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Locked MS seal running tool in surface WH, observed 0,4 l return - ok. Performed 10 MT overpull to confirm latch - ok. Set MS seal assembly by applying 4300 psi. Observed 1,62\" travel / 3,5 liter returned fluid - ok.", "dTimEnd": "2008-04-06T07:00:00+02:00", "dTimStart": "2008-04-06T06:00:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressure tested MS seal through test port in surface wellhead to 380 bar / 10 min - ok.", "dTimEnd": "2008-04-06T07:45:00+02:00", "dTimStart": "2008-04-06T07:00:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Released dogs in MS seal RT by rotating 5 turns to the right.", "dTimEnd": "2008-04-06T08:15:00+02:00", "dTimStart": "2008-04-06T07:45:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with MS seal RT on 5 1/2\" DP stand. Broke RT tool and laid down.", "dTimEnd": "2008-04-06T09:00:00+02:00", "dTimStart": "2008-04-06T08:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbx talk before running bowl protector.", "dTimEnd": "2008-04-06T09:15:00+02:00", "dTimStart": "2008-04-06T09:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up bowl protector RT. RIH and set bowl protector at 20,10 m MD.", "dTimEnd": "2008-04-06T10:00:00+02:00", "dTimStart": "2008-04-06T09:15:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke out RT and laid down same. Laid out 2 joints of 5 1/2\" DP.", "dTimEnd": "2008-04-06T10:45:00+02:00", "dTimStart": "2008-04-06T10:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk and prepared for running casing drift. Experienced problems with programming PDM.", "dTimEnd": "2008-04-06T11:30:00+02:00", "dTimStart": "2008-04-06T10:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Troubleshot PDM. Unable to travel to port aft pipe bay.", "dTimEnd": "2008-04-06T13:15:00+02:00", "dTimStart": "2008-04-06T11:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Tested PDM - ok. Tested stabbing. Discussed issues related to pipe handling.", "dTimEnd": "2008-04-06T14:00:00+02:00", "dTimStart": "2008-04-06T13:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up 9,567\" casing drift and made up to 5 1/2\" HWDP single.", "dTimEnd": "2008-04-06T14:15:00+02:00", "dTimStart": "2008-04-06T14:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 9,567\" casing drift from surface to 140 m MD on 5 1/2\" HWDP singels. Re-arranged pipe on cantilever deck.", "dTimEnd": "2008-04-06T17:15:00+02:00", "dTimStart": "2008-04-06T14:15:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 9,567\" casing drift from 140 m to 245 m MD on 5 1/2\" DP singles. Detected exhaust fumes on drillfloor.", "dTimEnd": "2008-04-06T18:15:00+02:00", "dTimStart": "2008-04-06T17:15:00+02:00", "md": "245", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Exhaust fumes on drillfloor. Made up TDS and spaced out for BOP. Abandoned drillfloor. Shut down one of the gas turbines to reduce exhaust fumes.", "dTimEnd": "2008-04-06T19:15:00+02:00", "dTimStart": "2008-04-06T18:15:00+02:00", "md": "245", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Resumed operations. Continued to RIH with 9,567\" drift from 245 m to 580 m MD.", "dTimEnd": "2008-04-06T21:45:00+02:00", "dTimStart": "2008-04-06T19:15:00+02:00", "md": "580", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with 9,567\" drift on 5 1/2\" DP from 580 m to 223 m MD. Laid out singles on deck when pulling out. Performed kick drill.", "dTimEnd": "2008-04-07T00:00:00+02:00", "dTimStart": "2008-04-06T21:45:00+02:00", "md": "223", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_08
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-07T00:00:00+02:00
2008-04-08T00:00:00+02:00
normal
2018-05-03T13:52:55+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "19.7", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-08T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-07T20:45:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Run 7\" tubing to 2000 m MD.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3448", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "92", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Retrieved GTV plug at 615 m MD. Retrieved secondary bowl protector in surface wellhead. Prepared for running 7\" tubing and rigged up tubing handling equipment. Ran completion assemblies. Ran 7\" tubing to 72 m MD.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-07T16:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "3510", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-08T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "POOH with 9,567\" drift on 5 1/2\" HWDP from 223 m to surface. Laid out singles on deck when pulling out. Observed dropped object on drillfloor - half crest of external lock ring / simmer ring for pin, 70 mm x 2 mm / 10 grammes. Suspended operations for investigation. Fenced off drillfloor.", "dTimEnd": "2008-04-07T02:00:00+02:00", "dTimStart": "2008-04-07T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Inspected rig equipment. Found source of dropped object to be cherry picker main hydraulic lift cylinder. No risk of larger dropped object from equipment - lock ring served no purpose.", "dTimEnd": "2008-04-07T02:45:00+02:00", "dTimStart": "2008-04-07T02:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Resumed operations. Held toolbox talk. Made up GTV pulling tool to stand of drillpipe hanging in block. Ran stand carefully through BOP. RIH to 80 m MD on 5 1/2\" HWDP singles. Observed leakage on BX-elevator.", "dTimEnd": "2008-04-07T04:00:00+02:00", "dTimStart": "2008-04-07T02:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Fixed BX elevator. Changed 3 ea hydraulic hoses/fittings running from TDS to BX elevator.", "dTimEnd": "2008-04-07T05:30:00+02:00", "dTimStart": "2008-04-07T04:00:00+02:00", "md": "80", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "RIH with GTV pulling tool from 80 m to 130 m MD on 5 1/2\" HWDP singles.", "dTimEnd": "2008-04-07T06:00:00+02:00", "dTimStart": "2008-04-07T05:30:00+02:00", "md": "130", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with GTV pulling tool from 130 m to 600 m MD on 5 1/2\" singles.", "dTimEnd": "2008-04-07T09:00:00+02:00", "dTimStart": "2008-04-07T06:00:00+02:00", "md": "600", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Tagged plug with 2 MT at 615 m MD.", "dTimEnd": "2008-04-07T09:30:00+02:00", "dTimStart": "2008-04-07T09:00:00+02:00", "md": "615", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled back 1 joint and made up DP to TDS. Displaced his-vis at 2400 lpm. Pumped a total of 37 m3 1,03 sg completion fluid.", "dTimEnd": "2008-04-07T10:30:00+02:00", "dTimStart": "2008-04-07T09:30:00+02:00", "md": "615", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk prior to releasing plug.", "dTimEnd": "2008-04-07T10:45:00+02:00", "dTimStart": "2008-04-07T10:30:00+02:00", "md": "615", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Due to unsactisfactory cleanliness of completion fluid, pumped additional 26 m3 at 2400 lpm.", "dTimEnd": "2008-04-07T11:15:00+02:00", "dTimStart": "2008-04-07T10:45:00+02:00", "md": "615", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Latched onto plug and confirmed by 10 MT overpull. No pressure observed on standpipe but slight gain in triptank indicating equlized plug. Rotated at 5 rpm righthand while holding 3 MT overpull, released plug with 10 turns, no gain observed. Pulled back 5 m and waited for elastomer element to relax.", "dTimEnd": "2008-04-07T12:00:00+02:00", "dTimStart": "2008-04-07T11:15:00+02:00", "md": "610", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with plug to 620 m MD to confirm released. Pulled 5 1/2\" single and gained 0,2 m3 in trip tank due to swabbing plug.", "dTimEnd": "2008-04-07T12:30:00+02:00", "dTimStart": "2008-04-07T12:00:00+02:00", "md": "610", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled 3 x 5 1/2\" singles while pumping at 200 lpm. Swabbing stopped when plug entered 10 3/4\" casing.", "dTimEnd": "2008-04-07T14:00:00+02:00", "dTimStart": "2008-04-07T12:30:00+02:00", "md": "578", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with GTV plug on 5 1/2\" DP singles from 578 m to 145 m MD.", "dTimEnd": "2008-04-07T17:15:00+02:00", "dTimStart": "2008-04-07T14:00:00+02:00", "md": "145", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with GTV plug on 5 1/2 HWDP singles from 145 m MD to surface.", "dTimEnd": "2008-04-07T20:15:00+02:00", "dTimStart": "2008-04-07T17:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke out and laid down GTV plug and pulling tool.", "dTimEnd": "2008-04-07T20:45:00+02:00", "dTimStart": "2008-04-07T20:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up secondary bowl protector pulling tool. RIH and latched secondary bowl protector. Strapped pipe while POOH, measured 20,45 m to tubing hanger landing shoulder. Made up kick assembly.", "dTimEnd": "2008-04-07T22:30:00+02:00", "dTimStart": "2008-04-07T20:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk for rigging up tubing running equipment.", "dTimEnd": "2008-04-07T22:45:00+02:00", "dTimStart": "2008-04-07T22:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Positioned HTS and moved rollers on cantilever. Cleared drillfloor. Positioned control line reel on fwd pipe setback. Meanwhile installed NPR plug with ballseat in tailpipe joint.", "dTimEnd": "2008-04-08T00:00:00+02:00", "dTimStart": "2008-04-07T22:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_09
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-08T00:00:00+02:00
2008-04-09T00:00:00+02:00
normal
2018-05-03T13:52:55+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "20", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-09T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-07T20:45:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Run 7\" tubing to 2164 m MD. Install DHSV. Space out towards PBR at 2661 m MD and TH landing point. Install tubing hanger.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3448", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "93", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Investigated problems with casing tong transducer. POOH with 5 tubing joints and SB-3 injection packer. RIH with back-up packer assy. Investigated faulty torque setting on casing tong. Drifted 2 tubing couplings with 5,98\"/5,8\" drift to verify plug retrieval. Ran 7\" tubing to 750 m MD.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-08T16:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "3510", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-09T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Re-arranged kick joint. Re-booted PDM and tested same.", "dTimEnd": "2008-04-08T00:30:00+02:00", "dTimStart": "2008-04-08T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Changed to BX3 elevator. Positioned Odfjell casing tong on rails in front of IR, hooked up same to panel on aft pipe setback. Removed master bushing and installed PS-30 slips. Bulit scaffolding platforms for dropped object protection above tong operating panel and control line reel panel.", "dTimEnd": "2008-04-08T03:30:00+02:00", "dTimStart": "2008-04-08T00:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk before running 7\" tubing.", "dTimEnd": "2008-04-08T03:45:00+02:00", "dTimStart": "2008-04-08T03:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up completion assy#1. Function tested ratcheting mule shoe - ok. Checked seals and rupture disk - ok. Hung off assy#1 in slips. Picked up and made up joint #265 with presintalled NPR plug / ball seat 1,98 m from collar. Picked up and made up 1 joint of tubing. Picked up and made up completion assy#2 / SB-3 injection packer. Checked packer element and slips.", "dTimEnd": "2008-04-08T05:00:00+02:00", "dTimStart": "2008-04-08T03:45:00+02:00", "md": "37", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 7\" 29# S13%Cr tubing from 37 m to 72 m MD. Checked self filling of tubing - ok. Raised doubt about torque read back on jam computer.", "dTimEnd": "2008-04-08T06:00:00+02:00", "dTimStart": "2008-04-08T05:00:00+02:00", "md": "72", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Investigated deviation between tong gauge and jam coumputer. Found that wrong transducer was set up in the jam computer, with the consequence that the casing tong output too low torque.", "dTimEnd": "2008-04-08T07:30:00+02:00", "dTimStart": "2008-04-08T06:00:00+02:00", "md": "85", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Held toolbox talk prior to laying out undertorqued tubing. Laid out tubing joints #258 to #262.", "dTimEnd": "2008-04-08T09:30:00+02:00", "dTimStart": "2008-04-08T07:30:00+02:00", "md": "31", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Installed pipe guide in PS-30 slips.", "dTimEnd": "2008-04-08T09:45:00+02:00", "dTimStart": "2008-04-08T09:30:00+02:00", "md": "31", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Inspected box on joint #263 and found it to be damaged / gaulled. Broke off box and inspected pin thread - ok. Made up new coupling collar on joint#263 - ok.", "dTimEnd": "2008-04-08T10:30:00+02:00", "dTimStart": "2008-04-08T09:45:00+02:00", "md": "31", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Held toolbox talk prior to making up back-up assy#2 SB-3 injection packer.", "dTimEnd": "2008-04-08T10:45:00+02:00", "dTimStart": "2008-04-08T10:30:00+02:00", "md": "31", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Picked up and made up back-up assy#2 SB-3 injection packer, RIH and hung off in slips.", "dTimEnd": "2008-04-08T11:45:00+02:00", "dTimStart": "2008-04-08T10:45:00+02:00", "md": "36", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Picked up and made up 7\" tubing joint. Raised doubt about torque setting on tong. Stopped operations for investigation.", "dTimEnd": "2008-04-08T12:15:00+02:00", "dTimStart": "2008-04-08T11:45:00+02:00", "md": "48", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Found casing tong to be programmed with wrong torque values. Optimum torque set to 15660 ft lbs instead of 15660 Nm. Two tubing connections on assy#2 overtorqued. No back-up assembly available. Discussed situation. Evaluated and discussed further actions with town. Got confirmation that VamTop thread should be good within 30% overtorque. Decided to do drift run through overtorqued couplings to verify no deformation or restrictions. \n\nMeanwhile :\n-Repaired handrails and kick plates in derrick\n-Removed 10 allen/hex bolts from fwd PRS", "dTimEnd": "2008-04-08T19:00:00+02:00", "dTimStart": "2008-04-08T12:15:00+02:00", "md": "48", "phase": "fixed", "proprietaryCode": "interruption -- repair", "state": "ok", "stateDetailActivity": "operation failed" }, { "comments": "Rigged up tugger with Seawell adjustable drift sub. Performed drift run through 1st coupling (13,2 m) to 5,977\" - ok. Perfomed drift run through assy#2 and 2nd coupling (21,2 m) to 5,80\" - ok.", "dTimEnd": "2008-04-08T20:45:00+02:00", "dTimStart": "2008-04-08T19:00:00+02:00", "md": "48", "phase": "fixed", "proprietaryCode": "interruption -- repair", "state": "ok", "stateDetailActivity": "operation failed" }, { "comments": "Held toolbox talk prior to continuing tubing running. Verified Odfjell jam computer with correct torque values.", "dTimEnd": "2008-04-08T21:00:00+02:00", "dTimStart": "2008-04-08T20:45:00+02:00", "md": "48", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 7\" 29# S13%Cr tubing from 48 m to 238 m MD. Running speed 30 sec per joint. Checked self filling of tubing - ok.", "dTimEnd": "2008-04-09T00:00:00+02:00", "dTimStart": "2008-04-08T21:00:00+02:00", "md": "238", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_10
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-09T00:00:00+02:00
2008-04-10T00:00:00+02:00
normal
2018-05-03T13:52:55+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "20.6", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-10T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-07T20:45:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "RIH with 7\" tubing to 2661 m MD. Space out tubing. Install tubing hanger. Land tubing hanger in surface wellhead.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3448", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "94", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Ran 7\" tubing from 750 m to 2164 m MD. Picked up and made up completion assy#3 DHSV.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-09T16:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "3510", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-10T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "RIH with 7\" 29# S13%Cr tubing from 238 m to 561 m MD. Running speed 30 sec per joint. Checked self filling of tubing - ok.", "dTimEnd": "2008-04-09T02:45:00+02:00", "dTimStart": "2008-04-09T00:00:00+02:00", "md": "561", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Handover for short change of Mærsk crew. Held toolbox talk for continued operations. Greased PS-30 and elevator.", "dTimEnd": "2008-04-09T03:15:00+02:00", "dTimStart": "2008-04-09T02:45:00+02:00", "md": "561", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 7\" 29# S13%Cr tubing from 561 m to 750 m MD. Reduced running speed to 1 min per joint in 9 5/8\" casing. Checked self filling of tubing - ok.", "dTimEnd": "2008-04-09T06:00:00+02:00", "dTimStart": "2008-04-09T03:15:00+02:00", "md": "750", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 7\" 29# S13%Cr tubing from 750 m to 834 m MD.", "dTimEnd": "2008-04-09T06:45:00+02:00", "dTimStart": "2008-04-09T06:00:00+02:00", "md": "834", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Bad make up on joint #189, laid out same. Broke out box on joint #190. Inspected pin and made up new box on joint #190. Moved mobile cherry picker to aft part of drillfloor for use on aft PRS.", "dTimEnd": "2008-04-09T08:00:00+02:00", "dTimStart": "2008-04-09T06:45:00+02:00", "md": "834", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 7\" 29# S13%Cr tubing from 834 m to 963 m MD.", "dTimEnd": "2008-04-09T10:00:00+02:00", "dTimStart": "2008-04-09T08:00:00+02:00", "md": "963", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Bad make up on joint #177, laid out same. Broke out box on joint #178. Inspected pin and made up new box on joint #178.", "dTimEnd": "2008-04-09T10:45:00+02:00", "dTimStart": "2008-04-09T10:00:00+02:00", "md": "963", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 7\" 29# S13%Cr tubing from 963 m to 1345 m MD.", "dTimEnd": "2008-04-09T15:00:00+02:00", "dTimStart": "2008-04-09T10:45:00+02:00", "md": "1345", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Not able to make up joint #146, laid out same. Inspected box - negative. Laid out joint 145.", "dTimEnd": "2008-04-09T16:15:00+02:00", "dTimStart": "2008-04-09T15:00:00+02:00", "md": "1333", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 7\" 29# S13%Cr tubing from 1333 m to 1434 m MD.", "dTimEnd": "2008-04-09T17:45:00+02:00", "dTimStart": "2008-04-09T16:15:00+02:00", "md": "1434", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Inspected threads on joint #134 - negative - laid out joint.", "dTimEnd": "2008-04-09T18:00:00+02:00", "dTimStart": "2008-04-09T17:45:00+02:00", "md": "1434", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 7\" 29# S13%Cr tubing from 1434 m to 1455 m MD.", "dTimEnd": "2008-04-09T18:30:00+02:00", "dTimStart": "2008-04-09T18:00:00+02:00", "md": "1455", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Inspected threads on joint #129 - negative - laid out joint. Mærsk crew change and toolbox talk.", "dTimEnd": "2008-04-09T19:45:00+02:00", "dTimStart": "2008-04-09T18:30:00+02:00", "md": "1455", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 7\" 29# S13%Cr tubing from 1455 m to 1743 m MD.", "dTimEnd": "2008-04-10T00:00:00+02:00", "dTimStart": "2008-04-09T19:45:00+02:00", "md": "1743", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_11
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-10T00:00:00+02:00
2008-04-11T00:00:00+02:00
normal
2018-05-03T13:52:55+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "21", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-11T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-07T20:45:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Test control line thru TH. MU communication collar and tubing hanger RT. Land tubing hanger in surface wellhead. Perform low pressure tubing leak test and function test of TRSCSSV. Set production packer and leak test tubing to 245 bar. Inflow test TRSCSSV. Run BPV and set in tubing hanger.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "95", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "RIH with 7\" tubing from 2164 m to 2661 m MD. Entered 7\" liner PBR with lower most seal on seal stem at 2664.3 m. Spaced out tubing. Installed tubing hanger. Terminated control line.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-10T15:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-11T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "RIH with 7\" 29# S13%Cr tubing from 1743 m to 1938 m MD.", "dTimEnd": "2008-04-10T01:45:00+02:00", "dTimStart": "2008-04-10T00:00:00+02:00", "md": "1938", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Bad make up on joint #90, laid out same. Washed and inspected threads on pipedeck. Applied API mod lubeseal dope to pin ends on pipedeck.", "dTimEnd": "2008-04-10T02:30:00+02:00", "dTimStart": "2008-04-10T01:45:00+02:00", "md": "1938", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 7\" 29# S13%Cr tubing from 1938 m to 2164 m MD.", "dTimEnd": "2008-04-10T05:15:00+02:00", "dTimStart": "2008-04-10T02:30:00+02:00", "md": "2164", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk prior to picking up completion assy#3 DHSV. Counted joints left on deck 84 - ok.", "dTimEnd": "2008-04-10T05:30:00+02:00", "dTimStart": "2008-04-10T05:15:00+02:00", "md": "2164", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up completion assy#3 DHSV. Made up completion assy#3 and ran through RT. Isolated pipe guides on PS-30 slips.\n", "dTimEnd": "2008-04-10T06:00:00+02:00", "dTimStart": "2008-04-10T05:30:00+02:00", "md": "2164", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "PU and installed one tubing joint above TRSCSSV assembly. Flushed control line. Connected control line to TRSCSSV and leak tested to 570 bar/10 min. Bled pressure down to zero. Checked slips alignement. Made guide arrangement for control line from tubing to CL drum. Pressured up control line to 420 bar to keep TRSCSSV open while RIH.", "dTimEnd": "2008-04-10T08:00:00+02:00", "dTimStart": "2008-04-10T06:00:00+02:00", "md": "2164", "phase": "fixed", "proprietaryCode": "completion -- test scsssv", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 7\" 29# S13%Cr tubing with CL and clamps from 2164 m to 2645 m MD. \n\nUp weight 172 MT / down weight 141 MT. Distance between up and down weight was 0.3 m.", "dTimEnd": "2008-04-10T16:30:00+02:00", "dTimStart": "2008-04-10T08:00:00+02:00", "md": "2645", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk before entering 7\" liner.", "dTimEnd": "2008-04-10T17:00:00+02:00", "dTimStart": "2008-04-10T16:30:00+02:00", "md": "2645", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up to pump down kill line and to be able to observe overflow from top of tubing. Verified line up with 15 bar.", "dTimEnd": "2008-04-10T17:45:00+02:00", "dTimStart": "2008-04-10T17:00:00+02:00", "md": "2645", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 7\" 29# S13%Cr tubing with CL and clamps from 2645 m to 2649 m MD. \n\nClosed annular BOP at 280 psi. Attempted to reverse circulate, neg. Leaked through annular. Closed annular BOP at 580 psi. Reverse circulated using clean brine at 50 lpm / 3 bar and 100 lpm / 3.5 bar to get a reference. Observed returns. Stopped circulating and opened annular BOP.", "dTimEnd": "2008-04-10T18:30:00+02:00", "dTimStart": "2008-04-10T17:45:00+02:00", "md": "2649", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 7\" 29# S13%Cr tubing with CL and clamps from 2649 m to 2659.8 m MD. \n\nPerformed reverse circulation exercise 50-100 lpm / 3.5 bar. Moved string down in 30 cm increments from 2659.8 m to 2662.2 m and repeated reverse circulation exercise with same pressure response (50-100 lpm / 3.5 bar).", "dTimEnd": "2008-04-10T21:00:00+02:00", "dTimStart": "2008-04-10T18:30:00+02:00", "md": "2662.2", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with 7\" 29# S13%Cr tubing with CL and clamps from 2662.2 m to 2644 m MD. PU 2.89 m pup joint to space out to be able to close annular without a coupling or a clamp in the interval. RIH with 7\" 29# S13%Cr tubing from 2644 m to 2662.2 m MD.", "dTimEnd": "2008-04-10T23:15:00+02:00", "dTimStart": "2008-04-10T21:00:00+02:00", "md": "2662.2", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed reverse circulation exercise 50-100 lpm / 3.5 bar. Moved string down in 20 cm increments from 2662.2 m to 2662.8 m.", "dTimEnd": "2008-04-11T00:00:00+02:00", "dTimStart": "2008-04-10T23:15:00+02:00", "md": "2662.8", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_12
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-11T00:00:00+02:00
2008-04-12T00:00:00+02:00
normal
2018-05-03T13:52:55+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "21", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-12T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-11T03:30:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "ND BOP and surface riser. Install spacer spool. Skid rig to lift XMT into XMT deck. Lift XMT in place and install dart in BPV. Install XMT assy and flowline and test same.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "96", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Performed high pressure test of control line through TH. MU communication collar and tubing hanger RT. RIH and landed tubing hanger in surface wellhead. Performed low pressure tubing leak test and function test of TRSCSSV. Sat packer and leak tested tubing to 345 bar. Inflow tested TRSCSSV and tested A-annulus to 380 bar. Ran BPV and installed in tubing hanger. ND and pulled diverter.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-11T15:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-12T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Performed reverse circulation exercise 50-100 lpm / 3.5 bar. Moved string down in 20 cm increments from 2662.8 m to 2664.3 m. Had 1 bar increase in pressure from 2663.4 m. Had overflow response on tubing while RIH at 2664.3 m before flow was cut off - indicating that the lower most seal had entered 7\" liner PBR. Confirmed the situation by reverse circulating 50 lpm up to 8.6 bar with no returns. Stopped circulating. Measured 7.24 m stick-up. TOL found at 2662.85 m.", "dTimEnd": "2008-04-11T01:00:00+02:00", "dTimStart": "2008-04-11T00:00:00+02:00", "md": "2664.3", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with 7\" 29# S13%Cr tubing with CL and clamps from 2664.3 m to 2631 m MD. Calculated and performed space-out with pup A,D,E, and F, leaving lower most seal on seal stem stung in by 75 cm (2.2 m from end of string).", "dTimEnd": "2008-04-11T03:30:00+02:00", "dTimStart": "2008-04-11T01:00:00+02:00", "md": "2664.3", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to PU tubing hanger. PU and MU tubing hanger with handling tool to space-out pup joints sitting in the slips. Secured control line with clamp on pup joint coupling. RD control line cable sheave and terminated cable to TH. Wrapped control line 5 times and fed control line thru TH using swagelok fittings above and below hanger. Plugged off penetration holes in TH with 3/8\" NPT blind plugs. Leak tested TH fittings through 1/8\" test port to 35 bar/5 min.", "dTimEnd": "2008-04-11T06:00:00+02:00", "dTimStart": "2008-04-11T03:30:00+02:00", "md": "2643", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Leak tested TH fittings through 1/8\" test port to 380 bar/10 min using BOT pump.", "dTimEnd": "2008-04-11T07:00:00+02:00", "dTimStart": "2008-04-11T06:00:00+02:00", "md": "2643", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk. Lifted TH hanger above slips. Removed PS30 slips and installed master bushings. Installed C-plate and landed TH in C-plate. BO handling tool and LO same.", "dTimEnd": "2008-04-11T08:15:00+02:00", "dTimStart": "2008-04-11T07:00:00+02:00", "md": "2643", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed communication collar onto hanger and made 5 right hand turns until it shouldered out on TH. Wrapped CL 3 times around hanger neck. Connected TRSCSSV CL to 1/4\" communication port at btm of communication collar. \n\nPU tubing hanger RT with 7\" #29 pup joint. Backed out THRT piston retaining screws and MU THRT to communication collar with 8 turns left hand rotation. Connected TRSCSSV CL to 1/4\" communication ports on top of THRT.", "dTimEnd": "2008-04-11T09:15:00+02:00", "dTimStart": "2008-04-11T08:15:00+02:00", "md": "2647", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Leak tested TRSCSSV control line to 570 bar/10 min using BOT test pump. Kept 520 bar pressure on line while RIH. Screwed in THRT piston retaining screws. Control-measured RT and pup-joint lengths.", "dTimEnd": "2008-04-11T10:00:00+02:00", "dTimStart": "2008-04-11T09:15:00+02:00", "md": "2647", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Stopped trip tank and drained production riser.", "dTimEnd": "2008-04-11T10:30:00+02:00", "dTimStart": "2008-04-11T10:00:00+02:00", "md": "2647", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed C-plate. Ran in with THRT below rotary. Installed bowls. PU and MU joints for landing string. Up weight 173 MT / down weight 144 MT. RIH with 7\" 29# S13%Cr tubing, TH and THRT on landing string from 2647 m to 2665,2 m MD. Got indications when ratcheting muleshoe and seals entered 7\" liner PBR. Landed TH on no-go shoulder in surface tubing head. SO weight.\n\nLeak tested TH in port 1 and 2 on surface well head to 70 bar/5 min to verify that TH had landed correctly. Engaged TH lock down ring by applying 207 bar. Performed pull test with 15 MT overpull to verify TH lock down. SO weight.", "dTimEnd": "2008-04-11T13:00:00+02:00", "dTimStart": "2008-04-11T10:30:00+02:00", "md": "2665", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressure tested TH seal through test port 1 and 2 on surface WH to 35/380 bar for 5/10 min using Vetco pump.", "dTimEnd": "2008-04-11T13:30:00+02:00", "dTimStart": "2008-04-11T13:00:00+02:00", "md": "2665", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk. Installed 7\" #29 Vam Top P x 5 1/2\" FH B swedge and 2\" Wetco pump in sub with lo-torque valve. RU cmt hose/cmt unit to lo-torque valve and flushed CMT line to rig floor. Performed line test to 345 bar / 10 min using packer fluid. Observed 1.6 bar drop (0.46%). Performed line test without cmt hose and observed 0.3 bar drop.", "dTimEnd": "2008-04-11T16:00:00+02:00", "dTimStart": "2008-04-11T13:30:00+02:00", "md": "2665", "phase": "fixed", "proprietaryCode": "completion -- test scsssv", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressured up tubing against NPR plug at 2648 m MDRT to 30 bar / 10 min to check tubing integrity before initiating packer setting. 70 ltrs pumped. Kept 570 bar on TRSCSSV CL. Observed 0.3 bar drop. \n\nClosed TRSCSSV. Bled down to 5 bar above TRSCSSV and function tested TRSCSSV for 10 min. Bled back 36 ltrs. Observed 0.2 bar drop. Equalized and opened TRSCSSV.", "dTimEnd": "2008-04-11T17:00:00+02:00", "dTimStart": "2008-04-11T16:00:00+02:00", "md": "2665", "phase": "fixed", "proprietaryCode": "completion -- test scsssv", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to pressure up tubing to 345 bar. Held pressure for 15 min to set SB-3 packer and test tubing. 1050 ltrs pumped. Observed 1.5 bar drop (0.43%).", "dTimEnd": "2008-04-11T17:30:00+02:00", "dTimStart": "2008-04-11T17:00:00+02:00", "md": "2665", "phase": "fixed", "proprietaryCode": "completion -- test scsssv", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Bled down pressure to 320 bar. 60 ltrs bled back. Closed TRSCSSV and bled off pressure above to 250 bar. Bled back 35 ltrs. Inflow tested TRSCSSV with 70 bar diff / 30 min. Inflow test OK.\n \nBled off pressure above TRSCSSV to 10 bar. Bled back 120 ltrs. Inflow tested TRSCSSV with 310 bar diff / 30 min. Inflow test OK. Equalized and opened TRSCSSV using 157 ltrs. Bled off pressure in tubing to zero. Bled back 800 ltrs.", "dTimEnd": "2008-04-11T19:00:00+02:00", "dTimStart": "2008-04-11T17:30:00+02:00", "md": "2665", "phase": "fixed", "proprietaryCode": "completion -- test scsssv", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RU cmt hose/cmt unit to A-annulus to leak test packer from above and TH from below. Opened B-annulus to vent. Performed line test to 35/380 bar for 5/10 min pumping brine at 70 lpm. Observed 1.8 bar drop (0.47%) on high pressure test.", "dTimEnd": "2008-04-11T20:00:00+02:00", "dTimStart": "2008-04-11T19:00:00+02:00", "md": "2665", "phase": "fixed", "proprietaryCode": "completion -- test scsssv", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressured up A-annulus to leak test packer from below and TH from below to 35/380 bar for 5/10 min pumping brine at 70 lpm. Kept tubing open on drill floor and 570 bar on TRSCSSV CL. Pumped 125 ltrs and observed 0.2 bar drop on low pressure test. Pumped 1130 ltrs (total) and observed 2.1 bar (0.5%) drop on high pressure test. Had flow on both tubing and B-annulus while pressuring up A-annulus due to ballooning effect. No flow observed when pumps was shut in. Bled pressure down to zero and had 1100 ltrs in return. Closed TRSCSSV.", "dTimEnd": "2008-04-11T21:00:00+02:00", "dTimStart": "2008-04-11T20:00:00+02:00", "md": "2665", "phase": "fixed", "proprietaryCode": "completion -- test scsssv", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box meeting. Released landing string by 9 right hand turns. POOH and LD landing string. Changed to 5 1/2\" handling equipment.", "dTimEnd": "2008-04-11T23:00:00+02:00", "dTimStart": "2008-04-11T21:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box meeting. PU and MU XO 5 1/2\" FH box x 3 1/2\" IF box to centralizer / BPV running adaptor / BPV. RIH and landed BPV on 5 1/2\" DP in TH at 20.3 m. Sat down string weight to extend locking keys and energize seals. Rotated string 8 1/2\" turns clockwise to lock mandrel and free running adaptor in J-slot. POOH with running string and LD RT.", "dTimEnd": "2008-04-12T00:00:00+02:00", "dTimStart": "2008-04-11T23:00:00+02:00", "md": "20.3", "phase": "fixed", "proprietaryCode": "completion -- test scsssv", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_13
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-12T00:00:00+02:00
2008-04-13T00:00:00+02:00
normal
2018-05-03T13:52:55+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "21.5", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-13T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-12T20:30:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Install XMT assy and flowline and test same. Pull dart and BPV.\n", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "97", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "ND BOP and surface riser. Installed spacer spool on WH and dart in BPV. Skidded rig to lift XMT into wellhead module. Lifted XMT on to F-4 spacer spool. ", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-12T15:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-13T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "POOH with running string and LD RT.", "dTimEnd": "2008-04-12T00:30:00+02:00", "dTimStart": "2008-04-12T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- test scsssv", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RD completion handling equipment.", "dTimEnd": "2008-04-12T02:45:00+02:00", "dTimStart": "2008-04-12T00:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "PU 2 joints of 5 1/2\" HWDP and RIH and drained riser.", "dTimEnd": "2008-04-12T03:45:00+02:00", "dTimStart": "2008-04-12T02:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "ND and pulled diverter.", "dTimEnd": "2008-04-12T06:00:00+02:00", "dTimStart": "2008-04-12T03:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- completion string", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued ND diverter. Went trough SJA and procedure with day crew. Attached slings to slick joint. Prepared barriers, handrails and slings. Lifted out diverter. Installed outer ring and master bushings. Loosened nuts on slick joint.", "dTimEnd": "2008-04-12T10:15:00+02:00", "dTimStart": "2008-04-12T06:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk and reviewed SJA and procedures. Disconnected tension cylinders in WH module.", "dTimEnd": "2008-04-12T12:00:00+02:00", "dTimStart": "2008-04-12T10:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "ND NT2 connection on BOP. Informed production department to shut in well at 12.30.", "dTimEnd": "2008-04-12T13:15:00+02:00", "dTimStart": "2008-04-12T12:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited on production to shut in well. Meanwhile removed 2 HP hoses connected to WH.", "dTimEnd": "2008-04-12T14:00:00+02:00", "dTimStart": "2008-04-12T13:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "ND slick joint and BOP.", "dTimEnd": "2008-04-12T14:45:00+02:00", "dTimStart": "2008-04-12T14:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Dismantled scaffolding on NT2 connection in moonpool and installed slings on riser. RU for disconnecting riser NT2 connection and disconnected same.", "dTimEnd": "2008-04-12T16:15:00+02:00", "dTimStart": "2008-04-12T14:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Dismantled scaffolding in moonpool. PU riser and terminated control lines on well head. Installed carrier on HTS. Installed hatch on weather deck and master bushings on rig floor. Hoisted riser to rig floor and retracted same.", "dTimEnd": "2008-04-12T17:30:00+02:00", "dTimStart": "2008-04-12T16:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Disconnected control lines from communication collar and hoisted same to rig floor. Installed hatch in moonpool. Installed outer ring and master bushings on rig floor. Installed anti vibration ring on TH. Removed one control line exit block on multi bowl. Unwrapped required length of CL around TH neck and fed control line through dedicated port on multi bowl. Fed high pressure packings and fittings onto CL and MU fittings to threads in multi bowl. Installed dart in BPV in TH by hand. Installed 137 VG seal ring on top of multi bowl and VG 63 seal ring on top of TH.\n", "dTimEnd": "2008-04-12T19:15:00+02:00", "dTimStart": "2008-04-12T17:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- test scsssv", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed hatch to F-4. Lowered spacer spool down from rig floor with TDS until NT2 box connector landed out on top of WH. MU locking dogs until connection leveled out. MU actuation screws with 800 ft-lbs. Disconnected slings and removed same. \n\nPressure tested and energized BT seals through ports 7/8. Tested VG 63 connection trough test port 9/10 to 35 bar/5 min.\n\nTested TH void, grafoil seals and BT seals 35/380 bar for 5/10 min via test port 5/6.\n\nMU ferrule swagelock fittings for CL. Installed seal rings and CL exit block. Installed seal ring on top of spacer spool.", "dTimEnd": "2008-04-12T20:30:00+02:00", "dTimStart": "2008-04-12T19:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- test scsssv", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Skidded cantiliver 1.5 m starboard and as far aft as possible to be able to possition crane for lifting XMT.", "dTimEnd": "2008-04-13T00:00:00+02:00", "dTimStart": "2008-04-12T20:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_14
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-13T00:00:00+02:00
2008-04-14T00:00:00+02:00
normal
2018-05-03T13:52:55+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "21.9", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-14T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-12T20:30:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Pressure test and commision XMT.\n", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "98", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Lifted XMT on to F-4 spacer spool. Installed XMT assy and flowline. Waited on production department to start production from F-12. Pressure tested line up from cmt unit to 20 bar for 5 min against XMT KWV.\n", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-13T11:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-14T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Held tool box meeting. Connected crane hook to one of the two chackles in the end of the chain hoist and wire sling. Disconnected transport plate. Lifted XMT to wireline deck and landed it on wooden beams, where it hung suspended in crane hook and resting on wooden beams with 1 MT.", "dTimEnd": "2008-04-13T02:00:00+02:00", "dTimStart": "2008-04-13T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Skidded rig to sea fastening position to gain access for lifting XMT with the port aft deck crane.", "dTimEnd": "2008-04-13T05:15:00+02:00", "dTimStart": "2008-04-13T02:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box meeting. Attempted to lift XMT from wireline deck to F-4 wellhead. Could not reach F-4. Decided to skid further to starboard.", "dTimEnd": "2008-04-13T06:00:00+02:00", "dTimStart": "2008-04-13T05:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Skidded 0.6 m further starboard and reached max skidded position starboard and fwd (sea fastning position).", "dTimEnd": "2008-04-13T07:00:00+02:00", "dTimStart": "2008-04-13T06:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Unable to reach F-4 and F-5 with port aft deck crane. Evalutated alternative methode for landing of XMT. \n\nMeanwhile held toolbox meeting and went through procedures and SJA with day crew.", "dTimEnd": "2008-04-13T09:00:00+02:00", "dTimStart": "2008-04-13T07:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Skidded port and aft out to F-4.\n\nMeanwhile lined up from CMT onto F-12 kill valve. Lined up over choke manifold to equalize above TRSCSSV. Tested lines. Equalized TRSCSSV with 84 bar and opened same. Started production from F-12.", "dTimEnd": "2008-04-13T10:30:00+02:00", "dTimStart": "2008-04-13T09:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held time-out for safety. Talked about everyones right to stop the operation if anything is unclear or confusing. Went through operational plan and safety aspects involved.", "dTimEnd": "2008-04-13T11:00:00+02:00", "dTimStart": "2008-04-13T10:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed staircase to cantiliver.", "dTimEnd": "2008-04-13T12:00:00+02:00", "dTimStart": "2008-04-13T11:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed big moonpool hatch and lowered XMT to moonpool. Re-installed hatch.", "dTimEnd": "2008-04-13T13:30:00+02:00", "dTimStart": "2008-04-13T12:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Transfered XMT from turtle to weather deck and skidded cantiliver to port and fwd to position XMT in center.", "dTimEnd": "2008-04-13T15:30:00+02:00", "dTimStart": "2008-04-13T13:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited on production to shut in well.", "dTimEnd": "2008-04-13T16:15:00+02:00", "dTimStart": "2008-04-13T15:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Attached TDS to XMT. Positioned and disconnected base plate.", "dTimEnd": "2008-04-13T16:45:00+02:00", "dTimStart": "2008-04-13T16:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Skidded rig fwd and port to position XMT over F-4 for final installation.\n\nMeanwhile bled down all pressures on F-12 to zero bar.", "dTimEnd": "2008-04-13T17:30:00+02:00", "dTimStart": "2008-04-13T16:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Moved hatch on weather deck to allow XMT to pass through. Lowered XMT until 1 m above F-4 spacer spool.", "dTimEnd": "2008-04-13T18:45:00+02:00", "dTimStart": "2008-04-13T17:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box meeting. Lowered XMT on to spacer spool with TDS and verified correct orientation.\n\nMU graylock connection. Re-built scaffolding around XMT for proper working environment. Checked alignment of flanges between flow hose and XMT. Pressure tested seal ring 35 bar/10 min through test port 3/4 on spacer spool to confirm proper seal. \n", "dTimEnd": "2008-04-13T20:15:00+02:00", "dTimStart": "2008-04-13T18:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed flow line spool. Disconnected lifting wire from TDS. Connected flexible flow line to flow line spool. Re-installed hatch.", "dTimEnd": "2008-04-14T00:00:00+02:00", "dTimStart": "2008-04-13T20:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_15
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-14T00:00:00+02:00
2008-04-15T00:00:00+02:00
normal
2018-05-03T13:52:55+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "22.3", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-15T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-12T20:30:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Commision XMT.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "99", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Pressure tested XMT. Pulled dart and BPV in TH. Pressure tested flowline. Started commisioning XMT.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[ { "dTim": "2008-04-15T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Postphoned XMT tests to assist production to start up F-12. Lined up from CMT onto F-12 kill valve. Lined up over choke manifold to equalize above TRSCSSV. Tested lines. Equalized TRSCSSV and opened same. Started production from F-12.", "dTimEnd": "2008-04-14T02:45:00+02:00", "dTimStart": "2008-04-14T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box meeting. Opened HMV with Seawell test pump. Lined up from cmt unit and connected hose on KWV. Performed line test to 20 bar for 5 min.", "dTimEnd": "2008-04-14T06:00:00+02:00", "dTimStart": "2008-04-14T02:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Trouble shoot line up from cmt unit through valves and hose from moonpool to KWV due to failing line test. Detected exhaust fumes in WH area.", "dTimEnd": "2008-04-14T07:30:00+02:00", "dTimStart": "2008-04-14T06:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Exhaust fumes in well head area. Abandoned WH. Shud down on of the gas turbines to reduce exhaust fumes.\n", "dTimEnd": "2008-04-14T08:15:00+02:00", "dTimStart": "2008-04-14T07:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed line test to 30/380 bar for 5/10 min against KWV. 2.2 bar drop on high pressure test.\n", "dTimEnd": "2008-04-14T08:30:00+02:00", "dTimStart": "2008-04-14T08:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Attempted to pressure test XMT body and VG 63 ring to 30/380 bar for 5/10 min against dart in BPV. Failed due to leaking dart/BPV.", "dTimEnd": "2008-04-14T10:15:00+02:00", "dTimStart": "2008-04-14T08:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk. Removed XMT tree cap. Opened HMV. RIH with retrieving tool for dart on stinger and retrieved dart. POOH with dart. RIH and installed new dart. Flushed XMT. Closed HMV.", "dTimEnd": "2008-04-14T12:30:00+02:00", "dTimStart": "2008-04-14T10:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Attempted to pressure test XMT body and VG 63 ring to 30/380 bar for 5/10 min against dart in BPV. Failed due to leaking dart/BPV.", "dTimEnd": "2008-04-14T13:00:00+02:00", "dTimStart": "2008-04-14T12:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled dart and BPV. Installed a new BPV and dart. Flushed XMT.", "dTimEnd": "2008-04-14T14:00:00+02:00", "dTimStart": "2008-04-14T13:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressure tested XMT body and VG 63 ring to 30/380 bar for 5/10 min against dart in BPV. 2.5 bar drop on high pressure test.", "dTimEnd": "2008-04-14T14:30:00+02:00", "dTimStart": "2008-04-14T14:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressured up to 130 bar against BPV & dart. Close MMV and bled off pressure above MMV to 10 bar. Inflow tested MMV to 120 bar differential pressure for 15 min. 1.9 bar drop.\n\nEqualized pressure above MMV. Opened MMV and closed HMV. Bled of any pressure above HMV to 10 bar. Inflow test HMV to 120 bar differential pressure for 15 min. 2.4 bar drop.\n\nEqualized pressure across HMV. Opened HMV. Bled off pressure. Closed valves.", "dTimEnd": "2008-04-14T16:00:00+02:00", "dTimStart": "2008-04-14T14:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed XMT tree cap. Opened HMV. RIH with retrieving tool for dart on stinger and retrieved dart. POOH with dart. Pulled BPV from TH.", "dTimEnd": "2008-04-14T17:00:00+02:00", "dTimStart": "2008-04-14T16:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Re-installed XMT tree cap. Close HMV. Test three cap 380 bar/10 min against SV. Bled off pressure. \n", "dTimEnd": "2008-04-14T17:30:00+02:00", "dTimStart": "2008-04-14T17:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressure test TRSCSSV CL exit block to 570 bar/15 min, using BOT pump. Test ok. No indication that TRSCSSV opened. Bled off 155 ml on line.", "dTimEnd": "2008-04-14T18:00:00+02:00", "dTimStart": "2008-04-14T17:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Evalutated options for flushing flowline and made plan for flowline test. Handover with new crew.", "dTimEnd": "2008-04-14T19:00:00+02:00", "dTimStart": "2008-04-14T18:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box meeting. Hooked up flexible hose and lined up for pressure testing flowline. Flushed through XMT PWV, KWV and lo-torque to cement unit with pot-water.", "dTimEnd": "2008-04-14T20:45:00+02:00", "dTimStart": "2008-04-14T19:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Attempted to pressure test flow line and XMT to 30/345 bar for 5/10 min. Observed leak at flange on flexible hose.", "dTimEnd": "2008-04-14T21:30:00+02:00", "dTimStart": "2008-04-14T20:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Inspected, greased and torqued up flange on flow line flexible hose.\n\nMeanwhile worked on varco bolts on AFT PRS and installed tension cylinders on F-14.\n", "dTimEnd": "2008-04-15T00:00:00+02:00", "dTimStart": "2008-04-14T21:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_16
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-15T00:00:00+02:00
2008-04-16T00:00:00+02:00
normal
2018-05-03T13:52:55+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "22.4", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-16T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-12T20:30:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Commision XMT.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "100", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Completed instumentation on XMT. Commenced commisioning.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-15T11:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" }, { "dTim": "2008-04-15T00:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[]
[]
[ { "comments": "Inspected, greased and torqued up flange on flow line flexible hose.\n\nMeanwhile worked varco bolt on AFT PRS and installed tension cylinders on F-14.", "dTimEnd": "2008-04-15T02:15:00+02:00", "dTimStart": "2008-04-15T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Flushed through XMT to cmt unit prior to testing flowline. Pressure tested flow line and XMT to 30/345 bar for 5/10 min. 1.1 bar drop on low pressure test and 1.7 bar drop on high pressure test.", "dTimEnd": "2008-04-15T04:00:00+02:00", "dTimStart": "2008-04-15T02:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Commisioned XMT.\n\nMeanwhile worked on varco bolts on AFT PRS and installed tension cylinders on F-14.\n", "dTimEnd": "2008-04-15T06:00:00+02:00", "dTimStart": "2008-04-15T04:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed instrumentation on F-4 XMT. Connected umbilical to bulk head plate.\n\nMeanwhile changed out chain on HTS, emptied trip tank and repaired sensor on gate valve shakers. Started to change out one tension cylinder on F-14. Carried out work scope with climbers in derrick.", "dTimEnd": "2008-04-15T12:00:00+02:00", "dTimStart": "2008-04-15T06:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited on production to restart after production shut-down.", "dTimEnd": "2008-04-15T12:45:00+02:00", "dTimStart": "2008-04-15T12:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Energized instrumentation on XMT.\n\nMeanwhile changed out one tension cylinder on F-14 and cleaned area. lined up from cement unit onto F-12 kill valve. Lined up over choke manifold. Equalized TRSCSSV with 94 bar and opened same. Started production from F-12. Carried out work scope with climbers in derrick.", "dTimEnd": "2008-04-15T16:30:00+02:00", "dTimStart": "2008-04-15T12:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Function tested XMT pressure transmitters.\n\nMeanwhile retrieved base plate from weather deck to moonpool. Carried out work scope with climbers in derrick.", "dTimEnd": "2008-04-15T17:00:00+02:00", "dTimStart": "2008-04-15T16:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Mounted umbilical termination plate on XMT.\n\nMeanwhile performed housekeeping on cantilever. Carried out work scope with climbers in derrick.", "dTimEnd": "2008-04-15T19:30:00+02:00", "dTimStart": "2008-04-15T17:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Tested annulus pressure transmitters on XMT.\n\nMeanwhile worked on Varco bolts on aft PRS. Built suspended scaffolding for repair on fwd PRS. parked and landed BOP on test stump.", "dTimEnd": "2008-04-15T21:30:00+02:00", "dTimStart": "2008-04-15T19:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Function tested PWV and HMV on XMT with process operator present. Feed back on valve position to process control room read OK.\n\nMeanwhile continued building suspended scaffolding for fwd PRS in paralell with securing bolts on aft PRS.", "dTimEnd": "2008-04-15T22:45:00+02:00", "dTimStart": "2008-04-15T21:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Commenced commisioning of XMT. Verified documentation from Vetco Gray and Aibel. Performed pre-commisioning checks.\n\nMeanwhile continued building suspended scaffolding for fwd PRS in paralell with securing bolts on aft PRS. Started to lift parts for fwd PRS onto scaffolding.", "dTimEnd": "2008-04-16T00:00:00+02:00", "dTimStart": "2008-04-15T22:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_17
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-16T00:00:00+02:00
2008-04-17T00:00:00+02:00
normal
2018-05-03T13:52:55+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "22.6", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-17T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-16T17:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Wait on WL equipment and personnel to arrive on rig. RU WL equipment. Pull NPR plug.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "101", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Commisioned XMT. Waited on WL equipment and personnel to arrive on rig. ", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-16T10:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-17T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Performed pre-commisioning checks of valves on XMT. Function tested MMV and SV and XMT with process operator present. Feed back on valve position to control room read OK.\n\nMeanwhile continued building suspended scaffolding for fwd PRS in paralell with securing bolts on aft PRS.", "dTimEnd": "2008-04-16T06:00:00+02:00", "dTimStart": "2008-04-16T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed pre-commisioning checks of valves on XMT. Function tested MMV and SV and XMT with process operator present. Feed back on valve position to control room read OK.\n\nMeanwhile continued building suspended scaffolding for fwd PRS in parallell with securing bolts on aft PRS.", "dTimEnd": "2008-04-16T07:00:00+02:00", "dTimStart": "2008-04-16T06:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Commisioned XMT.\n\nMeanwhile performed derrick inspection with climbers and worked on BOP.", "dTimEnd": "2008-04-16T17:00:00+02:00", "dTimStart": "2008-04-16T07:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waiting on WL equipment and personnel to arrive on rig. Completed commisioning of XMT 38 hrs ahead of plan.\n\nMeanwhile erected scaffolding platform for fwd PRS and performed 3-montly maintenance on BOP.\n", "dTimEnd": "2008-04-17T00:00:00+02:00", "dTimStart": "2008-04-16T17:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wait", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_18
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-17T00:00:00+02:00
2008-04-18T00:00:00+02:00
normal
2018-05-03T13:52:56+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "23.1", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-18T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-16T17:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Continue RU WL equipment. Pull NPR plug.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "102", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Waited on WL equipment and personnel to arrive on rig. Spotted WL equipment on rig floor. Started RU WL equipment. ", "tightWell": "0", "tvd": "3138.5", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-17T11:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-18T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Waiting on WL equipment and personnel to arrive on rig. \n\nMeanwhile erected scaffolding platform for fwd PRS and performed 3-montly maintenance on BOP.\n", "dTimEnd": "2008-04-17T06:00:00+02:00", "dTimStart": "2008-04-17T00:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waiting on WL equipment and personnel to arrive on rig. \n\nMeanwhile performed derrick inspection with climbers and performed 3-montly maintenace on BOP.\n", "dTimEnd": "2008-04-17T11:00:00+02:00", "dTimStart": "2008-04-17T06:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Prepared for RU wireline equipment and tested dual and trippel BOP's.\n\nMeanwhile equalized above DHSV on F-12 with cmt unit to re-start production. Observed leak in F-12 XMT.\nMeanwhile performed derrick inspection with climbers and performed 3-montly maintenace on BOP.", "dTimEnd": "2008-04-17T12:30:00+02:00", "dTimStart": "2008-04-17T11:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Prepared for RU wireline equipment and tested dual and trippel BOP's.\n\nMeanwhile identified leak on F-12 XMT to be in MEG injection valve. \nMeanwhile performed derrick inspection with climbers and performed 3-montly maintenace on BOP.", "dTimEnd": "2008-04-17T19:00:00+02:00", "dTimStart": "2008-04-17T12:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Prepared for RU wireline equipment and tested dual and trippel BOP's.\n\nMeanwhile continued to work on scaffolding platform for fwd PRS.", "dTimEnd": "2008-04-17T20:45:00+02:00", "dTimStart": "2008-04-17T19:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box meeting. Spotted WL equipment on rig floor and hooked up BCU and pump skids. Prepared riser and BOP for lifting down to moonpool area.\n\nMeanwhile changed MEG injection valve on F-12 and re-tested valve to 325 bar/30 min.", "dTimEnd": "2008-04-18T00:00:00+02:00", "dTimStart": "2008-04-17T20:45:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_19
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-18T00:00:00+02:00
2008-04-19T00:00:00+02:00
normal
2018-05-03T13:52:56+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "23.7", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-19T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-16T17:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "POOH with NPR plug. RIH and perforate, run #1. POOH. RIH and perforate, run #2. POOH.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "103", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Continued RU WL equipment. RU WL tool string with GS and equalizing prong for pulling NPR plug. Released and retracted slips in pre-installed NPR plug at 2649.7 m MD.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-18T14:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-19T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Spotted WL equipment on rig floor and hooked up BCU and pump skids. Prepared riser and BOP for lifting down to moonpool area.\n\nMeanwhile equalized above DHSV on F-12 with cmt unit to re-start production. Production on F-12 started 02:00.\nMeanwhile built scaffolding bridge from cantiliver to Schlumberger WL deck (port aft leg).", "dTimEnd": "2008-04-18T02:15:00+02:00", "dTimStart": "2008-04-18T00:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box meeting. Hooked up chicksan line in moonpool from cmt unit to both F-12 and F-4 with seperate high pressure hoses. Lifted off hatch on F-4. Leak tested line from cmt unit to XMT KWV with LTV4 closed 30/380 bar for 5/10 min. Dropped 0.75 bar/10 min. Verified no pressure under XMT cap and removed same.", "dTimEnd": "2008-04-18T06:00:00+02:00", "dTimStart": "2008-04-18T02:15:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lowered the assembled XO, pump-in sub and short riser section through the rotary with tugger from drill floor and connected it to XMT. Installed BOP's with dual placed on top of tripple BOP.", "dTimEnd": "2008-04-18T11:00:00+02:00", "dTimStart": "2008-04-18T06:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Built scaffolding around BOP's to enabling handling of riser above BOP's.", "dTimEnd": "2008-04-18T12:15:00+02:00", "dTimStart": "2008-04-18T11:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed riser sections to rig floor.", "dTimEnd": "2008-04-18T13:30:00+02:00", "dTimStart": "2008-04-18T12:15:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Opened SV. Attempted to pressure test riser sections and BOP's without sucess. Identified leak in FMC drain valve. Bled off pressure. Closed SV. Attempted to rectify the leaking valve without sucess.", "dTimEnd": "2008-04-18T17:00:00+02:00", "dTimStart": "2008-04-18T13:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "interruption -- rig up/down", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Built grease injection head, with cable head already installed and one lubricator section on rig floor. PU grease injection head and one lubricator section using tugger. Connected two more lubricator sections. Installed sheave wheels.\n\nMeanwhile drained riser and installed new FMC drain valve. \n", "dTimEnd": "2008-04-18T21:00:00+02:00", "dTimStart": "2008-04-18T17:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "PU and MU WL toolstring for pulling NPR plug and installed in lubricator. Connected lubricator at in-situ sub. \n\nOpened SV partly and flushed and filled lubricator with packer fluid using cement unit through KWV. Attempted to pressure test wireline rig-up. Observed leak in lubricator XO below tool catcher.\n\nMeanwhile transfered operation of HMV and TRSCSSV to pump skid in moonpool. Production operator was present during the transfer.", "dTimEnd": "2008-04-18T22:15:00+02:00", "dTimStart": "2008-04-18T21:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "BO lubricator and toostring. Changed leaking o-ring in XO. MU toolstring and re-connected lubricator.", "dTimEnd": "2008-04-18T23:00:00+02:00", "dTimStart": "2008-04-18T22:15:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "interruption -- rig up/down", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Opened SV partly and flushed and filled lubricator with packer fluid using cement unit through KWV. Pressure tested wireline rig-up 30/185 bar for 5/10 min against HMV. Dropped 0.75 bar/10 min. Filled lubricator with 700 ltrs. Bled off pressure in lubricator/rig-up to cmt unit. Closed SV.\n\nPressured up and opened HMV and TRSCSSV using WL pump in moonpool. Observed for leak on well head for 10 min. No leak observed. Opened SV.", "dTimEnd": "2008-04-18T23:45:00+02:00", "dTimStart": "2008-04-18T23:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Started RIH WL toolstring for pulling NPR plug. Production shut down at 23:57 and had shut down WL unit. Re-powered up WL unit.", "dTimEnd": "2008-04-19T00:00:00+02:00", "dTimStart": "2008-04-18T23:45:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_20
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-19T00:00:00+02:00
2008-04-20T00:00:00+02:00
normal
2018-05-03T13:52:56+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "24.6", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-20T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-16T17:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Connect firing head to guns. MU lubricator and test against in-situ sub to 185 bar. RIH with perforation run #1, correlate and fire guns. POOH and LD fired guns. PU and MU guns for perforation run #2. RIH with perforation run #2, correlate and fire guns. POOH and LD fired guns.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "104", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "POOH with NPR plug. Pressure tested 7\" tubing/liner to 380 bar. Extended rig up with additional lengths of riser and lubricator. Built scaffolding to be able to install perforation guns in riser. Tested rig-up to 30/185 bar with dummy toolstring. Broke riser at in-situ sub and installed perforation guns.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-19T16:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-20T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "RIH WL toolstring for pulling NPR plug from surface to TRSCSSV at 496 m MDRT. Found that TRSCSSV was closed. Decided not to wait for cmt unit - production needed to equalize and open TRSCSSV on F-12 to re-start production. \n\nHooked up pump on rig floor to needle valve on lubricator to equalize and open TRSCSSV in F-4. Ran through TRSCSSV at 496 m MDRT and verified that it was fully open.", "dTimEnd": "2008-04-19T01:15:00+02:00", "dTimStart": "2008-04-19T00:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued RIH WL toolstring for pulling NPR plug to 2600 m MDRT using running procedures for new cables. Running speed 40 m/min. Did not bleed off pressure while RIH and had 11-12 bar in well at 2600 m. Up weight 710 kg / Hanging weight 530 kg / RIH weight 422 kg.", "dTimEnd": "2008-04-19T03:00:00+02:00", "dTimStart": "2008-04-19T01:15:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH and latched GS pulling tool into NPR plug at 2649.7 m. Jared down to equalize ports in the plug. Waited 15 min for pressure across plug to equalize. Pressure dropped to 10 bar. Bleed off pressure. Released NPR plug by jaring up once. Got 150 kg increase in string weight. Waited 30 min to allow elements to retract.", "dTimEnd": "2008-04-19T04:00:00+02:00", "dTimStart": "2008-04-19T03:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with NPR plug. Observed that weight dropped back to up weight while POOH. RIH and latched GS pulling tool into NPR plug at 2649.7 m. Pressured up well to 10 bar. Jarred down to equalize ports in the plug. Waited 15 min for pressure across plug to equalize. No pressure drop observed. \n\nReleased NPR plug by jaring up 105 hits. Adjusted stress point on cable after 60 hits with jar. Got approx 300 kg increase in string weight. Bleed off pressure. Waited 30 min to allow elements to retract.", "dTimEnd": "2008-04-19T06:00:00+02:00", "dTimStart": "2008-04-19T04:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with NPR plug on 7/32 cable, worked through TRSCSSV at 496 m with 200 kg overpull. Closed SV using 42 turns and closed HMV. Bled off pressure in XMT, riser and lubricator to closed drain.", "dTimEnd": "2008-04-19T09:00:00+02:00", "dTimStart": "2008-04-19T06:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RD lubricator and cut wireline as per Seawell instructions. LD and inspected BHA and NPR plug. Plug had only small rift on rubber element.", "dTimEnd": "2008-04-19T10:30:00+02:00", "dTimStart": "2008-04-19T09:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box meeting. Attempted to increase TRSCSSV CL pressure to 570 bar with Seawell pump without sucess. Max pressure of 540 bar with Seawell pump. RU Vetco pump to pressure up CL to 570 bar.", "dTimEnd": "2008-04-19T11:45:00+02:00", "dTimStart": "2008-04-19T10:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- test scsssv", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up to test 7\" tubing/liner to 380 bar through KWV with cmt pump. Opened LTV1 and LTV2. Pressured up well to test 7\" tubing/liner to 35/380 bar for 5/10 min against EZSV plug at 3448 m MDRT. Pumped 1195 ltrs and bled back 1190 ltrs. Dropped 1.6 bar/10 min. Closed HMV. Adjusted TRSCSSV CL pressure to 520 bar.", "dTimEnd": "2008-04-19T12:45:00+02:00", "dTimStart": "2008-04-19T11:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- test scsssv", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed Check Valve in test line to cmt unit. Performed line test from cmt unit against KWV to 185 bar/10 min. Dropped 0.9 bar/10 min. Bled down to 10 bar on cmt unit to inflow test Check Valve. Bled down pressure between KWV and Check Valve to closed drain.\n\nMeanwhile RU scaffolding and lubricator to grease head.", "dTimEnd": "2008-04-19T15:00:00+02:00", "dTimStart": "2008-04-19T12:45:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RU additional lubricator sections needed for perforation runs. Lifted riser sections to rig floor. Modified scaffolding to a higher level to be able to assemble lubricator. RU to run 7/16\" electric line. Prepared grease injection head. MU cable head with PGGT.", "dTimEnd": "2008-04-19T20:45:00+02:00", "dTimStart": "2008-04-19T15:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed cable head and PGGT with bottom nose in riser. Connected WL riser at in-situ sub. Confirmed correct line up from cmt unit. Opened SV and KWV on XMT. Filled up riser and leak tested WL rigup to 30/185 bar for 5/10 min with cmt pump against HMV. Dropped 0.6 bar/10 min. Bled off pressure to closed drain. Closed SV.", "dTimEnd": "2008-04-19T23:00:00+02:00", "dTimStart": "2008-04-19T20:45:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drained lubricator. Broke riser at in-situ sub and LD toolstring. Cleared drill floor. Installed nitrogen rack and regulator on drill floor.", "dTimEnd": "2008-04-20T00:00:00+02:00", "dTimStart": "2008-04-19T23:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_21
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-20T00:00:00+02:00
2008-04-21T00:00:00+02:00
normal
2018-05-03T13:52:56+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "25", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-21T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-16T17:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Continue POOH with perforation guns. Confirm that guns has fired. Test well and leave MEG above TRSCSSV. LD guns. RD WL equipment.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "105", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Connected firing head to guns. MU lubricator and tested against in-situ sub to 185 bar. RIH with perforation run #1, correlate and fire guns. POOH and LD fired guns. PU and MU guns for perforation run #2. RIH with perforation run #2, correlate and fire guns. POOH from 3390 m to 1800 m MD.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-20T11:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-21T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Discussed method for PU and MU perforation guns due to uncertified lifting cap.", "dTimEnd": "2008-04-20T02:15:00+02:00", "dTimStart": "2008-04-20T00:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "interruption -- rig up/down", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Held tool box meeting prior to PU and MU gun sections.", "dTimEnd": "2008-04-20T02:45:00+02:00", "dTimStart": "2008-04-20T02:15:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Checked GR/CCL on rig floor. Shut down power to Schlumberger unit to follow procedure for MU perforation guns. Closed off rig floor, WH and XMT. Made PA announcement.", "dTimEnd": "2008-04-20T03:15:00+02:00", "dTimStart": "2008-04-20T02:45:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "PU gun sections from cantiliver onto HTS with crane. Connected toolstring and swivel to gun and lifted guns into riser using both tugger and electric line with gooseneck. Connected and hung off all three gun sections in C-plate.", "dTimEnd": "2008-04-20T06:00:00+02:00", "dTimStart": "2008-04-20T03:15:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "MU firing head, PGGT and new swiwel to guns hung off in riser. Connected upper toolstring to guns hanging in riser and armed guns. PU tension on toolstring and took off C-plate.", "dTimEnd": "2008-04-20T08:45:00+02:00", "dTimStart": "2008-04-20T06:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Connected lubricator and tested in-situ sub to 30/185 bar for 5/10 min with Seawell test pump. Ok.", "dTimEnd": "2008-04-20T09:15:00+02:00", "dTimStart": "2008-04-20T08:45:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Opened HMV and observed 2 bar WHP. Verified TRSCSSV was open. Opened SV and RIH with 4.5\" TCP guns on 7/16\" electric line from surface to 3442 m MD. Up weight 2850 kg / Running weight 1500 kg.", "dTimEnd": "2008-04-20T13:00:00+02:00", "dTimStart": "2008-04-20T09:15:00+02:00", "md": "3442", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Bled 50 bar WHP down to zero through closed drain. Correlated guns to shooting depth using GR. Hanging weight 2570 kg. Fired guns and perforated interval #1 from 3408.5 m to 3422.0 m MD. Positiv confirmation that guns had fired, but observed no increase in WHP.", "dTimEnd": "2008-04-20T13:30:00+02:00", "dTimStart": "2008-04-20T13:00:00+02:00", "md": "3426", "phase": "wire line", "proprietaryCode": "workover -- perforate", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH and logged GR/CCL to above production packer. POOH with perforation guns to OOH. Powered down logging unit at 70 m below seabed. Made PA announcement and pulled cable head into tool catcher. Closed SV to verify BHA OOH.", "dTimEnd": "2008-04-20T15:30:00+02:00", "dTimStart": "2008-04-20T13:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Closed HMV. Observed no WHP. Opened bleed to closed drain as a precaution. Opened needle valve and confirmed that lubricator was empty and that the well was on vacuum.\n\nBroke lubricator at in-situ sub. BO and LD guns using sertified lifting sub. Observed that all shots had fired.", "dTimEnd": "2008-04-20T20:30:00+02:00", "dTimStart": "2008-04-20T15:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "PU gun sections from cantiliver onto HTS with crane. MU lifting sub and lifted guns into riser. Connected and hung off all three gun sections in C-plate.", "dTimEnd": "2008-04-20T22:00:00+02:00", "dTimStart": "2008-04-20T20:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Built and tested new cable head. Checked CCL on rig floor. Shut down power to Schlumberger unit according to procedure for MU perforation gun.", "dTimEnd": "2008-04-20T23:30:00+02:00", "dTimStart": "2008-04-20T22:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "MU firing head, CAL-B and new swiwel to guns hung off in riser. Connected upper toolstring to guns hanging in riser and armed guns.", "dTimEnd": "2008-04-21T00:00:00+02:00", "dTimStart": "2008-04-20T23:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_22
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-21T00:00:00+02:00
2008-04-22T00:00:00+02:00
normal
2018-05-03T13:52:56+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "25.6", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-22T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-16T17:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Continue RD WL equipment. Test tree cap. Hand over well to production.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "106", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Continued POOH with perforation guns from 1800 m to OOH. Confirmed that guns had not fired due to leak in logging head. Built new logging head and MU and checked toolstring. RIH with perforation run #3, correlated and fired guns. POOH from 3390 m to OOH. Had zero WHP. Left MEG above TRSCSSV and tested XMT cross. LD guns. RD WL equipment.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-21T15:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-22T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "Continued connecting upper toolstring to guns hanging in riser and armed guns. PU tension on toolstring and took off C-plate.", "dTimEnd": "2008-04-21T00:30:00+02:00", "dTimStart": "2008-04-21T00:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Connected lubricator and tested in-situ sub to 30/185 bar for 5/10 min with Seawell test pump. Ok. Opened HMV and observed 0 WHP. Verified TRSCSSV was open. Opened SV.", "dTimEnd": "2008-04-21T01:00:00+02:00", "dTimStart": "2008-04-21T00:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 4.5\" TCP guns on 7/16\" electric line from surface to 3300 m MD. \n\nMeanwhile worked on synergi report for derrick, performed general maintenace and prepared BOP for pressure test.", "dTimEnd": "2008-04-21T04:00:00+02:00", "dTimStart": "2008-04-21T01:00:00+02:00", "md": "3300", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Correlated depth to 2 m pup-joint in 7\" liner at 3228.38-3230.42 m tally depth / 3229.5 -3231.5 m WL dept correlated with GR on reservoar log using CCL.", "dTimEnd": "2008-04-21T04:30:00+02:00", "dTimStart": "2008-04-21T04:00:00+02:00", "md": "3390.3", "phase": "wire line", "proprietaryCode": "workover -- perforate", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with guns to shooting depth. No WHP. Up weight 2985 kg / Running weight 1540 kg. Hanging weight 2330 kg. Fired guns and perforated interval #2 from 3395.0 m to 3408.5 m MD. \n\nNo obvious indication that guns has fired, but observed short circuit in string and CCL stopped working. Observed no increase in WHP. PU weight increased with 100 kg (3100 kg).", "dTimEnd": "2008-04-21T05:15:00+02:00", "dTimStart": "2008-04-21T04:30:00+02:00", "md": "3390.3", "phase": "wire line", "proprietaryCode": "workover -- perforate", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with perforation guns from 3390 m to 1800 m MD.", "dTimEnd": "2008-04-21T06:00:00+02:00", "dTimStart": "2008-04-21T05:15:00+02:00", "md": "1800", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with perforation guns from 1800 m to OOH. Powered down logging unit at 70 m below seabed. Made PA announcement and pulled cable head into tool catcher. Closed SV to verify BHA OOH. Closed HMV. Observed no WHP. Opened bleed to closed drain as a precaution. Opened needle valve and confirmed that lubricator was empty and that the well was on vacuum. Broke lubricator at in-situ sub. Confirmed that guns had not fired.", "dTimEnd": "2008-04-21T07:45:00+02:00", "dTimStart": "2008-04-21T06:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Disarmed guns and removed firing head. Found leak in rope socket/cable head which caused short circuit in toolstring. Built and tested new cable head. Checked CCL on rig floor. Shut down power to Schlumberger unit according to procedure for MU perforation gun.", "dTimEnd": "2008-04-21T13:00:00+02:00", "dTimStart": "2008-04-21T07:45:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "interruption -- rig up/down", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "MU firing head, CAL-B and new swiwel to guns hung off in riser. Connected upper toolstring to guns hanging in riser and armed guns. PU tension on toolstring and took off C-plate. Connected lubricator and tested in-situ sub to 30/185 bar for 5/10 min with Seawell test pump. Ok. Opened HMV and observed 0 WHP. Verified TRSCSSV was open. Opened SV.", "dTimEnd": "2008-04-21T14:00:00+02:00", "dTimStart": "2008-04-21T13:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "interruption -- rig up/down", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "RIH with 4.5\" TCP guns on 7/16\" electric line from surface to 701 m MD.", "dTimEnd": "2008-04-21T15:00:00+02:00", "dTimStart": "2008-04-21T14:00:00+02:00", "md": "701", "phase": "wire line", "proprietaryCode": "interruption -- rig up/down", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "POOH with perforation guns from 701 m to 360 m MD due to weak CCL signal.", "dTimEnd": "2008-04-21T15:45:00+02:00", "dTimStart": "2008-04-21T15:00:00+02:00", "md": "360", "phase": "wire line", "proprietaryCode": "interruption -- rig up/down", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Schlumberger discussed with town and confirmed that CCL was ok. RIH with 4.5\" TCP guns on 7/16\" electric line from 360 m to 3408 m MD.", "dTimEnd": "2008-04-21T17:30:00+02:00", "dTimStart": "2008-04-21T15:45:00+02:00", "md": "3408", "phase": "wire line", "proprietaryCode": "interruption -- rig up/down", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Correlated depth to 2 m pup-joint in 7\" liner at 3228.38-3230.42 m tally depth / 3229.5 -3231.5 m WL dept correlated with GR on reservoar log using CCL. RIH with guns to shooting depth. No WHP. Fired guns and perforated interval #2 from 3395.0 m to 3408.5 m MD. Positiv indication that guns fired.", "dTimEnd": "2008-04-21T18:15:00+02:00", "dTimStart": "2008-04-21T17:30:00+02:00", "md": "3390.3", "phase": "wire line", "proprietaryCode": "interruption -- rig up/down", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "POOH with perforation guns from 3390 m to OOH. Powered down logging unit at 70 m below seabed. Made PA announcement and pulled cable head into tool catcher. Closed SV to verify BHA OOH. Closed HMV. Observed no WHP. Opened bleed to closed drain as a precaution. Opened needle valve and confirmed that lubricator was empty and that the well was on vacuum. Broke lubricator at in-situ sub. Confirmed that guns had fired.", "dTimEnd": "2008-04-21T20:30:00+02:00", "dTimStart": "2008-04-21T18:15:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "interruption -- rig up/down", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Connected lubricator and tested in-situ sub to 30/185 bar for 5/10 min with Seawell test pump. Ok. Opened HMV and observed 0 WHP. Verified TRSCSSV was open. Opened KWV. Pumped /bullheaded 3 m3 100% MEG at 180 lpm and 8 bar into well with cmt pump to provide cusion above closed TRSCSSV. Displaced MEG to above TRSCSSV by chasing it with 5.5 m3 packer fluid at 180 lpm and 8-20 bar. WHP started to increase after approx. 3 m3 packer fluid pumped.", "dTimEnd": "2008-04-21T21:45:00+02:00", "dTimStart": "2008-04-21T20:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pumped 300 ltrs 100% MEG and displaced line with 500 ltrs packer fluid to fill XMT cross with 100% MEG. Closed TRSCSSV and HMV. Leak tested XMT cross to 123 bar / 10 min against closed HMV. Dropped 1.1 bar / 10 min. Bled off pressure to zero bar. Closed KWV.", "dTimEnd": "2008-04-21T22:15:00+02:00", "dTimStart": "2008-04-21T21:45:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke lubricator at in-situ sub. BO and LD guns using certified lifting sub.", "dTimEnd": "2008-04-22T00:00:00+02:00", "dTimStart": "2008-04-21T22:15:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2008_04_23
NO 15/9-F-4
NO 15/9-F-4
name
2008-04-22T00:00:00+02:00
2008-04-23T00:00:00+02:00
normal
2018-05-03T13:52:56+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": "25.6", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-04-23T00:00:00+02:00", "dTimDiaHoleStart": "2008-04-16T17:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Continue maintenance program on F-99.", "hpht": "0", "md": "3510", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "107", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Continued RD WL equipment. Tested tree cap and KWV cap. Handed over well to production. Removed scaffolding and installed hatch.", "tightWell": "0", "tvd": "3138.8", "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2008-04-22T06:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "other", "presBopRating": "690", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[ { "dTim": "2008-04-23T00:00:00+02:00", "equivalentMudWeight": "1.08", "md": "3510", "readingKind": "measured" } ]
[]
[ { "comments": "BO and LD guns using certified lifting sub. Observed that all shots had fired.", "dTimEnd": "2008-04-22T01:00:00+02:00", "dTimStart": "2008-04-22T00:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RD lubricatoor on rig floor. Disconnected and pulled riser sections above BOP to rig floor.", "dTimEnd": "2008-04-22T03:00:00+02:00", "dTimStart": "2008-04-22T01:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Opened HMV and confirmed 0 WHP below. Closed HMV and opened KWV. Leak tested XMT cross to 123 bar / 10 min against closed HMV. Dropped 0.6 bar / 10 min. Bled off pressure to zero bar. Closed KWV.", "dTimEnd": "2008-04-22T03:45:00+02:00", "dTimStart": "2008-04-22T03:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box meeting. RD hydraulic BOP hoses. Disconnected WL BOP's and transfered to overhead crane in moonpool. Transported BOP's to main deck. Dismantled scaffolding around BOP's.", "dTimEnd": "2008-04-22T06:00:00+02:00", "dTimStart": "2008-04-22T03:45:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed tree cap and tested same 35/380 bar for 5/10 min against closed SV using Seawell test pump and 100% MEG. Bled off pressure.", "dTimEnd": "2008-04-22T07:00:00+02:00", "dTimStart": "2008-04-22T06:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RD HP line from XMT KWV to cmt unit. Installed 1502 weco blind cap outside KWV and opened KWV. Leak tested KWV cap to 35/380 bar for 5/10 min aginst closed SV using Seawell test pump and 100% MEG.", "dTimEnd": "2008-04-22T08:45:00+02:00", "dTimStart": "2008-04-22T07:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Transfered operation of HMV and TRSCSSV to platform system/production. Filled in and signed \"Well handover document\" and handed over well from Volve D&W to Mærsk Production at 09:00. \n\nMeanwhile RD scaffolding on rig floor and cleared rig floor of excess equipment.", "dTimEnd": "2008-04-22T09:30:00+02:00", "dTimStart": "2008-04-22T08:45:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed scaffolding around moonpool hatch and installed hatch. \n ****************END OF OPERATIONS****************", "dTimEnd": "2008-04-22T10:45:00+02:00", "dTimStart": "2008-04-22T09:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2010_09_24
NO 15/9-F-4
NO 15/9-F-4
name
2010-09-23T00:00:00+02:00
2010-09-24T00:00:00+02:00
normal
2018-05-03T13:52:56+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2010-09-24T00:00:00+02:00", "dTimDiaHoleStart": "2010-09-23T16:30:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Leak test RU. Perform RST logging on 5/16\" mono cable.\n\nExpected status 06:00 tomorrow: RD pressure control equipment.", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "1", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Took over well from production department. Skidded rig in position. Installed workover hatch and leak tested XMT cross.", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Well handed over from production department. Skidded rig in position. Changed to workover hatch. Meanwhile held pre job meeting with involved personnel.", "dTimEnd": "2010-09-23T22:30:00+02:00", "dTimStart": "2010-09-23T16:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box meeting on rig floor. Leak tested XMT cross to 20/100 bar for 5/10 min.", "dTimEnd": "2010-09-24T00:00:00+02:00", "dTimStart": "2010-09-23T22:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2010_09_25
NO 15/9-F-4
NO 15/9-F-4
name
2010-09-24T00:00:00+02:00
2010-09-25T00:00:00+02:00
normal
2018-05-03T13:52:56+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2010-09-25T00:00:00+02:00", "dTimDiaHoleStart": "2010-09-23T16:30:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "POOH with BHA #1. RD wireline pressure control equipment and hand over well to Production department. Pack and prepare equipment for backload.", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "2", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "RU wireline pressure control equipment. RIH with BHA #1 to 3400 m. Logged RST in IC mode at 0,5 m/min and in Sigma mode at 4,5 m/min from 3390 to 3230 m. Logged second IC mode pass from 3390 to 3370 m.", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Installed chiksan manifold on TKV and leak tested same to 20/100 bar for 5/10 min.", "dTimEnd": "2010-09-24T01:30:00+02:00", "dTimStart": "2010-09-24T00:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed XMT top cap and installed lower riser and BOP. Leak tested lower riser/BOP connections and function tested BOP. Lowered down upper riser from rig floor and stabbed riser onto BOP.\nMeanwhile checked and tested RST toolstring on surface.\n", "dTimEnd": "2010-09-24T05:00:00+02:00", "dTimStart": "2010-09-24T01:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk and lifted up lubricator and GIH in elevator. Started to install toolstring into lubricator.", "dTimEnd": "2010-09-24T06:00:00+02:00", "dTimStart": "2010-09-24T05:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued installing toolstring into lubricator.", "dTimEnd": "2010-09-24T07:45:00+02:00", "dTimStart": "2010-09-24T06:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited due to broken bolt in the wheel for KWV. Mechanic attempted to chang bolt without success and found a temporary solution.", "dTimEnd": "2010-09-24T09:15:00+02:00", "dTimStart": "2010-09-24T07:45:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Leak tested rig up. 20/100 bar for 5/10 min. Opened well. WHP = 7 bar.", "dTimEnd": "2010-09-24T10:00:00+02:00", "dTimStart": "2010-09-24T09:15:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with BHA#1, RST. Stopped in DHSV at 498 m.", "dTimEnd": "2010-09-24T10:45:00+02:00", "dTimStart": "2010-09-24T10:00:00+02:00", "md": "498", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up AWS pump, pumped MEG into well and equalized DHSV at 39 bar.", "dTimEnd": "2010-09-24T11:15:00+02:00", "dTimStart": "2010-09-24T10:45:00+02:00", "md": "498", "phase": "wire line", "proprietaryCode": "workover -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued RIH with BHA#2, RST to 3420 m.", "dTimEnd": "2010-09-24T13:30:00+02:00", "dTimStart": "2010-09-24T11:15:00+02:00", "md": "3420", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Ran correlation passes. Adjusted the depth according to reference log.", "dTimEnd": "2010-09-24T14:00:00+02:00", "dTimStart": "2010-09-24T13:30:00+02:00", "md": "3420", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Logged RST-D in IC mode from 3390 to 3230 m at 0.5 m/min.", "dTimEnd": "2010-09-24T21:15:00+02:00", "dTimStart": "2010-09-24T14:00:00+02:00", "md": "3230", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH to 3400 m.", "dTimEnd": "2010-09-24T21:45:00+02:00", "dTimStart": "2010-09-24T21:15:00+02:00", "md": "3400", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Logged RST in Sigma mode from 3390 to 3230 m at 4,5 m/min.", "dTimEnd": "2010-09-24T22:30:00+02:00", "dTimStart": "2010-09-24T21:45:00+02:00", "md": "3230", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH to 3400 m.", "dTimEnd": "2010-09-24T22:45:00+02:00", "dTimStart": "2010-09-24T22:30:00+02:00", "md": "3400", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Logged RST-D in IC mode from 3390 to 3370 m at 0.5 m/min.", "dTimEnd": "2010-09-25T00:00:00+02:00", "dTimStart": "2010-09-24T22:45:00+02:00", "md": "3370", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2010_09_26
NO 15/9-F-4
NO 15/9-F-4
name
2010-09-25T00:00:00+02:00
2010-09-26T00:00:00+02:00
normal
2018-05-03T13:52:56+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2010-09-26T00:00:00+02:00", "dTimDiaHoleStart": "2010-09-23T16:30:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "None.", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "3", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Logged RST in IC mode from 3370 to 3230 m. Inflow tested HMV and DHSV. RD wireline pressure control equipment. Handed well over to Production department. Prepared wireline equipment for demobilization.", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Continued logging RST-D in IC mode from 3370 to 3260 m at 0.5 m/min.", "dTimEnd": "2010-09-25T06:00:00+02:00", "dTimStart": "2010-09-25T00:00:00+02:00", "md": "3260", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued logging RST-D in IC mode from 3260 to 3230 m at 0.5 m/min.", "dTimEnd": "2010-09-25T08:00:00+02:00", "dTimStart": "2010-09-25T06:00:00+02:00", "md": "3230", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with BHA #1.", "dTimEnd": "2010-09-25T10:45:00+02:00", "dTimStart": "2010-09-25T08:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "OOH. WHP 37 bar. Closed well and inflow tested HMV. Bled off and flushed lubricator with N2. Held toolbox meeting.", "dTimEnd": "2010-09-25T13:00:00+02:00", "dTimStart": "2010-09-25T10:45:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "LD RST toolstring and inspected same.", "dTimEnd": "2010-09-25T14:00:00+02:00", "dTimStart": "2010-09-25T13:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Closed BOP. Flushed riser with N2 through KWV to blow down.", "dTimEnd": "2010-09-25T14:45:00+02:00", "dTimStart": "2010-09-25T14:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Closed DHSV and bled down to 8 bar. Inflow tested DHSV. Bled off pressure above and closed well. Lined up and leak tested XMT cross.", "dTimEnd": "2010-09-25T16:15:00+02:00", "dTimStart": "2010-09-25T14:45:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox meeting and LD lubricator onto cat walk machine. Lifted upper riser section to rig floor with top drive. Lifted BOP away in moon pool. RD lower riser.", "dTimEnd": "2010-09-25T18:30:00+02:00", "dTimStart": "2010-09-25T16:15:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed chiksan manifold on KWV and installed end cap. Installed XMT top cap. Leak tested KWV end cap and XMT top cap to 20/345 bar for 5/10 min. Disconnected local control panel for HMV and DHSV.\nHanded well over to Production department.", "dTimEnd": "2010-09-25T21:00:00+02:00", "dTimStart": "2010-09-25T18:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Disassambled riser and lubricator and lifted out riser sections from rig floor.", "dTimEnd": "2010-09-26T00:00:00+02:00", "dTimStart": "2010-09-25T21:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2010_09_27
NO 15/9-F-4
NO 15/9-F-4
name
2010-09-26T00:00:00+02:00
2010-09-27T00:00:00+02:00
normal
2018-05-03T13:52:56+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2010-09-27T00:00:00+02:00", "dTimDiaHoleStart": "2010-09-23T16:30:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "None.", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3510", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "4", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Cleared rig floor off remaining WL equipment. Skidded rig in parking position. Prepared and packed WL equipment for demobilization.", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Cleared rig floor off remaining WL equipment.Tidied and cleaned rig floor. Skidded rig in parking position. Prepared and packed WL equipment for demobilization.\n---------------------------- END OF OPERATION --------------------------------------------", "dTimEnd": "2010-09-26T06:00:00+02:00", "dTimStart": "2010-09-26T00:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- rig up/down", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2012_09_12
NO 15/9-F-4
NO 15/9-F-4
name
2012-09-11T00:00:00+02:00
2012-09-12T00:00:00+02:00
normal
2018-05-03T13:52:57+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2012-09-12T00:00:00+02:00", "dTimDiaHoleStart": "2012-09-11T07:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Prepare wireline equipment for WL operation. Wait for access to well.\n\nExpected status tomorrow at 06:00: Waiting for access to well.", "hpht": "0", "md": "-999.99", "mdCsgLast": null, "mdDiaHoleStart": null, "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "1", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Received and spotted wireline equipment. Started to prepare equipment for wireline operation.", "tightWell": "0", "tvd": null, "tvdCsgLast": null, "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Received WL equipment from boat.", "dTimEnd": "2012-09-11T11:00:00+02:00", "dTimStart": "2012-09-11T07:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed containers, tanks, equipment and prepared pipe deck area for spotting wireline equipment.", "dTimEnd": "2012-09-11T13:00:00+02:00", "dTimStart": "2012-09-11T11:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Started to spot WL equipment on pipe deck.", "dTimEnd": "2012-09-11T17:00:00+02:00", "dTimStart": "2012-09-11T13:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Leak tested BOP on stump. Started to prepare WL equipment.", "dTimEnd": "2012-09-11T21:00:00+02:00", "dTimStart": "2012-09-11T17:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held Mearsk Toolbox Talk together with Maersk personnel prior to build lubricator.\nHeld AWS check card meeting prior to thread the cable through GIH and toolcatcher.", "dTimEnd": "2012-09-11T21:20:00+02:00", "dTimStart": "2012-09-11T21:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lifted and spotted Smart skid in front of winch. Lifted toolcatcher and GIH to rig floor. Threaded the cable through GIH and tool catcher, prior to build cable head. Built lubricator with fork lift on main deck.", "dTimEnd": "2012-09-12T00:00:00+02:00", "dTimStart": "2012-09-11T21:20:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2012_09_13
NO 15/9-F-4
NO 15/9-F-4
name
2012-09-12T00:00:00+02:00
2012-09-13T00:00:00+02:00
normal
2018-05-03T13:52:57+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2012-09-13T00:00:00+02:00", "dTimDiaHoleStart": "2012-09-11T07:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Get access to well. R/U wireline equipment.\n\nExpected status tomorrow at 06:00: Logging RST.", "hpht": "0", "md": "-999.99", "mdCsgLast": null, "mdDiaHoleStart": null, "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "2", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Waited on Mearsk electrician, prior to hook up all wireline units. Hooked up wireline units to power and F&G. Prepared wireline equipment and build cable head. Waited for Production Department to prepare well for handover.", "tightWell": "0", "tvd": null, "tvdCsgLast": null, "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Waited on Mearsk electrician, prior to hook up all wireline units. Electrician busy with other jobs.\nMeanwhile lifted BOP down to BOP deck through hatch on drill floor and prepared wireline equipment.", "dTimEnd": "2012-09-12T06:00:00+02:00", "dTimStart": "2012-09-12T00:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited on Mearsk electrician, prior to hook up all wireline units. Electrician busy with other jobs.\nMeanwhile prepared wireline equipment.", "dTimEnd": "2012-09-12T09:00:00+02:00", "dTimStart": "2012-09-12T06:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Hooked up wireline units to power and F&G.", "dTimEnd": "2012-09-12T12:00:00+02:00", "dTimStart": "2012-09-12T09:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Assembled lubricator and riser on rig floor.", "dTimEnd": "2012-09-12T14:00:00+02:00", "dTimStart": "2012-09-12T12:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Prepared wireline equipment. Meanwhile built cable head.", "dTimEnd": "2012-09-12T17:00:00+02:00", "dTimStart": "2012-09-12T14:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited for Production Department to prepare well for handover. Meanwhile built cable head and megged same. Tried to connect logging unit to internet, no success.", "dTimEnd": "2012-09-12T21:00:00+02:00", "dTimStart": "2012-09-12T17:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited for Production Department to prepare well for handover. Meanwhile held start up meeting with night crew.", "dTimEnd": "2012-09-12T21:30:00+02:00", "dTimStart": "2012-09-12T21:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited for Production Department to prepare well for handover. Meanwhile tested counter system and RST tool.", "dTimEnd": "2012-09-13T00:00:00+02:00", "dTimStart": "2012-09-12T21:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2012_09_14
NO 15/9-F-4
NO 15/9-F-4
name
2012-09-13T00:00:00+02:00
2012-09-14T00:00:00+02:00
normal
2018-05-03T13:52:57+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2012-09-14T00:00:00+02:00", "dTimDiaHoleStart": "2012-09-11T07:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Leak test R/U. RIH and log RST.\n\nExpected status tomorrow at 06:00: POOH with RST toolstring.", "hpht": "0", "md": "-999.99", "mdCsgLast": null, "mdDiaHoleStart": null, "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "3", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Well handed over from production department. R/U wireline equipment and installed RST toolstring in lubricator.", "tightWell": "0", "tvd": null, "tvdCsgLast": null, "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Waited for Production Department to prepare well for handover. Meanwhile tested RST tool.", "dTimEnd": "2012-09-13T06:00:00+02:00", "dTimStart": "2012-09-13T00:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited for Production Department to prepare well for handover. Meanwhile tested RST tool.", "dTimEnd": "2012-09-13T10:30:00+02:00", "dTimStart": "2012-09-13T06:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Well handed over from production department.", "dTimEnd": "2012-09-13T11:00:00+02:00", "dTimStart": "2012-09-13T10:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held DOP#1 meeting prior to R/U on well.", "dTimEnd": "2012-09-13T11:30:00+02:00", "dTimStart": "2012-09-13T11:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Leak tested XMT cross to 20/120 bar for 5/10 min. Meanwhile prepared to install lower riser and BOP.", "dTimEnd": "2012-09-13T13:00:00+02:00", "dTimStart": "2012-09-13T11:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held brief prior to install lower riser and BOP.", "dTimEnd": "2012-09-13T13:30:00+02:00", "dTimStart": "2012-09-13T13:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed XMT top cap and installed lower riser and BOP. Leak tested lower riser/BOP connections to 20/120 bar for 5/10 min.", "dTimEnd": "2012-09-13T16:30:00+02:00", "dTimStart": "2012-09-13T13:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lowered down lower lubricator from rig floor and stabbed lubricator onto BOP.", "dTimEnd": "2012-09-13T17:15:00+02:00", "dTimStart": "2012-09-13T16:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held brief prior to install toolstring into lubricator.", "dTimEnd": "2012-09-13T17:30:00+02:00", "dTimStart": "2012-09-13T17:15:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed toolstring into lubricator.", "dTimEnd": "2012-09-13T19:00:00+02:00", "dTimStart": "2012-09-13T17:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held brief prior to lift up lubricator and GIH in elevator.", "dTimEnd": "2012-09-13T19:30:00+02:00", "dTimStart": "2012-09-13T19:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Connected hoses and lifted up lubricator and GIH in elevator. Connected toolstring and stabbed upper lubricator unto lower lubricator.", "dTimEnd": "2012-09-13T22:30:00+02:00", "dTimStart": "2012-09-13T19:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held DOP#2 meeting prior to RIH with RST toolstring.", "dTimEnd": "2012-09-13T23:00:00+02:00", "dTimStart": "2012-09-13T22:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Prepared to leak test R/U.", "dTimEnd": "2012-09-14T00:00:00+02:00", "dTimStart": "2012-09-13T23:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2012_09_15
NO 15/9-F-4
NO 15/9-F-4
name
2012-09-14T00:00:00+02:00
2012-09-15T00:00:00+02:00
normal
2018-05-03T13:52:57+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2012-09-15T00:00:00+02:00", "dTimDiaHoleStart": "2012-09-11T07:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Log RST-D in IC mode pass#3. R/D. R/U on well F-5.\n\nExpected status tomorrow at 06:00: R/U on well F-5.", "hpht": "0", "md": "-999.99", "mdCsgLast": null, "mdDiaHoleStart": null, "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "4", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Leak tested R/U. Opened well. RIH and logged RST-D in sigma mode and RST-D in IC mode pass#1 and pass#2.", "tightWell": "0", "tvd": null, "tvdCsgLast": null, "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Leak tested R/U to 20/120 bar for 5/10 min. Opened well. WHP = 42 bar.", "dTimEnd": "2012-09-14T02:00:00+02:00", "dTimStart": "2012-09-14T00:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held well controll drill prior to RIH.", "dTimEnd": "2012-09-14T02:15:00+02:00", "dTimStart": "2012-09-14T02:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with BHA#1, RST to 556 m.", "dTimEnd": "2012-09-14T02:50:00+02:00", "dTimStart": "2012-09-14T02:15:00+02:00", "md": "556", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed test of RST according to Schlumberger procedure.", "dTimEnd": "2012-09-14T03:20:00+02:00", "dTimStart": "2012-09-14T02:50:00+02:00", "md": "556", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued RIH with BHA#1, RST to 3420 m.", "dTimEnd": "2012-09-14T05:20:00+02:00", "dTimStart": "2012-09-14T03:20:00+02:00", "md": "3420", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Ran correlation passes. Adjusted the depth according to reference log.", "dTimEnd": "2012-09-14T06:00:00+02:00", "dTimStart": "2012-09-14T05:20:00+02:00", "md": "3420", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Logged RST-D in Sigma mode from 3400 to 3210 m at 4,5 m/min.", "dTimEnd": "2012-09-14T07:05:00+02:00", "dTimStart": "2012-09-14T06:00:00+02:00", "md": "3210", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH to 3420 m.", "dTimEnd": "2012-09-14T07:30:00+02:00", "dTimStart": "2012-09-14T07:05:00+02:00", "md": "3420", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Logged RST-D in IC mode pass#1 from 3410 to 3215 m at 0,5 m/min.", "dTimEnd": "2012-09-14T14:20:00+02:00", "dTimStart": "2012-09-14T07:30:00+02:00", "md": "3215", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH to 3420 m.", "dTimEnd": "2012-09-14T15:00:00+02:00", "dTimStart": "2012-09-14T14:20:00+02:00", "md": "3420", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Logged RST-D in IC mode pass#2 from 3410 to 3215 m at 0,5 m/min.", "dTimEnd": "2012-09-14T23:00:00+02:00", "dTimStart": "2012-09-14T15:00:00+02:00", "md": "3215", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH to 3420 m.", "dTimEnd": "2012-09-14T23:30:00+02:00", "dTimStart": "2012-09-14T23:00:00+02:00", "md": "3420", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Logged RST-D in IC mode pass#3 from 3410 to 3380 m at 0,5 m/min.", "dTimEnd": "2012-09-15T00:00:00+02:00", "dTimStart": "2012-09-14T23:30:00+02:00", "md": "3380", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2012_09_16
NO 15/9-F-4
NO 15/9-F-4
name
2012-09-15T00:00:00+02:00
2012-09-16T00:00:00+02:00
normal
2018-05-03T13:52:57+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2012-09-16T00:00:00+02:00", "dTimDiaHoleStart": "2012-09-11T07:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "None", "hpht": "0", "md": "-999.99", "mdCsgLast": null, "mdDiaHoleStart": null, "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "5", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Logged RST-D in IC mode pass#3. POOH. R/D and handed well over to production department.", "tightWell": "0", "tvd": null, "tvdCsgLast": null, "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Logged RST-D in IC mode pass#3 from 3380 to 3250 m at 0,5 m/min.", "dTimEnd": "2012-09-15T06:00:00+02:00", "dTimStart": "2012-09-15T00:00:00+02:00", "md": "3180", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued logging RST-D in IC mode pass#3 from 3250 to 3220 m at 0,5 m/min.", "dTimEnd": "2012-09-15T07:40:00+02:00", "dTimStart": "2012-09-15T06:00:00+02:00", "md": "3220", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH from 3220 m to surface. WHP:42 bar.", "dTimEnd": "2012-09-15T09:30:00+02:00", "dTimStart": "2012-09-15T07:40:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "OOH. Closed in SWAB and HMV. Inflow tested same. Opened HMV and inflow tested DHSV.", "dTimEnd": "2012-09-15T11:00:00+02:00", "dTimStart": "2012-09-15T09:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- test scsssv", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/D upper lubricator on drill floor and removed BHA#1, RST-D logging tool.", "dTimEnd": "2012-09-15T12:30:00+02:00", "dTimStart": "2012-09-15T11:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed brief prior to rig down.", "dTimEnd": "2012-09-15T13:00:00+02:00", "dTimStart": "2012-09-15T12:30:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lifted lower lubricator to rig floor with top drive. Lifted BOP away in moon pool. R/D lower riser.", "dTimEnd": "2012-09-15T15:10:00+02:00", "dTimStart": "2012-09-15T13:00:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed chiksan manifold on KWV and installed end cap. Installed XMT top cap. Leak tested KWV end cap and XMT top cap to 20/345 bar for 5/10 min. Disconnected local panal for HMV and DHSV. Handed well over to production department.\n---------------------------------------- END OF OPERATION-------------------------------------------------", "dTimEnd": "2012-09-15T19:00:00+02:00", "dTimStart": "2012-09-15T15:10:00+02:00", "md": "0", "phase": "wire line", "proprietaryCode": "workover -- wire line", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2016_10_01
NO 15/9-F-4
NO 15/9-F-4
name
2016-09-30T00:00:00+02:00
2016-10-01T00:00:00+02:00
normal
2018-05-03T13:52:57+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2016-10-01T00:00:00+02:00", "dTimDiaHoleStart": null, "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "- R/U cement spool\n- Bullhead well to sea water\n\n", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": null, "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "1", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "- Skidded cantilever to enable to position winch for gas export lines\n- Installed winch for gas export lines\n- Suspended skidding to F-4 due to problem with glide plates. Worked on solution", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[]
[]
15_9_F_4_2016_10_02
NO 15/9-F-4
NO 15/9-F-4
name
2016-10-01T00:00:00+02:00
2016-10-02T00:00:00+02:00
normal
2018-05-03T13:52:57+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2016-10-02T00:00:00+02:00", "dTimDiaHoleStart": "2016-10-01T15:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "- R/U cement head\n- Bullhead well to sea water\n- Bullhead cement in 7in liner/perfs\n- WOC\n", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3500", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "1", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "- Troubleshoot problems with skidding system\n- Skidded cantilever to F-4\n- Tested Xmas tree valves\n- Started R/U cement head", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Reporting continued from F-99.\n\nContinued to skid cantilever to F-04 9m inboard/1.25m port. Continued work with Aft PRS", "dTimEnd": "2016-10-01T16:00:00+02:00", "dTimStart": "2016-10-01T15:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed covers to skidding system. Meanwhile held TBT for connecting HP hose to F-04 and for removal of well head cover/installation of split cover", "dTimEnd": "2016-10-01T16:30:00+02:00", "dTimStart": "2016-10-01T16:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Connected HP hose to F-04. Meanwhile tested aft PRS. Prepared subs for pressure testing", "dTimEnd": "2016-10-01T17:30:00+02:00", "dTimStart": "2016-10-01T16:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed line test down to XMT. Performed test of XMT cross 20/345bar for 5/10min. Good test", "dTimEnd": "2016-10-01T19:00:00+02:00", "dTimStart": "2016-10-01T17:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to remove moonpool hatches", "dTimEnd": "2016-10-01T19:15:00+02:00", "dTimStart": "2016-10-01T19:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed hatches and installed split hatch", "dTimEnd": "2016-10-01T20:15:00+02:00", "dTimStart": "2016-10-01T19:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Adjusted scaffolding around Xmas tree. Prepared lines and bled off A and B annulus to MGS. Worked to fill A and B annulus with sea water. Bled off pressure and removed Tree cap from Xmas tree w/ rigfloor winch", "dTimEnd": "2016-10-01T21:30:00+02:00", "dTimStart": "2016-10-01T20:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Hooked up hydraulic pump for local control of DHSV an HMV. Meanwhile worked to fill A and B annulus with sea water, carried out TBT for R/U cement head", "dTimEnd": "2016-10-01T23:45:00+02:00", "dTimStart": "2016-10-01T21:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Worked to P/U cement head in moonpool using overhead crane and transfered to TDS lifting chains", "dTimEnd": "2016-10-02T00:00:00+02:00", "dTimStart": "2016-10-01T23:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2016_10_03
NO 15/9-F-4
NO 15/9-F-4
name
2016-10-02T00:00:00+02:00
2016-10-03T00:00:00+02:00
normal
2018-05-03T13:52:57+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2016-10-03T00:00:00+02:00", "dTimDiaHoleStart": "2016-10-01T15:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "- N/D Xmas tree and spacer spool\n- N/U high pressure riser and BOP\n- Install THRT and release TH", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3500", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "2", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "- R/U cement head\n- Bullheaded well to sea water\n- Bullhead cement in 7in liner/perfs\n- Worked to test BOP, meanwhile WOC\n- Pressure tested and inflow tested cement plug\n- Inflow tested DHSV\n- R/D cement head\n- Installed BPV plug\n", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Worked to P/U cement head in moonpool using overhead crane and transfered to TDS lifting chains", "dTimEnd": "2016-10-02T00:45:00+02:00", "dTimStart": "2016-10-02T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "M/U cement head to the Xmas tree, installed split hatch in moonpool", "dTimEnd": "2016-10-02T01:45:00+02:00", "dTimStart": "2016-10-02T00:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Built scaffolding around cement head in moonpool", "dTimEnd": "2016-10-02T03:30:00+02:00", "dTimStart": "2016-10-02T01:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to pressure test cement head", "dTimEnd": "2016-10-02T03:45:00+02:00", "dTimStart": "2016-10-02T03:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Confirmed line up, flushed and pressure tested cement head and bleed off manifold to 20/345 bar for 5/10 min", "dTimEnd": "2016-10-02T04:45:00+02:00", "dTimStart": "2016-10-02T03:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting before bullheading operation", "dTimEnd": "2016-10-02T05:00:00+02:00", "dTimStart": "2016-10-02T04:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up to pump into the well. Opened HMV. Wellhead pressure went up to 20 bar. Bled off pressure to MGS. Pressured up DHSV control line to 520bar. Pressured up above DHSV to equalize pressure. Observed indecation of DHSV openning on hydraulic pump pressure gauge.", "dTimEnd": "2016-10-02T05:30:00+02:00", "dTimStart": "2016-10-02T05:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pumped 10m3 of wash pill, 1100 l/min - 134bar", "dTimEnd": "2016-10-02T06:00:00+02:00", "dTimStart": "2016-10-02T05:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Bullheaded sea water into the well, 1300 l/min - 143 bar, totally pumped 140m3. Meanwhile carried out TBT for cement job", "dTimEnd": "2016-10-02T08:00:00+02:00", "dTimStart": "2016-10-02T06:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up valves on the cement head, released bottom dart, mixed and pumped 13.6m3 1,90SG cement, 600l/min. Pressure 130 bar, decreasing to 90bar, indicating cement moving down in the tubing. Displaced lines w/ 0,9m3 of Hi-vis pill. Released top dart. Pumped 12,2m3 of Hi-vis (totally pumped 13,1m3 of Hi-vis). Displaced w/ 37,7m3 of sea water at initial rate of 1000lpm. Increased pumping rate to 1300l/min - 101bar. Reduced pumping rate in the end of displacement to 700l/min - 83bar. Switched to contamination pill. Observed rapid increase in pressure while pumping contamination pill indicating cement plugging into perforations. Shut down after having pumped 3,5m3 contamination pill, 111 bar and monitored WH pressure decline. Recorded final stabilized squeeze pressure of 60bar. Closed swab valve. \nVerified volumes pumped by checking volumes left in the pits and silos. Theoretical top of cement 2755mMD. DHSV was cycled 3 times after 30m3 of sea water displacement was pumped", "dTimEnd": "2016-10-02T09:45:00+02:00", "dTimStart": "2016-10-02T08:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Flushed manifolds after cement job. Worked aloft in derrick to repair crown grease system. Lined up and prepare to pressure test BOP. Meanwhile WOC", "dTimEnd": "2016-10-02T13:00:00+02:00", "dTimStart": "2016-10-02T09:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed BOP test No1 20/345 bar 5/10 minutes. Cycleed HMV and MMV. Meanwhile WOC", "dTimEnd": "2016-10-02T13:45:00+02:00", "dTimStart": "2016-10-02T13:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up for BOP test No2, flushed 0.5m3 through kill and choke lines", "dTimEnd": "2016-10-02T14:45:00+02:00", "dTimStart": "2016-10-02T13:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed BOP test No2 20/345 bar 5/10 minutes. Cycled HMV and MMV. Meanwhile pumped out dirty side of skimmer tank to mill tank, WOC", "dTimEnd": "2016-10-02T15:45:00+02:00", "dTimStart": "2016-10-02T14:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up and performed BOP test No3 20/345 bar 5/10 minutes. Continued to clear out dirty side of skimmer tank, transfered to mud pits 7.5m3. Lined up to bleed off pressure from XMT 110bar down to 62bar. Meanwhile WOC", "dTimEnd": "2016-10-02T17:00:00+02:00", "dTimStart": "2016-10-02T15:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Opened all low torque valves on cement head and pressure tested rig up against SV to 310 bar/10 minutes. Meanwhile WOC", "dTimEnd": "2016-10-02T17:30:00+02:00", "dTimStart": "2016-10-02T17:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Closed HMV , bled off pressure above HMV from 72bar to 0. Opened SV, pressured up to 72bar to equalize, opened HMV. Pressured up well against cement plug with cement pump to 310bar/10min. Pumped 620liters. Good pressure test.", "dTimEnd": "2016-10-02T18:15:00+02:00", "dTimStart": "2016-10-02T17:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Carried out inflow test of cement plug. Bled down pressure in tubing to 10 bar. Monitored pressure pressure for 30 min. Pressure increased 3.6 bar with clear decreasing trend towards the end. Good inflow test", "dTimEnd": "2016-10-02T19:15:00+02:00", "dTimStart": "2016-10-02T18:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Carried out inflow test of DHSV. Equalized pressure and opened swab valve, applied 310 bar to tubing. 770l pumped. Closed DHSV. Bled off pressure in tubing above DHSV to 240 bar. Monitored pressure above DHSV for 30 min for 70bar LP inflow test. Pressure increased 1.5bar in 30 min with decreasing trend towards the end. Good LP inflow test. Bled down pressure in tubing above DHSV to 10bar. 110l bled off. Monitored pressure above DHSV for 30 min for 300bar HP inflow test. Pressure increased 2,4bar in 30 min with decreasing trend towards the end. Good HP inflow test. Equalized pressure above DHSV, pressured up control line to DHSV to 520bar to open DHSV. Bled off tubing pressure to 20bar. 710l bled off. Closed DHSV. Bled off remaining pressure from Xmas tree. Meanwhile performed TBT to R/D cement head", "dTimEnd": "2016-10-02T22:00:00+02:00", "dTimStart": "2016-10-02T19:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Closed SV. R/D cement head. Removed hydraulic control hoses to HMV and DHSV. Broke off bleed off manifold from kill wing side", "dTimEnd": "2016-10-02T23:30:00+02:00", "dTimStart": "2016-10-02T22:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Worked to installed BPV plug for drop protection and Xmas tree lifting cap. Meanwhile performed BOP test No4", "dTimEnd": "2016-10-03T00:00:00+02:00", "dTimStart": "2016-10-02T23:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2016_10_04
NO 15/9-F-4
NO 15/9-F-4
name
2016-10-03T00:00:00+02:00
2016-10-04T00:00:00+02:00
normal
2018-05-03T13:52:57+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2016-10-04T00:00:00+02:00", "dTimDiaHoleStart": "2016-10-01T15:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "- Engage THRT and release TH\n- R/U WL, cut tubing on WL\n- Pull TH\n- Pull 7in tubing", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3500", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "2755", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "3", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "- Installed BPV plug\n- N/D Xmas tree and spacer spool\n- N/U high pressure riser and BOP\n- Retrieved BPV plug\n- P/U THRT", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Continued to install BPV plug for drop protection and Xmas tree lifting cap. Meanwhile worked to perform BOP test No5", "dTimEnd": "2016-10-03T00:15:00+02:00", "dTimStart": "2016-10-03T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Remove scaffolding from around Xmas tree and R/D electric and hydraulic lines from Xmas tree. Meanwhile performed pre-job meeting to N/D Xmas tree, pressure tested BOP test No5", "dTimEnd": "2016-10-03T02:30:00+02:00", "dTimStart": "2016-10-03T00:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed hatches and beam between slots. Meanwhile worked to pressure test BOP test No6, 7", "dTimEnd": "2016-10-03T03:15:00+02:00", "dTimStart": "2016-10-03T02:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed master bushing and outer ring. Lowered diverter chains on TDS bails to wellhead and attached to X-tree. Meanwhile pressure tested BOP test No7", "dTimEnd": "2016-10-03T04:00:00+02:00", "dTimStart": "2016-10-03T03:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to lift Xmas tree", "dTimEnd": "2016-10-03T04:15:00+02:00", "dTimStart": "2016-10-03T04:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Took weight as per lifting plan and removed Grayloc clamp. Lifted X-tree to moonpool. Transfered load to gantry crane in moonpool. Attached lifting arrangement from TDS to Spacer spool", "dTimEnd": "2016-10-03T05:15:00+02:00", "dTimStart": "2016-10-03T04:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Released NT-2 connector on wellhead, had difficulties to release 2x tight bolts. Meanwhile prepared HP riser on rig floor", "dTimEnd": "2016-10-03T06:30:00+02:00", "dTimStart": "2016-10-03T05:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cut control lines, installed communication collar and dart on BPV, cleaned up seal area. Meanwhile P/U riser from HTS", "dTimEnd": "2016-10-03T08:15:00+02:00", "dTimStart": "2016-10-03T06:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed covers in moonpool using rigfloor winch", "dTimEnd": "2016-10-03T08:45:00+02:00", "dTimStart": "2016-10-03T08:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "P/U and RIH HP riser and M/U NT-2 connector", "dTimEnd": "2016-10-03T09:15:00+02:00", "dTimStart": "2016-10-03T08:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed scaffolding from test stump and built scaffolding around HP Riser. Performed checks prior to skid BOP to well center. Meanwhile worked to M/U TDS test assembly", "dTimEnd": "2016-10-03T11:00:00+02:00", "dTimStart": "2016-10-03T09:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to move BOP to well center", "dTimEnd": "2016-10-03T11:15:00+02:00", "dTimStart": "2016-10-03T11:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Skidded BOP to well center and landed off on HP riser. Meanwhile pressure tested kelly hose to 20/345 bar, 5/10 min", "dTimEnd": "2016-10-03T12:00:00+02:00", "dTimStart": "2016-10-03T11:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to M/U NT-2 connector", "dTimEnd": "2016-10-03T12:15:00+02:00", "dTimStart": "2016-10-03T12:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "M/U NT-2 connector. Meanwhile pressure tested upper/lower IBOPs and 2x FOSVs to 20/345 bar, 5/10 min", "dTimEnd": "2016-10-03T13:30:00+02:00", "dTimStart": "2016-10-03T12:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to connect tension cylinders", "dTimEnd": "2016-10-03T13:45:00+02:00", "dTimStart": "2016-10-03T13:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/U tension system", "dTimEnd": "2016-10-03T15:00:00+02:00", "dTimStart": "2016-10-03T13:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to handle slick joint", "dTimEnd": "2016-10-03T15:15:00+02:00", "dTimStart": "2016-10-03T15:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed master bushing, RIH with Slick joint and M/U same, measured RKB to top of Annular = 5.78m", "dTimEnd": "2016-10-03T16:00:00+02:00", "dTimStart": "2016-10-03T15:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to handle diverter", "dTimEnd": "2016-10-03T16:15:00+02:00", "dTimStart": "2016-10-03T16:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "P/U and RIH w/ diverter and landed off. Continued M/U slick joint. Meanwhile removed chains from bails and connected overshot hose. Energized overshot, lined up and filled hole with 3m3. No leaks observed", "dTimEnd": "2016-10-03T17:45:00+02:00", "dTimStart": "2016-10-03T16:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up cement unit through kill HCR, closed BSRs. Applied 20 bar to kill HCR valve to confirm line up", "dTimEnd": "2016-10-03T18:00:00+02:00", "dTimStart": "2016-10-03T17:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "With slick joint made up, fine tuned tension cylinders for equal pull", "dTimEnd": "2016-10-03T18:30:00+02:00", "dTimStart": "2016-10-03T18:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed connection test to 20/345 bar 5/10 min, good test", "dTimEnd": "2016-10-03T19:00:00+02:00", "dTimStart": "2016-10-03T18:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Finished to M/U slick joints, cleaned and cleared rig floor", "dTimEnd": "2016-10-03T19:30:00+02:00", "dTimStart": "2016-10-03T19:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Changed handling equipment to 3.5in DP", "dTimEnd": "2016-10-03T20:00:00+02:00", "dTimStart": "2016-10-03T19:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to retrieve dart and BPV", "dTimEnd": "2016-10-03T20:15:00+02:00", "dTimStart": "2016-10-03T20:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Retrieved dart from BPV", "dTimEnd": "2016-10-03T21:15:00+02:00", "dTimStart": "2016-10-03T20:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Retrieved BPV", "dTimEnd": "2016-10-03T21:45:00+02:00", "dTimStart": "2016-10-03T21:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/B 3.5in DP, L/D retrieval tool", "dTimEnd": "2016-10-03T22:15:00+02:00", "dTimStart": "2016-10-03T21:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Changed handling gear, prepared for running THRT", "dTimEnd": "2016-10-03T22:30:00+02:00", "dTimStart": "2016-10-03T22:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to R/U casing tong", "dTimEnd": "2016-10-03T22:45:00+02:00", "dTimStart": "2016-10-03T22:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/U casing tong", "dTimEnd": "2016-10-03T23:30:00+02:00", "dTimStart": "2016-10-03T22:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to run w/ THRT and landing string", "dTimEnd": "2016-10-03T23:45:00+02:00", "dTimStart": "2016-10-03T23:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "P/U and RIH with tubing hanger running tool (THRT).", "dTimEnd": "2016-10-04T00:00:00+02:00", "dTimStart": "2016-10-03T23:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2016_10_05
NO 15/9-F-4
NO 15/9-F-4
name
2016-10-04T00:00:00+02:00
2016-10-05T00:00:00+02:00
normal
2018-05-03T13:52:57+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2016-10-05T00:00:00+02:00", "dTimDiaHoleStart": "2016-10-01T15:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "- Pull the rest of tubing\n- RIH w/ tubing on DP\n- Circulate well to sea water\n- Place balanced cement plug\n- WOC", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3500", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "2755", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "4", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "- Engaged THRT and released TH\n- R/U WL, cut tubing on WL\n- Pulled TH\n- Pulled 7in tubing to 2109m", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Continued to P/U and M/U tubingTHRT and landing string. POOH, installed control lines and inspected THRT. RIH and landed off THRT on TH. Observed top box of landing string is too high for casing tong to be able to M/U swedge.", "dTimEnd": "2016-10-04T02:00:00+02:00", "dTimStart": "2016-10-04T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to rearrange landing string to be able to M/U swedge w/ casing tong. Started to position upper pup joint of landing string for casing tong to break off. Observed hydraulic oil leak from elevator", "dTimEnd": "2016-10-04T02:15:00+02:00", "dTimStart": "2016-10-04T02:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- repair", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Identified faulty hydraulic hose inside of the elevator and changed same", "dTimEnd": "2016-10-04T03:00:00+02:00", "dTimStart": "2016-10-04T02:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- repair", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke top 6m pup from landing string. M/U swedge using aft PRS and casing tong. Realized that it is not possible to break swedge while connected to TH with THRT. Broke off swedge using aft PRS and casing tong. Located 4m tubing joint (3m + 1m pups) on the pipe deck. M/U same to landing string, M/U 1m pup joint to landing string. Achieved sufficient stick up to be able to M/U swedge", "dTimEnd": "2016-10-04T05:30:00+02:00", "dTimStart": "2016-10-04T03:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- repair", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Attempted to engage THRT to TH. No success, POOH, checked THRT, observed shear pins sheared prematurely. Repaired THRT", "dTimEnd": "2016-10-04T06:15:00+02:00", "dTimStart": "2016-10-04T05:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- repair", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH and landed off THRT, engaged tool and confirmed w/ 2t overpull. Applied pressure to shear pin and then rotated string 8x turns CCW into communication collar", "dTimEnd": "2016-10-04T07:00:00+02:00", "dTimStart": "2016-10-04T06:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Connected cement hose and LT valve, flushed hose. Pressure tested same to 100 bar. Lined up pumps through cement hose. Applied pressure of 520bar to DHSV control lines. Pressured up well above DHSV, observed DHSV equalized and opened at 100 bar pressure. No indications of gas below DHSV/in the well observed. Bled off pressure from the well through the cement hose to MGS to 0. Closed DHSV. Verified no pressure in the A-annulus", "dTimEnd": "2016-10-04T08:00:00+02:00", "dTimStart": "2016-10-04T07:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke off swedge", "dTimEnd": "2016-10-04T08:15:00+02:00", "dTimStart": "2016-10-04T08:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Released TH and and pulled 180t on hook load. String stretch of 0,75m", "dTimEnd": "2016-10-04T08:30:00+02:00", "dTimStart": "2016-10-04T08:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to R/U WL equipment", "dTimEnd": "2016-10-04T08:45:00+02:00", "dTimStart": "2016-10-04T08:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/U wireline equipment", "dTimEnd": "2016-10-04T09:30:00+02:00", "dTimStart": "2016-10-04T08:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH w/ cutter BHA, run #9 from surface 2616 m. Average running speed 20 m/min.", "dTimEnd": "2016-10-04T11:45:00+02:00", "dTimStart": "2016-10-04T09:30:00+02:00", "md": "2616", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Correlated across interval 2616 - 2638 . Positioned cutter at 2621 m . Performed cut. Observed backflow from pipe after tubing was cut", "dTimEnd": "2016-10-04T13:00:00+02:00", "dTimStart": "2016-10-04T11:45:00+02:00", "md": "2621", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH from 2621 m to surface. Average pulling speed 22 m/min. Backflow at rotary gradually decreased and eventually stopped", "dTimEnd": "2016-10-04T15:00:00+02:00", "dTimStart": "2016-10-04T13:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/D wireline equipment", "dTimEnd": "2016-10-04T15:30:00+02:00", "dTimStart": "2016-10-04T15:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed flowcheck. Static", "dTimEnd": "2016-10-04T15:45:00+02:00", "dTimStart": "2016-10-04T15:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH w/ tubing and tubing hanger on landing string. Spooled control line. L/D landing string and TH on deck", "dTimEnd": "2016-10-04T17:00:00+02:00", "dTimStart": "2016-10-04T15:45:00+02:00", "md": "2600", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed casing slips and control line spooler", "dTimEnd": "2016-10-04T17:45:00+02:00", "dTimStart": "2016-10-04T17:00:00+02:00", "md": "2600", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to pull and L/D 7in tubing", "dTimEnd": "2016-10-04T18:00:00+02:00", "dTimStart": "2016-10-04T17:45:00+02:00", "md": "2600", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/D 3x pup joints", "dTimEnd": "2016-10-04T18:15:00+02:00", "dTimStart": "2016-10-04T18:00:00+02:00", "md": "2595", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled and L/D 2x joints of tubing", "dTimEnd": "2016-10-04T19:00:00+02:00", "dTimStart": "2016-10-04T18:15:00+02:00", "md": "2573", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to pull and L/D 7in tubing w/ new crew", "dTimEnd": "2016-10-04T19:15:00+02:00", "dTimStart": "2016-10-04T19:00:00+02:00", "md": "2573", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Checked red zone barriers and equipment", "dTimEnd": "2016-10-04T19:30:00+02:00", "dTimStart": "2016-10-04T19:15:00+02:00", "md": "2573", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pull and L/D 7in tubing from 2573m to 2109m, spooled control line. Pulled and L/D DHSV assembly. Average pulling speed 8,5 joints/hour. Totally pulled 39joints and DHSV assy", "dTimEnd": "2016-10-05T00:00:00+02:00", "dTimStart": "2016-10-04T19:30:00+02:00", "md": "2109", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2016_10_06
NO 15/9-F-4
NO 15/9-F-4
name
2016-10-05T00:00:00+02:00
2016-10-06T00:00:00+02:00
normal
2018-05-03T13:52:57+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2016-10-06T00:00:00+02:00", "dTimDiaHoleStart": "2016-10-01T15:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "- Tag cement w/ tubing\n- Release spear from tubing, \n- POOH w/ spear and L/D 5.5in DP\n- Retrieve MS-T seal\n- Cut 10 3/4in surface tieback\n- Pull and L/D 10 3/4in surface tieback casing\n- Release tieback adapter", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3500", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "2755", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "5", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "- Finished pulling and L/D 7in tubing\n- Circulated well clean to sea water\n- Placed balanced cement plug in 9 5/8in casing\n- L/D 300m of 5.5in DP\n- Engaged spear and RIH w/ 7in tubing on spear\n- WOC", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2016-10-05T15:40:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "-999.99", "mudClass": "water based", "presBopRating": "345", "pv": "-999.99", "tempHthp": null, "type": "Seawater", "visFunnel": "-999.99", "yp": "-999.99" } ]
[]
[]
[ { "comments": "Pulled and L/D the remaining 5x joints of 7in tubing. Average pulling speed 7joints/hour. Totally pulled 45x joints and DHSV assy", "dTimEnd": "2016-10-05T00:30:00+02:00", "dTimStart": "2016-10-05T00:00:00+02:00", "md": "2049", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to M/U swedge", "dTimEnd": "2016-10-05T00:45:00+02:00", "dTimStart": "2016-10-05T00:30:00+02:00", "md": "2049", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "M/U swedge assembly w/ casing tong", "dTimEnd": "2016-10-05T01:15:00+02:00", "dTimStart": "2016-10-05T00:45:00+02:00", "md": "2049", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed control line drum. Moved casing tong. Broke off swedge from FOSV. Install 5,5in inserts in BX elevator. M/U 1x std of 5,5in DP. Removed casing slips and installed DP slips. Cleared rig floor", "dTimEnd": "2016-10-05T03:00:00+02:00", "dTimStart": "2016-10-05T01:15:00+02:00", "md": "2049", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH w/ 7in tubing on 5,5in DP from 2049m to 2291. Average RIH speed 485m/hour", "dTimEnd": "2016-10-05T03:30:00+02:00", "dTimStart": "2016-10-05T03:00:00+02:00", "md": "2049", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Filled pipe", "dTimEnd": "2016-10-05T03:45:00+02:00", "dTimStart": "2016-10-05T03:30:00+02:00", "md": "2291", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH w/ 7in tubing on 5,5in DP from 2291m to 2616m. Average RIH speed 650 m/hour", "dTimEnd": "2016-10-05T04:15:00+02:00", "dTimStart": "2016-10-05T03:45:00+02:00", "md": "2616", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting prior to circulating well to sea water", "dTimEnd": "2016-10-05T04:30:00+02:00", "dTimStart": "2016-10-05T04:15:00+02:00", "md": "2616", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Started to circulate well to sea water. Staged up pumps to 3000 l/min - 78bar. Observed dirty fluid in returns. OIW reading is above 100ppm. No gas. After 50m3 pumped pulled 3m above combination wiper plug. Continued circulating. Shakers overflowed, reduced the rate to 2200l/min - 56bar. Circulated additional 112 m3. Observed clear returns after total of 162 m3 pumped. OIW content less than 30 ppm. Stopped pumps. Installed pump in sub w/ LT valve.", "dTimEnd": "2016-10-05T06:00:00+02:00", "dTimStart": "2016-10-05T04:30:00+02:00", "md": "2616", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/B 1x stand. Installed side entry sub assembly and connected cement hose, spaced out to 2614m bottom of tubing string", "dTimEnd": "2016-10-05T06:45:00+02:00", "dTimStart": "2016-10-05T06:00:00+02:00", "md": "2614", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up/prepared to pump wash pill", "dTimEnd": "2016-10-05T07:00:00+02:00", "dTimStart": "2016-10-05T06:45:00+02:00", "md": "2614", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to place pump balance cement plug", "dTimEnd": "2016-10-05T07:15:00+02:00", "dTimStart": "2016-10-05T07:00:00+02:00", "md": "2614", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pumped 20m3 wash pill with mud pumps, 2700l/min - 79bar. Applied 20 bar behind IBOP, verified line up", "dTimEnd": "2016-10-05T08:00:00+02:00", "dTimStart": "2016-10-05T07:15:00+02:00", "md": "2614", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Balanced cement plug (2616 m - 2416 m ): Mixed and pumped 9,4 m3 of 1,9 SG cement slurry, 600 l/min. Displaced the cement to the rig floor with 2900 l of drill water. Zeroed volume counters. Displaced the cement with 37 m3 (1670 strokes) of SW, 2900 l/min/ 51 bar. Pulled out of cement to 2416m at 4 min/stand. Theoretical TOC 2416 m MD.", "dTimEnd": "2016-10-05T09:30:00+02:00", "dTimStart": "2016-10-05T08:00:00+02:00", "md": "2416", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed sponge ball. Pumped 10m3 hi-vis at 2400l/min / 43 bar. Circulated out cement at max of 3400 l/min/ 116 bar. Diverted returns overboard. L/D pup joint and R/B 1x stand to 2372m. Meanwhile WOC", "dTimEnd": "2016-10-05T10:15:00+02:00", "dTimStart": "2016-10-05T09:30:00+02:00", "md": "2372", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to wash BOP w/ jetting tool. Meanwhile WOC", "dTimEnd": "2016-10-05T10:30:00+02:00", "dTimStart": "2016-10-05T10:15:00+02:00", "md": "2372", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed closed FOSV and BOP wash tool, made 10x passes in BOP and well head area at 1500 LPM / 12 bar, operated rams and annular once. L/D BOP wash tool. Meanwhile WOC", "dTimEnd": "2016-10-05T12:00:00+02:00", "dTimStart": "2016-10-05T10:30:00+02:00", "md": "2372", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to L/D DP. Meanwhile WOC", "dTimEnd": "2016-10-05T12:15:00+02:00", "dTimStart": "2016-10-05T12:00:00+02:00", "md": "2372", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed pipe deck rollers. POOH and L/D singles of 5,5in DP from 2372m to 2052m. Meanwhile WOC", "dTimEnd": "2016-10-05T14:15:00+02:00", "dTimStart": "2016-10-05T12:15:00+02:00", "md": "2052", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed DP slips and installed master bushing. Meanwhile WOC", "dTimEnd": "2016-10-05T14:30:00+02:00", "dTimStart": "2016-10-05T14:15:00+02:00", "md": "2052", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to R/U casing tong. Meanwhile WOC", "dTimEnd": "2016-10-05T14:45:00+02:00", "dTimStart": "2016-10-05T14:30:00+02:00", "md": "2052", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/U casing tong and broke off swedge from top of tubing string. Meanwhile WOC", "dTimEnd": "2016-10-05T15:15:00+02:00", "dTimStart": "2016-10-05T14:45:00+02:00", "md": "2049", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/D casing tong. Meanwhile WOC", "dTimEnd": "2016-10-05T15:45:00+02:00", "dTimStart": "2016-10-05T15:15:00+02:00", "md": "2049", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "P/U spear BHA, set in catch position and engaged into tubing string, RIH to 2084m. Meanwhile WOC", "dTimEnd": "2016-10-05T16:00:00+02:00", "dTimStart": "2016-10-05T15:45:00+02:00", "md": "2084", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH w/ 5,5in DP from 2084m to 2365m. Average tripping speed 612 m/hour. Performed kick drill. Meanwhile WOC", "dTimEnd": "2016-10-05T17:00:00+02:00", "dTimStart": "2016-10-05T16:00:00+02:00", "md": "2365", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed maintenance on TDS. Cleared chiksans from wellhead. Worked on PMs on drilling equipment. Tested back up BX elevators, good test. Meanwhile WOC", "dTimEnd": "2016-10-05T19:00:00+02:00", "dTimStart": "2016-10-05T17:00:00+02:00", "md": "2365", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cleaned in moonpool. Worked to service both PRSs and TDS. Installed drill pipe slips. Meanwhile WOC", "dTimEnd": "2016-10-06T00:00:00+02:00", "dTimStart": "2016-10-05T19:00:00+02:00", "md": "2365", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2016_10_07
NO 15/9-F-4
NO 15/9-F-4
name
2016-10-06T00:00:00+02:00
2016-10-07T00:00:00+02:00
normal
2018-05-03T13:52:57+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2016-10-07T00:00:00+02:00", "dTimDiaHoleStart": "2016-10-01T15:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "- Perforate below 10 3/4in subsea casing hanger\n- Cut 10 3/4in casing\n- Mill 10 3/4in subsea csing hanger\n- Pull and L/D 10 3/4in casing", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3500", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "2755", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "6", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "- Tagged cement w/ tubing\n- Released spear from tubing, \n- POOH w/ spear and L/D 5.5in DP\n- Retrieved MS-T seal\n- Cut 10 3/4in surface tieback\n- Pulled and L/D 10 3/4in surface tieback casing\n- Released tieback adapter\n- L/D 5,5in LH DP\n", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[ { "dTim": "2016-10-06T01:15:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "water based", "presBopRating": "345", "pv": "-999.99", "tempHthp": null, "type": "Seawater", "visFunnel": "-999.99", "yp": "-999.99" } ]
[]
[]
[ { "comments": "Initiated circulation and RIH to tag cement. Down weight 129t. Slowly washed down from theoretical TOC of 2416m to 2426m. 500l/min - 11bar. No indication of cement, stable pressure. Continued RIH. Observed increase in pressure to 13-14bar and no change of weight indicating poor cement. Stopped RIH at 2436m, 20m below theoretical TOC. Picked up string 10m and circulated well over shackers at max 2000l/min - 100bar. Shackers plugged with cement returns. Diverted returns overboard. Continued circulated until no cement observed in returns. Totally circulated 108m3. Meanwhile WOC", "dTimEnd": "2016-10-06T02:00:00+02:00", "dTimStart": "2016-10-06T00:00:00+02:00", "md": "2436", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited for cement, total of 2 hours from 1st tagging attempt", "dTimEnd": "2016-10-06T02:30:00+02:00", "dTimStart": "2016-10-06T02:00:00+02:00", "md": "2405", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Initiated circulation and RIH to tag cement. Down weight 126t. Slowly washed down from 2436m, 500l/min - 10bar, pressure dropped to 8 bar after reaching 2438m. Tagged TOC w/ 10t. Confirmed TOC at 2438m (22m below theoretical TOC)", "dTimEnd": "2016-10-06T02:45:00+02:00", "dTimStart": "2016-10-06T02:30:00+02:00", "md": "2438", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Released spear from tubing string. Pulled string 2m up, confirmed spear released, up weight of 82t. Top of tubing 389m", "dTimEnd": "2016-10-06T03:00:00+02:00", "dTimStart": "2016-10-06T02:45:00+02:00", "md": "2438", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to L/D 5.5in DP. Meanwhile performed flowcheck. Stable", "dTimEnd": "2016-10-06T03:15:00+02:00", "dTimStart": "2016-10-06T03:00:00+02:00", "md": "389", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH w/ spear and L/D 5.5in DP", "dTimEnd": "2016-10-06T05:15:00+02:00", "dTimStart": "2016-10-06T03:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to L/D spear BHA", "dTimEnd": "2016-10-06T05:30:00+02:00", "dTimStart": "2016-10-06T05:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed DP slips, installed master bushing", "dTimEnd": "2016-10-06T05:45:00+02:00", "dTimStart": "2016-10-06T05:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/D spear BHA", "dTimEnd": "2016-10-06T06:15:00+02:00", "dTimStart": "2016-10-06T05:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed power rollers. Cleaned and cleared rig floor", "dTimEnd": "2016-10-06T06:45:00+02:00", "dTimStart": "2016-10-06T06:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "P/U wash tool. RIH from surface to 20.5 m. Jetted wellhead w/ 2200 l/min, 10 rpm, moved string 1m up/down. POOH, L/D jetting tool", "dTimEnd": "2016-10-06T07:45:00+02:00", "dTimStart": "2016-10-06T06:45:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to P/U MS-T seal retrieval tool", "dTimEnd": "2016-10-06T08:00:00+02:00", "dTimStart": "2016-10-06T07:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "P/U and M/U MS-T seal retrieval tool and tested same RIH to 20.5m and engaged MS-T seal retrieval tool. Pulled seal free with 80t overpull POOH from 20,5m and L/D MS-T seal and retrieval tool", "dTimEnd": "2016-10-06T10:00:00+02:00", "dTimStart": "2016-10-06T08:00:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to P/U cutter BHA", "dTimEnd": "2016-10-06T10:15:00+02:00", "dTimStart": "2016-10-06T10:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- cut", "state": "ok", "stateDetailActivity": "success" }, { "comments": "P/U and RIH cutter BHA to 9,5m", "dTimEnd": "2016-10-06T10:30:00+02:00", "dTimStart": "2016-10-06T10:15:00+02:00", "md": "10", "phase": "fixed", "proprietaryCode": "plug abandon -- cut", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH w/ cutter BHA, positioned knives at 123m", "dTimEnd": "2016-10-06T11:00:00+02:00", "dTimStart": "2016-10-06T10:30:00+02:00", "md": "123", "phase": "fixed", "proprietaryCode": "plug abandon -- cut", "state": "ok", "stateDetailActivity": "success" }, { "comments": "M/U TDS, took parameters. Cut 10 3/4in surface casing tieback at 123m, 400 l/min - 50bar, 80 rpm, 2-10 kNm. Observed good indications of cut: pressure drop and reduction of torque", "dTimEnd": "2016-10-06T11:30:00+02:00", "dTimStart": "2016-10-06T11:00:00+02:00", "md": "123", "phase": "fixed", "proprietaryCode": "plug abandon -- cut", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Flowchecked for 5min, stable. POOH to 9,5m", "dTimEnd": "2016-10-06T11:45:00+02:00", "dTimStart": "2016-10-06T11:30:00+02:00", "md": "10", "phase": "fixed", "proprietaryCode": "plug abandon -- cut", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/D cutter BHA", "dTimEnd": "2016-10-06T12:00:00+02:00", "dTimStart": "2016-10-06T11:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- cut", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to R/U casing tong", "dTimEnd": "2016-10-06T12:15:00+02:00", "dTimStart": "2016-10-06T12:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- equipment recovery", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/U casing tong on the rig floor", "dTimEnd": "2016-10-06T13:15:00+02:00", "dTimStart": "2016-10-06T12:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- equipment recovery", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH w/ spear and engage in 10 3/4in surface casing hanger, pulled casing to surface", "dTimEnd": "2016-10-06T13:30:00+02:00", "dTimStart": "2016-10-06T13:15:00+02:00", "md": "103", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to pull and L/D 10 3/4in casing", "dTimEnd": "2016-10-06T13:45:00+02:00", "dTimStart": "2016-10-06T13:30:00+02:00", "md": "103", "phase": "fixed", "proprietaryCode": "plug abandon -- equipment recovery", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke out pup joint and casing hanger, L/D same", "dTimEnd": "2016-10-06T14:00:00+02:00", "dTimStart": "2016-10-06T13:45:00+02:00", "md": "98", "phase": "fixed", "proprietaryCode": "plug abandon -- equipment recovery", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Changed BX Elevators to BX-4s and PDM head", "dTimEnd": "2016-10-06T14:30:00+02:00", "dTimStart": "2016-10-06T14:00:00+02:00", "md": "98", "phase": "fixed", "proprietaryCode": "plug abandon -- equipment recovery", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH and L/D 10 3/4in caing tieback from 103m to surface", "dTimEnd": "2016-10-06T16:15:00+02:00", "dTimStart": "2016-10-06T14:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- equipment recovery", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/D casing tong and changed BX elevators", "dTimEnd": "2016-10-06T17:00:00+02:00", "dTimStart": "2016-10-06T16:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- equipment recovery", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to change saver sub to left hand one", "dTimEnd": "2016-10-06T17:15:00+02:00", "dTimStart": "2016-10-06T17:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Placed 3m pup in rotary. Screwed in TDS and broke off saver sub. L/D pup with saver sub on top. RIH 1x stand with left hand DP. M/U left hand saver sub to stand, screwed in TDS and M/U to saver sub", "dTimEnd": "2016-10-06T18:30:00+02:00", "dTimStart": "2016-10-06T17:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/B stand and P/U torque tool", "dTimEnd": "2016-10-06T18:45:00+02:00", "dTimStart": "2016-10-06T18:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH w/ torque tool on LH drill pipe to 140m", "dTimEnd": "2016-10-06T19:15:00+02:00", "dTimStart": "2016-10-06T18:45:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Washed profile area 1500l/min - 9bar. Released tieback adapter w/ 38kNm", "dTimEnd": "2016-10-06T19:30:00+02:00", "dTimStart": "2016-10-06T19:15:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to change handling gear, L/D 5,5in LH DP", "dTimEnd": "2016-10-06T19:45:00+02:00", "dTimStart": "2016-10-06T19:30:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed master bushing, installed DP slips. Changed PDM head", "dTimEnd": "2016-10-06T20:45:00+02:00", "dTimStart": "2016-10-06T19:45:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/B 1x stand of LH DP, L/D 16x joints of LH DP", "dTimEnd": "2016-10-06T21:45:00+02:00", "dTimStart": "2016-10-06T20:45:00+02:00", "md": "7", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/D torque tool", "dTimEnd": "2016-10-06T22:15:00+02:00", "dTimStart": "2016-10-06T21:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/D 4x singles of LH DP from the stand previously R/B", "dTimEnd": "2016-10-06T22:30:00+02:00", "dTimStart": "2016-10-06T22:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed DP slips, installed master bushing", "dTimEnd": "2016-10-06T22:45:00+02:00", "dTimStart": "2016-10-06T22:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to change saver sub back to right hand one", "dTimEnd": "2016-10-06T23:00:00+02:00", "dTimStart": "2016-10-06T22:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Worked to change saver sub back to right hand one", "dTimEnd": "2016-10-07T00:00:00+02:00", "dTimStart": "2016-10-06T23:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2016_10_08
NO 15/9-F-4
NO 15/9-F-4
name
2016-10-07T00:00:00+02:00
2016-10-08T00:00:00+02:00
normal
2018-05-03T13:52:58+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2016-10-08T00:00:00+02:00", "dTimDiaHoleStart": "2016-10-01T15:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "- Pull 10 3/4\" casing\n- Install 13 3/8\" EZSV plug at 303 mMD\n- Place OH to surface cement plug in 13 3/8\" casing\n- N/D BOP", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3500", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "2755", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "7", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "- Retrieved tie-back adapter\n- Perforated 10 3/4\" casing below casing hanger\n- Cut 10 3/4\" casing at 312 mMD\n- Milled ID in 10 3/4\" CH to 12 1/4\"", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Worked to change saver sub back to the right hand one", "dTimEnd": "2016-10-07T00:15:00+02:00", "dTimStart": "2016-10-07T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed Pre-job Meeting to P/U spear BHA", "dTimEnd": "2016-10-07T00:30:00+02:00", "dTimStart": "2016-10-07T00:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH w/ ITCO spear BHA", "dTimEnd": "2016-10-07T01:15:00+02:00", "dTimStart": "2016-10-07T00:30:00+02:00", "md": "128", "phase": "fixed", "proprietaryCode": "plug abandon -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Engaged spear in tieback adapter fish, pulled w/ 6t overpull. POOH w/ fish to surface", "dTimEnd": "2016-10-07T02:00:00+02:00", "dTimStart": "2016-10-07T01:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/B spear BHA, L/D tieback adapter stump", "dTimEnd": "2016-10-07T02:45:00+02:00", "dTimStart": "2016-10-07T02:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT to P/U perforation guns", "dTimEnd": "2016-10-07T03:00:00+02:00", "dTimStart": "2016-10-07T02:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- perforate", "state": "ok", "stateDetailActivity": "success" }, { "comments": "M/U and RIH w/ perforation BHA to 148m bottom shot depth", "dTimEnd": "2016-10-07T05:30:00+02:00", "dTimStart": "2016-10-07T03:00:00+02:00", "md": "148", "phase": "fixed", "proprietaryCode": "plug abandon -- perforate", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Closed UPR, opened choke. Confirmed line up. Filled string. Opened UPR, Broke off TDS and dropped 1 3/8 ball in string. M/U TDS. Closed UPR and opened choke. Fired guns with 160 l/min - 130 bar. Top shot at 145m, bottom shot at 148m. Continued to circulate w/ 160l/min", "dTimEnd": "2016-10-07T06:15:00+02:00", "dTimStart": "2016-10-07T05:30:00+02:00", "md": "148", "phase": "fixed", "proprietaryCode": "plug abandon -- perforate", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Circulated 1000 lpm / 5 bar. Maximum gas reading 0,41 %.", "dTimEnd": "2016-10-07T07:00:00+02:00", "dTimStart": "2016-10-07T06:15:00+02:00", "md": "148", "phase": "fixed", "proprietaryCode": "plug abandon -- perforate", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Stopped pumps and closed choke. Monitored well.\nUnable to circulate on TT due to contaminated OBM mixed with water.\nEmptied both TTs and re-filled TTs with clean SW.", "dTimEnd": "2016-10-07T07:30:00+02:00", "dTimStart": "2016-10-07T07:00:00+02:00", "md": "148", "phase": "fixed", "proprietaryCode": "plug abandon -- perforate", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Opened UPR and choke\nFlowchecked well for 10 min, static.", "dTimEnd": "2016-10-07T07:45:00+02:00", "dTimStart": "2016-10-07T07:30:00+02:00", "md": "148", "phase": "fixed", "proprietaryCode": "plug abandon -- perforate", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH w/ perforation BHA from 148 m to 14 m.", "dTimEnd": "2016-10-07T08:15:00+02:00", "dTimStart": "2016-10-07T07:45:00+02:00", "md": "14", "phase": "fixed", "proprietaryCode": "plug abandon -- perforate", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Changed to 4 1/2\" inserts in BX-elevator.", "dTimEnd": "2016-10-07T08:30:00+02:00", "dTimStart": "2016-10-07T08:15:00+02:00", "md": "14", "phase": "fixed", "proprietaryCode": "plug abandon -- perforate", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/D perforation BHA.", "dTimEnd": "2016-10-07T09:00:00+02:00", "dTimStart": "2016-10-07T08:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- perforate", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT for cutting 10 3/4\" casing", "dTimEnd": "2016-10-07T09:15:00+02:00", "dTimStart": "2016-10-07T09:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- cut", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed master bushing. Installed PS-21 slips.", "dTimEnd": "2016-10-07T09:30:00+02:00", "dTimStart": "2016-10-07T09:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- cut", "state": "ok", "stateDetailActivity": "success" }, { "comments": "P/U and M/U 10 3/4\" cutter BHA.", "dTimEnd": "2016-10-07T09:45:00+02:00", "dTimStart": "2016-10-07T09:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- cut", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH w/ 10 3/4\" cutter BHA on 5 1/2\" DP from surface to 312 m.", "dTimEnd": "2016-10-07T10:15:00+02:00", "dTimStart": "2016-10-07T09:45:00+02:00", "md": "312", "phase": "fixed", "proprietaryCode": "plug abandon -- cut", "state": "ok", "stateDetailActivity": "success" }, { "comments": "M/U TDS. Recorded up/down weight 76 / 71 ton.\nFilled DP. Initiated circulation 500 lpm / 73 bar, 50 rpm / 0 to 3 kNm.", "dTimEnd": "2016-10-07T10:30:00+02:00", "dTimStart": "2016-10-07T10:15:00+02:00", "md": "312", "phase": "fixed", "proprietaryCode": "plug abandon -- cut", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cut 10 3/4\" casing at 312 m, 400 lpm, 50 rpm.\nSPP dropped, good indication of cut.", "dTimEnd": "2016-10-07T10:45:00+02:00", "dTimStart": "2016-10-07T10:30:00+02:00", "md": "312", "phase": "fixed", "proprietaryCode": "plug abandon -- cut", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up to TT and performed flowcheck, well static.", "dTimEnd": "2016-10-07T11:00:00+02:00", "dTimStart": "2016-10-07T10:45:00+02:00", "md": "312", "phase": "fixed", "proprietaryCode": "plug abandon -- cut", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH w/ 10 3/4\" cutter BHA on 5 1/2\" DP from 312 m to 9,5 m.", "dTimEnd": "2016-10-07T11:30:00+02:00", "dTimStart": "2016-10-07T11:00:00+02:00", "md": "9.5", "phase": "fixed", "proprietaryCode": "plug abandon -- cut", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/D cutter BHA.", "dTimEnd": "2016-10-07T11:45:00+02:00", "dTimStart": "2016-10-07T11:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- cut", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cleaned and cleared drill floor.", "dTimEnd": "2016-10-07T12:00:00+02:00", "dTimStart": "2016-10-07T11:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- cut", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT for drops inspection prior to milling 10 3/4\" casing hanger.", "dTimEnd": "2016-10-07T12:15:00+02:00", "dTimStart": "2016-10-07T12:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- mill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed drops inspection of TDS, and both PRSs.", "dTimEnd": "2016-10-07T13:00:00+02:00", "dTimStart": "2016-10-07T12:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- mill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "M/U CH milling BHA", "dTimEnd": "2016-10-07T15:15:00+02:00", "dTimStart": "2016-10-07T13:00:00+02:00", "md": "72", "phase": "fixed", "proprietaryCode": "plug abandon -- mill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH w/ CH milling BHA on 5 1/2\" DP from 72 m to 110 m.\nM/U TDS and continued RIH, tagged top of 10 3/4\" CH at 139,9m. Pulled up and filled string.", "dTimEnd": "2016-10-07T15:45:00+02:00", "dTimStart": "2016-10-07T15:15:00+02:00", "md": "139.9", "phase": "fixed", "proprietaryCode": "plug abandon -- mill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Milled ID in 10 3/4\" CH to 12 1/4\". 100 rpm / 9-18 kNm, 2000 lpm / 10,8 bar, 4-5 ton WOB.\nIncreased WOB to 8 - 10 ton after milling first 20 cm.", "dTimEnd": "2016-10-07T19:00:00+02:00", "dTimStart": "2016-10-07T15:45:00+02:00", "md": "140.1", "phase": "fixed", "proprietaryCode": "plug abandon -- mill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued milling 10 3/4\" CH, 100 rpm / 10 - 16 kNm, 2000 lpm / 11 bar, WOB 8 - 10 ton.\nStalled out several times", "dTimEnd": "2016-10-07T21:15:00+02:00", "dTimStart": "2016-10-07T19:00:00+02:00", "md": "141", "phase": "fixed", "proprietaryCode": "plug abandon -- mill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Tagged top of 10 3/4\" casing 1 m below 10 3/4\" CH.\nDressed off approximately 5 cm of top of 10 3/4\" casing, 120 rpm / 5 - 10 kNm, 2000 lpm / 10 bar.", "dTimEnd": "2016-10-07T21:30:00+02:00", "dTimStart": "2016-10-07T21:15:00+02:00", "md": "142", "phase": "fixed", "proprietaryCode": "plug abandon -- mill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Circulated 2 x B/U w/ 3000 lpm / 22 bar.\nR/B 1 stand 5 1/2\" DP.", "dTimEnd": "2016-10-07T22:00:00+02:00", "dTimStart": "2016-10-07T21:30:00+02:00", "md": "110", "phase": "fixed", "proprietaryCode": "plug abandon -- mill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed drops inspection of TDS.\nMeanwhile: Flowchecked well, static. Performed TBT for L/O milling BHA.", "dTimEnd": "2016-10-07T22:30:00+02:00", "dTimStart": "2016-10-07T22:00:00+02:00", "md": "110", "phase": "fixed", "proprietaryCode": "plug abandon -- mill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH w/ CH milling BHA on 5 1/2\" DP from 110 m to 72 m.", "dTimEnd": "2016-10-07T23:00:00+02:00", "dTimStart": "2016-10-07T22:30:00+02:00", "md": "72", "phase": "fixed", "proprietaryCode": "plug abandon -- mill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/B 8 1/4\" DC.\nB/O and L/O CH milling BHA.", "dTimEnd": "2016-10-08T00:00:00+02:00", "dTimStart": "2016-10-07T23:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2016_10_09
NO 15/9-F-4
NO 15/9-F-4
name
2016-10-08T00:00:00+02:00
2016-10-09T00:00:00+02:00
normal
2018-05-03T13:52:58+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2016-10-09T00:00:00+02:00", "dTimDiaHoleStart": "2016-10-01T15:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "- Continue L/O over-torqued 5 1/2\" DP\n- N/D BOP\n- Skid rig", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3500", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "2755", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "8", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "- Pulled 10 3/4\" casing\n- Installed 13 3/8\" EZSV plug at 306 m\n- Placed OH to surface cement plug from 305 m to 205 m\n- L/D 10 3/4\" spear BHA, 8 1/4\" DC, 6 3/4\" DC and over-torqued 5 1/2\" DP", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Cleaned and cleared drill floor", "dTimEnd": "2016-10-08T00:30:00+02:00", "dTimStart": "2016-10-08T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- mill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT for RIH with spear and retrieve 10 3/4\" casing", "dTimEnd": "2016-10-08T00:45:00+02:00", "dTimStart": "2016-10-08T00:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- equipment recovery", "state": "ok", "stateDetailActivity": "success" }, { "comments": "M/U spear BHA", "dTimEnd": "2016-10-08T01:00:00+02:00", "dTimStart": "2016-10-08T00:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- equipment recovery", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH w/ 10 3/4\" spear in catch mode on 5 1/2\" DP from surface to 147 m", "dTimEnd": "2016-10-08T01:30:00+02:00", "dTimStart": "2016-10-08T01:00:00+02:00", "md": "147", "phase": "fixed", "proprietaryCode": "plug abandon -- equipment recovery", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with 10 3/4\" casing on 5 1/2\" landing string from 147 m to surface.", "dTimEnd": "2016-10-08T02:30:00+02:00", "dTimStart": "2016-10-08T01:30:00+02:00", "md": "170", "phase": "fixed", "proprietaryCode": "plug abandon -- equipment recovery", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Released spear at surface and R/B spear BHA", "dTimEnd": "2016-10-08T02:45:00+02:00", "dTimStart": "2016-10-08T02:30:00+02:00", "md": "170", "phase": "fixed", "proprietaryCode": "plug abandon -- equipment recovery", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT for R/U casing handling equipment and pulling casing.", "dTimEnd": "2016-10-08T03:00:00+02:00", "dTimStart": "2016-10-08T02:45:00+02:00", "md": "170", "phase": "fixed", "proprietaryCode": "plug abandon -- equipment recovery", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/D casing pup joint.\nContinued POOH with 10 3/4\" casing from 170 m to surface. Average 10 joints/hr.", "dTimEnd": "2016-10-08T06:00:00+02:00", "dTimStart": "2016-10-08T03:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- equipment recovery", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/D handling equipment.", "dTimEnd": "2016-10-08T08:15:00+02:00", "dTimStart": "2016-10-08T06:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- equipment recovery", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT for running 13 3/8\" EZSV plug", "dTimEnd": "2016-10-08T08:30:00+02:00", "dTimStart": "2016-10-08T08:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "P/U and M/U EZSV plug and RT. Installed centralizer on RT.\nL/D double 5 1/2\" DP. P/U and M/U 3 pup joints for space out", "dTimEnd": "2016-10-08T09:15:00+02:00", "dTimStart": "2016-10-08T08:30:00+02:00", "md": "24", "phase": "fixed", "proprietaryCode": "plug abandon -- mechanical plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH w/ 13 3/8\" EZSV plug from 24 m to 306 m.", "dTimEnd": "2016-10-08T10:30:00+02:00", "dTimStart": "2016-10-08T09:15:00+02:00", "md": "306", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "P/U and M/U pump-in sub.", "dTimEnd": "2016-10-08T10:45:00+02:00", "dTimStart": "2016-10-08T10:30:00+02:00", "md": "306", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "M/U TDS and washed setting area with 560 lpm / 6 bar.\nSet 13 3/8\" EZSV plug at 306m. Tagged EZSV plug with 10 ton.", "dTimEnd": "2016-10-08T11:15:00+02:00", "dTimStart": "2016-10-08T10:45:00+02:00", "md": "306", "phase": "fixed", "proprietaryCode": "plug abandon -- mechanical plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pumped 10 m3 wash pill followed by 10 m3 hi-vis pill at 2000 lpm / 9 bar.\nCirculated with clean SW until clean returns. Reduced to 900 lpm when hi-vis at shakers. Increased flow to 2440 lpm when clean SW in returns.\nMeanwhile: Flushed TTs.", "dTimEnd": "2016-10-08T12:30:00+02:00", "dTimStart": "2016-10-08T11:15:00+02:00", "md": "305", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT for cement job", "dTimEnd": "2016-10-08T12:45:00+02:00", "dTimStart": "2016-10-08T12:30:00+02:00", "md": "305", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Closed flow line and opened dump line. R/U cement hose to pump-in sub.\nApplied 20 bar behind FOSV and confirmed line-up. Leak tested surface lines to 100 bar / 3min.\n\nBalanced OH to surface cement plug in 13 3/8\" casing (305 m - 205 m ): Pumped 10 m3 DW at 1000 lpm with cement unit. Mixed and pumped 7,8 m3 1,95sg cement slurry at 600 lpm. Displaced cement with 2 m3 DW at 1000 lpm with cement unit.", "dTimEnd": "2016-10-08T13:45:00+02:00", "dTimStart": "2016-10-08T12:45:00+02:00", "md": "305", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/D cement hose. B/O and L/O pump-in sub.", "dTimEnd": "2016-10-08T14:00:00+02:00", "dTimStart": "2016-10-08T13:45:00+02:00", "md": "305", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH w/ EZSV RT on 5 1/2\" DP from 305 m to 160 m.", "dTimEnd": "2016-10-08T14:30:00+02:00", "dTimStart": "2016-10-08T14:00:00+02:00", "md": "160", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed 2x sponge balls. Circulated BU, 2000 lpm.", "dTimEnd": "2016-10-08T15:00:00+02:00", "dTimStart": "2016-10-08T14:30:00+02:00", "md": "160", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH w/ EZSV RT on 5 1/2\" DP from 160 m to 80 m.\nM/U BOP jetting tool and FOSV.", "dTimEnd": "2016-10-08T15:30:00+02:00", "dTimStart": "2016-10-08T15:00:00+02:00", "md": "80", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Jetted BOP 8 x passes up/down, 1450 lpm, 50 rpm. Operated annular preventer and pipe rams.\nB/O and L/O BOP jetting tool and FOSV.", "dTimEnd": "2016-10-08T17:00:00+02:00", "dTimStart": "2016-10-08T15:30:00+02:00", "md": "80", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed PS-21 slips and installed master bushing.", "dTimEnd": "2016-10-08T17:15:00+02:00", "dTimStart": "2016-10-08T17:00:00+02:00", "md": "80", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH and L/D the EZSV RT.", "dTimEnd": "2016-10-08T17:30:00+02:00", "dTimStart": "2016-10-08T17:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- cement plug", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 3 std 8 1/4\" DC. L/O 2 x singles to cantilever.", "dTimEnd": "2016-10-08T19:00:00+02:00", "dTimStart": "2016-10-08T17:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT with ongoing crew. Performed manual tong training.\nL/O 7 joints 8 1/4\" DC.", "dTimEnd": "2016-10-08T21:15:00+02:00", "dTimStart": "2016-10-08T19:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/O 10 3/4\" spear BHA", "dTimEnd": "2016-10-08T22:00:00+02:00", "dTimStart": "2016-10-08T21:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/O 3 joints 6 3/4\" DC", "dTimEnd": "2016-10-08T23:15:00+02:00", "dTimStart": "2016-10-08T22:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/O 5 joints over-torqued 5 1/2\" DP", "dTimEnd": "2016-10-09T00:00:00+02:00", "dTimStart": "2016-10-08T23:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2016_10_10
NO 15/9-F-4
NO 15/9-F-4
name
2016-10-09T00:00:00+02:00
2016-10-10T00:00:00+02:00
normal
2018-05-03T13:52:58+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2016-10-10T00:00:00+02:00", "dTimDiaHoleStart": "2016-10-01T15:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "None", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3500", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "2755", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "9", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "- L/O over-torqued 5 1/2\" DP\n- N/D BOP", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "L/O 13 joints 5 1/2\" over-torqued DP", "dTimEnd": "2016-10-09T01:15:00+02:00", "dTimStart": "2016-10-09T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/O 4 joints over-torqued 5 1/2\" HWDP. Used manual tongs to break one of the connections.", "dTimEnd": "2016-10-09T03:00:00+02:00", "dTimStart": "2016-10-09T01:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cleaned and cleared drill floor.\nChanged handling equipment for pulling diverter.", "dTimEnd": "2016-10-09T03:15:00+02:00", "dTimStart": "2016-10-09T03:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT for N/D BOP", "dTimEnd": "2016-10-09T03:30:00+02:00", "dTimStart": "2016-10-09T03:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "N/D diverter and pulled slickjoint.", "dTimEnd": "2016-10-09T04:15:00+02:00", "dTimStart": "2016-10-09T03:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Load shifted weight from tension system to BOP carrier.", "dTimEnd": "2016-10-09T04:45:00+02:00", "dTimStart": "2016-10-09T04:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Disconnected BOP tension system.\nMeanwhile: Disconnected BOP NT2 connector", "dTimEnd": "2016-10-09T05:30:00+02:00", "dTimStart": "2016-10-09T04:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Skidded BOP over to test stump", "dTimEnd": "2016-10-09T05:45:00+02:00", "dTimStart": "2016-10-09T05:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed scaffolding around HP-riser.\nMeanwhile: Performed TBT for pulling HP-riser", "dTimEnd": "2016-10-09T06:15:00+02:00", "dTimStart": "2016-10-09T05:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled HP-riser to drill floor.\nInstalled master bushing.", "dTimEnd": "2016-10-09T07:00:00+02:00", "dTimStart": "2016-10-09T06:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT for L/O HP-riser to HTS and installing hatches in moonpool", "dTimEnd": "2016-10-09T07:15:00+02:00", "dTimStart": "2016-10-09T07:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/O HP-riser to HTS", "dTimEnd": "2016-10-09T07:30:00+02:00", "dTimStart": "2016-10-09T07:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed hatches in moonpool.\nMeanwhile: Cleaned and preserved slickjoint\n\n******** END OF REPORT - CONTINUED REPORTING ON F-99 *********", "dTimEnd": "2016-10-09T09:00:00+02:00", "dTimStart": "2016-10-09T07:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2016_10_11
NO 15/9-F-4
NO 15/9-F-4
name
2016-10-10T00:00:00+02:00
2016-10-11T00:00:00+02:00
normal
2018-05-03T13:52:58+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2016-10-11T00:00:00+02:00", "dTimDiaHoleStart": "2016-10-01T15:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "- RIH with PR cutter BHA and multibowl pulling tool\n- Removed tension cylinders\n- Wait on supply boat with remaining equipment for pulling production riser\n- Pull production riser", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3500", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "2755", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "10", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "- Waited on equipment to pull production riser\n- L/D 5 1/2\" DP from set-back\n- Secured BOP on test stump\n- Removed hoses and cables from WH\n- Removed hatches", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Waited on supply boat with equipment for pulling production riser\n\nMeanwhile:\nL/O 3 1/2\" DP from set-back.\nMeanwhile: Performed PMs.", "dTimEnd": "2016-10-10T13:15:00+02:00", "dTimStart": "2016-10-10T10:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited on supply boat with equipment for pulling production riser\n\nMeanwhile:\nCanged handling equipment to handle 5 1/2\" DP.\nL/O 5 1/2\" DP from set-back.", "dTimEnd": "2016-10-10T15:00:00+02:00", "dTimStart": "2016-10-10T13:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued L/O 5 1/2\" DP from set-back.\nMeanwhile:\nRemoved remaining hoses and electrical cables from WH", "dTimEnd": "2016-10-10T19:00:00+02:00", "dTimStart": "2016-10-10T15:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT for L/D diverter", "dTimEnd": "2016-10-10T19:15:00+02:00", "dTimStart": "2016-10-10T19:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/U and attached lifting equipment to TDS and diverter.\nL/O diverter and secured same on main deck.\nRemoved diverter lifting equipment from TDS.\nMeanwhile: Performed TBT for building scaffolding around BOP connector on test stump.", "dTimEnd": "2016-10-10T20:45:00+02:00", "dTimStart": "2016-10-10T19:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Prepared 1502 hoses/chiksan at WH\nBuilt scaffolding around BOP.", "dTimEnd": "2016-10-10T21:30:00+02:00", "dTimStart": "2016-10-10T20:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "N/U BOP NT2 connector on test stump.\nPrepared lifting equipment on moonpool hatch.\nLifted multibowl NT2 connector to drill floor.\nLifted PR cutter BHA to HTS", "dTimEnd": "2016-10-10T22:15:00+02:00", "dTimStart": "2016-10-10T21:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued N/U BOP NT2 connector on test stump", "dTimEnd": "2016-10-10T23:00:00+02:00", "dTimStart": "2016-10-10T22:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed hatch in moonpool.", "dTimEnd": "2016-10-11T00:00:00+02:00", "dTimStart": "2016-10-10T23:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2016_10_12
NO 15/9-F-4
NO 15/9-F-4
name
2016-10-11T00:00:00+02:00
2016-10-12T00:00:00+02:00
normal
2018-05-03T13:52:58+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2016-10-12T00:00:00+02:00", "dTimDiaHoleStart": "2016-10-01T15:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "- Cut production riser at 134,9 m\n- Remove hoses and valves from multibowl\n- Pull multibowl to drill floor and rig up false rotary\n- Pull inner string and R/B BHAs\n- M/U multibowl RT and pull, cut and L/O tensioner joint\n- Pull, cut and L/O riser joints\n- R/D riser equipment", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3500", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "2755", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "11", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "- Installed NT2 connector on multibowl.\n- P/U and RIB with cutter and multibowl RT\n- Removed production riser tension cylinders\n- R/D riser centralizers and boat collision stool\n- Cleared cantilever and installed deck beams", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Lowered NT2 connector for multibowl. M/U NT2 connector on multibowl.", "dTimEnd": "2016-10-11T00:45:00+02:00", "dTimStart": "2016-10-11T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed master bushing and removed box ring from rotary.", "dTimEnd": "2016-10-11T01:00:00+02:00", "dTimStart": "2016-10-11T00:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT for handling PR cutter BHA", "dTimEnd": "2016-10-11T01:15:00+02:00", "dTimStart": "2016-10-11T01:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "P/U and M/U cutter BHA and RIH with same.\nP/U and M/U mutlibowl RT.", "dTimEnd": "2016-10-11T04:15:00+02:00", "dTimStart": "2016-10-11T01:15:00+02:00", "md": "134.9", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH w/ BHA and M/U multibowl RT in WH.\nTook 20 ton OP to verify RT engaged in WH.\nM/U TDS\nPerformed debrief after M/U BHA.", "dTimEnd": "2016-10-11T04:30:00+02:00", "dTimStart": "2016-10-11T04:15:00+02:00", "md": "134.9", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT for R/D tension cylinders on PR", "dTimEnd": "2016-10-11T05:00:00+02:00", "dTimStart": "2016-10-11T04:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Bled off pressure in PR tension cylinders, observed 35 ton increase on weight indicator", "dTimEnd": "2016-10-11T05:30:00+02:00", "dTimStart": "2016-10-11T05:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Prepared WH/tension ring for removal", "dTimEnd": "2016-10-11T07:00:00+02:00", "dTimStart": "2016-10-11T05:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT for removing tension cylinders with ongoing crew", "dTimEnd": "2016-10-11T07:15:00+02:00", "dTimStart": "2016-10-11T07:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued bleeding off tension cylinders.\nR/D tension cylinders, left the cylinders hanging from top mounting point.\nSecured tension cylinders.\nMeanwhile: Assisted crane with backload. Cleaned shaker pits.", "dTimEnd": "2016-10-11T11:30:00+02:00", "dTimStart": "2016-10-11T07:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed information meeting with all involved personnel for riser pulling operations.", "dTimEnd": "2016-10-11T12:00:00+02:00", "dTimStart": "2016-10-11T11:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/D boat collision stool and prepared to remove centralizers from centralizer deck.\nConnected 3 x weco 1502 hoses to WH outlets.\nMeanwhile: Assisted crane with backload. Continued cleaning shaker pits.", "dTimEnd": "2016-10-11T15:30:00+02:00", "dTimStart": "2016-10-11T12:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited on supply boat for riser equipment\n\nMeanwhile:\nPerformed housekeeping on cantilever. Removed pipes and equipment from cantilever to make space for riser joints.\nAssisted crane with backload. Continued cleaning shaker pits.", "dTimEnd": "2016-10-11T19:00:00+02:00", "dTimStart": "2016-10-11T15:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT for R/U riser handling equipment", "dTimEnd": "2016-10-11T19:15:00+02:00", "dTimStart": "2016-10-11T19:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/U tailing arm and saddle on HTS.\nContinued to clear cantilever.\nInstalled beams on cantilever deck for L/O riser joints.", "dTimEnd": "2016-10-11T20:30:00+02:00", "dTimStart": "2016-10-11T19:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed information meeting with all involved personnel for riser pulling operations.", "dTimEnd": "2016-10-11T21:00:00+02:00", "dTimStart": "2016-10-11T20:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to clear cantilever. Installed deck beams on cantilever.", "dTimEnd": "2016-10-11T23:45:00+02:00", "dTimStart": "2016-10-11T21:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Spotted riser handling equipment.\nMeanwhile: Cleared drill floor.", "dTimEnd": "2016-10-12T00:00:00+02:00", "dTimStart": "2016-10-11T23:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2016_10_13
NO 15/9-F-4
NO 15/9-F-4
name
2016-10-12T00:00:00+02:00
2016-10-13T00:00:00+02:00
normal
2018-05-03T13:52:58+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2016-10-13T00:00:00+02:00", "dTimDiaHoleStart": "2016-10-01T15:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "- Pull lower pup joint and stress joint (lift #7) and L/O same\n- Install hole covers and hatches\n- Skid rig to F-5", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3500", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "2755", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "12", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "- Cut production riser at 134,9 m.\n- Pulled multibowl to drill floor\n- Pulled inner string and R/B BHA\n- Pulled tensioner joint above drill floor and cut riser. L/O tensioner joint and multibowl\n- Pulled, cut and L/O riser joints (6 out of 7 lifts)", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "Continued spotting riser handling equipment.\nMeanwhile: Cleared drill floor.", "dTimEnd": "2016-10-12T01:00:00+02:00", "dTimStart": "2016-10-12T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT for cutting the production riser and pulling the multibowl to drill floor.", "dTimEnd": "2016-10-12T01:15:00+02:00", "dTimStart": "2016-10-12T01:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Took 5 ton overpull.\nStaged up pump rate to 900 lpm, observed water leaking over the top of the multibowl", "dTimEnd": "2016-10-12T01:30:00+02:00", "dTimStart": "2016-10-12T01:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Stopped pumping. Checked scribe line to confirm multibowl running tool still engaged to the multibowl.", "dTimEnd": "2016-10-12T01:45:00+02:00", "dTimStart": "2016-10-12T01:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Staged up pump rate to 2300 lpm / 87 bar. Continued pumping for approximately 15 min, lost overpull, good indication of cut.\nObserved multibowl/riser turned 1/4 turn clockwise at successful cut.", "dTimEnd": "2016-10-12T02:00:00+02:00", "dTimStart": "2016-10-12T01:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "P/U slowly to confirm successful cut.", "dTimEnd": "2016-10-12T02:15:00+02:00", "dTimStart": "2016-10-12T02:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed hoses and valves from multibowl.", "dTimEnd": "2016-10-12T03:00:00+02:00", "dTimStart": "2016-10-12T02:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled riser and multibowl to drill floor.\nRemoved master bushing and installed the big C-plate.", "dTimEnd": "2016-10-12T03:30:00+02:00", "dTimStart": "2016-10-12T03:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Disengaged multibowl RT by rotating elevator.", "dTimEnd": "2016-10-12T03:45:00+02:00", "dTimStart": "2016-10-12T03:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed small C-plate and false rotary.", "dTimEnd": "2016-10-12T04:00:00+02:00", "dTimStart": "2016-10-12T03:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "B/O and attempted to rack back multibowl RT. Unable to rack back due to too long assebly.\nParked AFT PRS with multibowl RT out of the way.", "dTimEnd": "2016-10-12T04:45:00+02:00", "dTimStart": "2016-10-12T04:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled inner string and R/B 2 x 5 1/2\" DP stands.\nR/B cutter BHA", "dTimEnd": "2016-10-12T06:00:00+02:00", "dTimStart": "2016-10-12T04:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "P/U and M/U multibowl RT.\nRemoved C-plate.", "dTimEnd": "2016-10-12T06:15:00+02:00", "dTimStart": "2016-10-12T06:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled up riser until first flange at centralizer deck. Cleaned flange for marine growth.", "dTimEnd": "2016-10-12T07:00:00+02:00", "dTimStart": "2016-10-12T06:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed TBT for pulling and cutting riser", "dTimEnd": "2016-10-12T07:15:00+02:00", "dTimStart": "2016-10-12T07:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled tensioner joint above drill floor. Cleaned flange for marine growth on WH deck.", "dTimEnd": "2016-10-12T07:45:00+02:00", "dTimStart": "2016-10-12T07:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed master bushing and elevator.\nLanded riser on elevator.", "dTimEnd": "2016-10-12T08:00:00+02:00", "dTimStart": "2016-10-12T07:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/U cutting machine.\nInstalled hole cover to collect swarf", "dTimEnd": "2016-10-12T09:00:00+02:00", "dTimStart": "2016-10-12T08:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cut tensioner joint", "dTimEnd": "2016-10-12T09:45:00+02:00", "dTimStart": "2016-10-12T09:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Collected swarf.\nR/D cutting machine.", "dTimEnd": "2016-10-12T10:00:00+02:00", "dTimStart": "2016-10-12T09:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/O tensioner joint", "dTimEnd": "2016-10-12T11:15:00+02:00", "dTimStart": "2016-10-12T10:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed running tool. Changed handling equipment.\nInstalled cradle on HTS\nCleared drill floor.", "dTimEnd": "2016-10-12T12:30:00+02:00", "dTimStart": "2016-10-12T11:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lifted riser. Removed master bushing", "dTimEnd": "2016-10-12T12:45:00+02:00", "dTimStart": "2016-10-12T12:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled riser (lift #2). Cleaned flanges on WH deck", "dTimEnd": "2016-10-12T13:00:00+02:00", "dTimStart": "2016-10-12T12:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed master bushing and elevator.\nRemoved fairing and landed riser onto elevator", "dTimEnd": "2016-10-12T13:15:00+02:00", "dTimStart": "2016-10-12T13:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/U cutting machine and hole cover.\nCut riser", "dTimEnd": "2016-10-12T14:00:00+02:00", "dTimStart": "2016-10-12T13:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Collected swarf.\nR/D cutting machine.", "dTimEnd": "2016-10-12T14:15:00+02:00", "dTimStart": "2016-10-12T14:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/O riser joint (lift #2).", "dTimEnd": "2016-10-12T14:45:00+02:00", "dTimStart": "2016-10-12T14:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled riser (lift #3).", "dTimEnd": "2016-10-12T15:15:00+02:00", "dTimStart": "2016-10-12T14:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed master bushing. Pulled flange through rotary.\nInstalled master bushing and elevator. Landed riser onto elevator.", "dTimEnd": "2016-10-12T15:30:00+02:00", "dTimStart": "2016-10-12T15:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/U cutting maching and cut riser", "dTimEnd": "2016-10-12T16:00:00+02:00", "dTimStart": "2016-10-12T15:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/D cutting maching. Collected swarf", "dTimEnd": "2016-10-12T16:15:00+02:00", "dTimStart": "2016-10-12T16:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/D riser joint (lift #3)", "dTimEnd": "2016-10-12T16:30:00+02:00", "dTimStart": "2016-10-12T16:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled riser joint (lift #4).\nPulled master bushing. Pulled flange through rotary, installed master bushing and elevator.\nLanded riser onto elevator.", "dTimEnd": "2016-10-12T17:00:00+02:00", "dTimStart": "2016-10-12T16:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/U cutting maching and attempted cut riser.\nKnifes worn out and broken.", "dTimEnd": "2016-10-12T17:30:00+02:00", "dTimStart": "2016-10-12T17:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Changed knifes and continued cutting riser.\nExperienced knifes not cutting evenly due to ovality of riser.", "dTimEnd": "2016-10-12T19:00:00+02:00", "dTimStart": "2016-10-12T17:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued cutting riser.\nMeanwhile: Performed TBT with ongoing crew.", "dTimEnd": "2016-10-12T19:15:00+02:00", "dTimStart": "2016-10-12T19:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/D cutting maching.\nCollected swarf", "dTimEnd": "2016-10-12T19:30:00+02:00", "dTimStart": "2016-10-12T19:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/O riser joint (lift #4).", "dTimEnd": "2016-10-12T20:00:00+02:00", "dTimStart": "2016-10-12T19:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled riser (lift #5)\nRemoved master bushing. Pulled flange through rotary, installed master bushing and elevator.\nLanded riser onto elevator.", "dTimEnd": "2016-10-12T20:45:00+02:00", "dTimStart": "2016-10-12T20:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/U cutting manchine and cut riser.\nExperienced knifes not cutting evenly due to ovality of riser.", "dTimEnd": "2016-10-12T22:15:00+02:00", "dTimStart": "2016-10-12T20:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/D cutting machine.\nCollected swarf", "dTimEnd": "2016-10-12T22:30:00+02:00", "dTimStart": "2016-10-12T22:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/O riser joint (lift #5).", "dTimEnd": "2016-10-12T22:45:00+02:00", "dTimStart": "2016-10-12T22:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled riser (lift #6).\nRemoved master bushing. Pulled flange through rotary, installed master bushing and elevator.\nLanded riser onto elevator.", "dTimEnd": "2016-10-12T23:15:00+02:00", "dTimStart": "2016-10-12T22:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/U cutting machine and cut riser.", "dTimEnd": "2016-10-12T23:45:00+02:00", "dTimStart": "2016-10-12T23:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "R/D cutting machine. Collected swarf.", "dTimEnd": "2016-10-13T00:00:00+02:00", "dTimStart": "2016-10-12T23:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_4_2016_10_14
NO 15/9-F-4
NO 15/9-F-4
name
2016-10-13T00:00:00+02:00
2016-10-14T00:00:00+02:00
normal
2018-05-03T13:52:58+02:00
{ "name": "15/9-F-4", "namingSystem": "NPD code" }
[ { "name": "15/9-F-4", "namingSystem": "NPD code" }, { "name": "5693", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-03-10T00:00:00+01:00", "dateDrillComplete": "2008-02-28", "daysBehind": null, "operator": "Statoil", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2016-10-14T00:00:00+02:00", "dTimDiaHoleStart": "2016-10-01T15:00:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "None", "hpht": "0", "md": "-999.99", "mdCsgLast": "3508", "mdDiaHoleStart": "3500", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "2755", "mdStrengthForm": "2760", "presTestType": "formation integrity test", "reportNo": "13", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "None", "tightWell": "0", "tvd": null, "tvdCsgLast": "3136.9", "tvdStrengthForm": "2599", "waterDepth": "91", "wellheadElevation": "138.7" } ]
[]
[]
[]
[ { "comments": "L/O riser joint (lift #6).", "dTimEnd": "2016-10-13T00:15:00+02:00", "dTimStart": "2016-10-13T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lifted riser (lift #7).\nRemoved master bushing.\nPulled riser.\nInstalled master bushing and hole cover in rotary.", "dTimEnd": "2016-10-13T00:45:00+02:00", "dTimStart": "2016-10-13T00:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/O riser joint.", "dTimEnd": "2016-10-13T01:15:00+02:00", "dTimStart": "2016-10-13T00:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed hole covers and hatches.", "dTimEnd": "2016-10-13T02:15:00+02:00", "dTimStart": "2016-10-13T01:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Changed elevator to handle BHA.\nMeanwhile: Removed scaffolding in moonpool.\n\n******* END OF REPORT *******", "dTimEnd": "2016-10-13T02:30:00+02:00", "dTimStart": "2016-10-13T02:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "plug abandon -- other", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2007_11_15
NO 15/9-F-5
NO 15/9-F-5
name
2007-11-14T00:00:00+01:00
2007-11-15T00:00:00+01:00
normal
2018-05-03T13:52:58+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2007-11-15T00:00:00+01:00", "dTimDiaHoleStart": null, "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Re-establish rig condition for operation. Pick up and make up 36\" BHA. Drill 36\" hole. ", "hpht": "0", "md": "0", "mdCsgLast": null, "mdDiaHoleStart": null, "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "0", "presTestType": null, "reportNo": "1", "ropCurrent": "-999.99", "strengthForm": "0", "sum24Hr": "Held tool box talk prior to skidding of the cantilever from F-14 to F-5. Skidded the catilever from F-14 to F-5.", "tightWell": "0", "tvd": null, "tvdCsgLast": null, "tvdStrengthForm": "0", "waterDepth": "91", "wellheadElevation": "0" } ]
[]
[]
[]
[]
[]
15_9_F_5_2007_11_16
NO 15/9-F-5
NO 15/9-F-5
name
2007-11-15T00:00:00+01:00
2007-11-16T00:00:00+01:00
normal
2018-05-03T13:52:59+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2007-11-16T00:00:00+01:00", "dTimDiaHoleStart": "2007-11-15T21:30:00+01:00", "diaHole": "36", "diaPilot": null, "distDrill": "10", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Drill 36\" to TD 222.8 m. Prepare and RIH with 30\" conductor.", "hpht": "0", "md": "155", "mdCsgLast": null, "mdDiaHoleStart": "144", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "0", "presTestType": null, "reportNo": "1", "ropCurrent": "-999.99", "strengthForm": "0", "sum24Hr": "Installed the rotating link adapter to TDS. Picked up and made up the 36\" BHA assembly. Drilled 36\" hole from 144 m to 165 m MD. ", "tightWell": "0", "tvd": "155", "tvdCsgLast": null, "tvdStrengthForm": "0", "waterDepth": "91", "wellheadElevation": "0" } ]
[ { "dTim": "2007-11-15T15:00:00+01:00", "density": "1.05", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "145", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "121", "yp": "-999.99" }, { "dTim": "2007-11-15T15:30:00+01:00", "density": "1.4", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "-999.99", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "120", "yp": "-999.99" } ]
[ { "dTim": "2007-11-16T00:00:00+01:00", "equivalentMudWeight": "1.03", "md": "164", "readingKind": "estimated" } ]
[]
[ { "comments": "Held tool box talk prior to skidding of the cantilever from F-14 to F-5", "dTimEnd": "2007-11-15T05:00:00+01:00", "dTimStart": "2007-11-15T04:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Skidded the catilever from F-14 to F-5.", "dTimEnd": "2007-11-15T05:45:00+01:00", "dTimStart": "2007-11-15T05:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Started to re-establish rig condition for operation.", "dTimEnd": "2007-11-15T06:00:00+01:00", "dTimStart": "2007-11-15T05:45:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed handrails on weather deck and lower levels in well head modul.\n", "dTimEnd": "2007-11-15T07:00:00+01:00", "dTimStart": "2007-11-15T06:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk with day shift. Removed hatch cover from F-5 at well bay area. Failure on TDS.\n", "dTimEnd": "2007-11-15T09:00:00+01:00", "dTimStart": "2007-11-15T07:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- repair", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Prepared and installed the rotating link adapter to TDS. Meanwhile removed hatch covers on F-14 prior to installing DCI stab for CRI hose.\n", "dTimEnd": "2007-11-15T10:30:00+01:00", "dTimStart": "2007-11-15T09:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Performed derrick inspection prior to start drilling 36\" hole.\n", "dTimEnd": "2007-11-15T11:00:00+01:00", "dTimStart": "2007-11-15T10:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk. Picked up and made up the 36\" BHA assembly. RIH with the 36\" BHA. Meanwhile ROV prepared to install DCI stab for CRI hose.", "dTimEnd": "2007-11-15T14:00:00+01:00", "dTimStart": "2007-11-15T11:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed oil filter and solenoid valve to TDS. Function tested TDS, the rotating link adapter and torque wrench. Meanwhile prepared and connected DCI stab for CRI hose.", "dTimEnd": "2007-11-15T17:00:00+01:00", "dTimStart": "2007-11-15T14:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Serviced and inspected the TDS prior to start drilling the 36\" hole. Prepared for moving drill cutting funnel from F-5.\n", "dTimEnd": "2007-11-15T18:00:00+01:00", "dTimStart": "2007-11-15T17:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Moved the drill cutting funnel from F-5. Using tugger and ROV.", "dTimEnd": "2007-11-15T20:15:00+01:00", "dTimStart": "2007-11-15T18:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "36\" BHA entered slot # 5 assisted by ROV.", "dTimEnd": "2007-11-15T21:30:00+01:00", "dTimStart": "2007-11-15T20:15:00+01:00", "md": "144", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Attempted to wash down 36\" BHA through template. \nDrilled 36\" hole from 144 m to 149 m MD.\nDrilling parameters : Flow 1000 lpm / SPP 4-5 bar / 18 RPM / Torque 3-12 kNm / WOB 1-10 MT. Drilling bushing landed out in template guide-funnel.\nParked ROV in garage. \n", "dTimEnd": "2007-11-15T23:30:00+01:00", "dTimStart": "2007-11-15T21:30:00+01:00", "md": "149", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled 36\" hole from 149 m to 155 m MD. \nDrilling parameters : Flow 1000 lpm / SPP 2 bar / 20 RPM / Torque 2-4 kNm / WOB 1-2 MT / ROP 3,5 m/hr.", "dTimEnd": "2007-11-16T00:00:00+01:00", "dTimStart": "2007-11-15T23:30:00+01:00", "md": "155", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2007_11_17
NO 15/9-F-5
NO 15/9-F-5
name
2007-11-16T00:00:00+01:00
2007-11-17T00:00:00+01:00
normal
2018-05-03T13:52:59+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2007-11-17T00:00:00+01:00", "dTimDiaHoleStart": "2007-11-15T21:30:00+01:00", "diaHole": "36", "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "RIH with 30\" conductor and cement same. Wait for the cement to set.", "hpht": "0", "md": "226", "mdCsgLast": null, "mdDiaHoleStart": "144", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "0", "presTestType": null, "reportNo": "2", "ropCurrent": "-999.99", "strengthForm": "0", "sum24Hr": "Drilled 36\" hole from 164 m to 226 m MD. Survey at 225 m 0.26 inc. Tight spot at 213m, reamed hole clear. POOH with 36\" BHA from 226m to surface. L/O 36\" HO. R/U for running of 30\" conductor. Started to RIH with 30\" conductor.", "tightWell": "0", "tvd": "226", "tvdCsgLast": null, "tvdStrengthForm": "0", "waterDepth": "91", "wellheadElevation": "0" } ]
[ { "dTim": "2007-11-16T16:00:00+01:00", "density": "1.4", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "226", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "122", "yp": "-999.99" }, { "dTim": "2007-11-16T13:00:00+01:00", "density": "1.05", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "200", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "145", "yp": "-999.99" } ]
[ { "dTim": "2007-11-17T00:00:00+01:00", "equivalentMudWeight": "1.03", "md": "226", "readingKind": "estimated" } ]
[]
[ { "comments": "Drilled 36\" hole from 155 m to 164 m MD. \nDrilling parameters : Flow 1000-2200 lpm / SPP 2-15 bar / 20-70 RPM / Torque 2-9 kNm / WOB 2-3 MT / ROP 1-4.5 m/hr. Pumped 20m³ hi-vis pills prior to connection.\n\nSurvey at 150.92 m 0.63 inc", "dTimEnd": "2007-11-16T04:15:00+01:00", "dTimStart": "2007-11-16T00:00:00+01:00", "md": "164", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Reamed hole from 164 m to 155 m \nReaming parameters : Flow 3100 lpm / SPP 36 bar / 70-90 RPM / Torque 2-4 kNm \n\n1. survey at 150.92 m 0.63 inc\n2. survey at 150.92 m 0.57 inc\n", "dTimEnd": "2007-11-16T05:45:00+01:00", "dTimStart": "2007-11-16T04:15:00+01:00", "md": "164", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled 36\" hole from 164 m to 165 m MD. \nDrilling parameters : Flow 4000 lpm / SPP 66 bar / 90 RPM / Torque 2-6 kNm / WOB 0-1 MT / ROP 12 m/hr.", "dTimEnd": "2007-11-16T06:00:00+01:00", "dTimStart": "2007-11-16T05:45:00+01:00", "md": "165", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled 36\" hole from 164m to 226m MD.(17½\" bit depth) \nDrilling parameters: Flow 4000-4640 lpm / SPP 62-84 bar / 90 RPM / Torque 2-8 kNm / WOB 1-3 MT / ROP 6-18 m/hr. \n\nPumped 20 m3 hi-vis pills prior to connection. \n\nSurvey at 177 m 0.55 inc\nSurvey at 187 m 0.47 inc\nSurvey at 197 m 0.46 inc\nSurvey at 207 m 0.27 inc\nSurvey at 217 m 0.33 inc\nSurvey at 225 m 0.26 inc\n", "dTimEnd": "2007-11-16T15:30:00+01:00", "dTimStart": "2007-11-16T06:00:00+01:00", "md": "226", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "TD with 17½\" bit at 226m, TD 36\" HO 222.8m. Circulated with sea water and pumped 25m³ hi-vis pills. Displaced well to 1.4 SG mud.", "dTimEnd": "2007-11-16T16:00:00+01:00", "dTimStart": "2007-11-16T15:30:00+01:00", "md": "226", "phase": "fixed", "proprietaryCode": "drilling -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to POOH. Started to POOH at 226m. Took 20MT overpull at 213m. Made up TDS and rotated pipe without pumping. Attempted to work through tight spot without rotation. Commenced to pump sea water at 1000 lpm and 30 rpm. Worked string reaming through tight spot. Slided back to bottom. Reciprocated string and circulated bottom up with sea water at 4600 lpm. Went back to bottom and pumped 20m³ hi-vis pill and displaced well to 1.4 SG mud.\n", "dTimEnd": "2007-11-16T16:45:00+01:00", "dTimStart": "2007-11-16T16:00:00+01:00", "md": "226", "phase": "fixed", "proprietaryCode": "drilling -- ream", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with 36\" BHA from 226m to 150m. \n", "dTimEnd": "2007-11-16T17:15:00+01:00", "dTimStart": "2007-11-16T16:45:00+01:00", "md": "150", "phase": "fixed", "proprietaryCode": "drilling -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "At 150m, 5m below sea bed topped up hole with 5m³ 1.4 SG mud. Continued POOH with 36\" BHA from 150m to 131m.", "dTimEnd": "2007-11-16T19:00:00+01:00", "dTimStart": "2007-11-16T17:15:00+01:00", "md": "131", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk with night shift prior to POOH with the 36\" BHA.\n", "dTimEnd": "2007-11-16T19:15:00+01:00", "dTimStart": "2007-11-16T19:00:00+01:00", "md": "131", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "General check of handling gear and checked dies in PRS's. Found FWD PRS dies to be normal dies.\n", "dTimEnd": "2007-11-16T19:30:00+01:00", "dTimStart": "2007-11-16T19:15:00+01:00", "md": "131", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Changed out dies in FWD PRS to Monell dies. \n", "dTimEnd": "2007-11-16T21:15:00+01:00", "dTimStart": "2007-11-16T19:30:00+01:00", "md": "131", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with 36\" BHA from 131m to 20m and racked back in derrick.\n", "dTimEnd": "2007-11-17T00:00:00+01:00", "dTimStart": "2007-11-16T21:15:00+01:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2007_11_18
NO 15/9-F-5
NO 15/9-F-5
name
2007-11-17T00:00:00+01:00
2007-11-18T00:00:00+01:00
normal
2018-05-03T13:52:59+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": ".7", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2007-11-18T00:00:00+01:00", "dTimDiaHoleStart": "2007-11-15T21:30:00+01:00", "diaHole": "36", "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Wait for cement to set. Release with CART tool pull same and rack back CART tool in derrick. Prepare for skidding and skid cantilever to F-15.", "hpht": "0", "md": "226", "mdCsgLast": "220.8", "mdDiaHoleStart": "144", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "0", "presTestType": null, "reportNo": "3", "ropCurrent": "-999.99", "strengthForm": "0", "sum24Hr": "RIH with 30\" conductor from surface to 220.8m. Cemented 30\" conductor. Wait for cement to set.", "tightWell": "0", "tvd": "226", "tvdCsgLast": "220.8", "tvdStrengthForm": "0", "waterDepth": "91", "wellheadElevation": "0" } ]
[ { "dTim": "2007-11-17T16:00:00+01:00", "density": "1.4", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "226", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "104", "yp": "-999.99" }, { "dTim": "2007-11-17T13:00:00+01:00", "density": "1.05", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "200", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "121", "yp": "-999.99" } ]
[ { "dTim": "2007-11-18T00:00:00+01:00", "equivalentMudWeight": "1.03", "md": "226", "readingKind": "estimated" } ]
[]
[ { "comments": "POOH with 36\" HO, cleaned and checked HO found in good condition. Laid out 36\" HO. Simultaneously ROV/Halliburton prepared forpressure testing of the CRI hose.\n", "dTimEnd": "2007-11-17T01:15:00+01:00", "dTimStart": "2007-11-17T00:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed elevators, bails and installed cradles on HTS. Meanwhile operated the CRI valve.Pressure tested the CRI hose to 200bars 10 min, 47l 100bars and 65l 200bars.", "dTimEnd": "2007-11-17T02:15:00+01:00", "dTimStart": "2007-11-17T01:15:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Serviced and inspected the TDS.\n", "dTimEnd": "2007-11-17T02:45:00+01:00", "dTimStart": "2007-11-17T02:15:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Isolated and de-isolated TDS.", "dTimEnd": "2007-11-17T03:00:00+01:00", "dTimStart": "2007-11-17T02:45:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Held tool box talk prior to rig surface equipment for running conductor. Rigged up same.\n", "dTimEnd": "2007-11-17T03:45:00+01:00", "dTimStart": "2007-11-17T03:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk with all involved personnel prior to RIH with 30\" conductor", "dTimEnd": "2007-11-17T04:15:00+01:00", "dTimStart": "2007-11-17T03:45:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up 30\" conductor shoe. Installed 30\" bushing and landed conductor in rotary. Filled 30\" conductor with water and tested float.", "dTimEnd": "2007-11-17T06:00:00+01:00", "dTimStart": "2007-11-17T04:15:00+01:00", "md": "8", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to run in with 30\" conductor from 8m to 84m. Tool box talk was held with day shift, prior to running in with 30\" conductor.\n", "dTimEnd": "2007-11-17T11:00:00+01:00", "dTimStart": "2007-11-17T06:00:00+01:00", "md": "84", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to change from 30\" to 5½\" handling equipment. Changed handling equipment\n", "dTimEnd": "2007-11-17T12:45:00+01:00", "dTimStart": "2007-11-17T11:00:00+01:00", "md": "84", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to pick up well head housing. Commenced picking up well head housing. Lost communication to auxiliary control.\n", "dTimEnd": "2007-11-17T13:00:00+01:00", "dTimStart": "2007-11-17T12:45:00+01:00", "md": "84", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Re-established communication to auxiliary control.\n", "dTimEnd": "2007-11-17T13:15:00+01:00", "dTimStart": "2007-11-17T13:00:00+01:00", "md": "84", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Picked up and made up the 30\" housing. Made up torque is 36 000 ft-lbs (49.000 Nm). Engage locking system with lock-plate. Secure with cap-screws. Inspect housing. Made several attempts to remove the 30\" housing protector.", "dTimEnd": "2007-11-17T15:30:00+01:00", "dTimStart": "2007-11-17T13:15:00+01:00", "md": "84", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cut of the protector of the 30\" housing.\n", "dTimEnd": "2007-11-17T16:15:00+01:00", "dTimStart": "2007-11-17T15:30:00+01:00", "md": "84", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Broke out housing handling tool. Laid out same. Filled the conductor with sea water to minimize the movement of the conductor.", "dTimEnd": "2007-11-17T16:30:00+01:00", "dTimStart": "2007-11-17T16:15:00+01:00", "md": "84", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to handling of the aluminum inner string. Rigged up inner string C-Plate on top of 30\" housing joint. Secure plate. Ran aluminum cement stinger. Installed the X-O for the CART.\n", "dTimEnd": "2007-11-17T17:45:00+01:00", "dTimStart": "2007-11-17T16:30:00+01:00", "md": "84", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked the CART from derrick and made up to X-O. Locked CART to housing as per Vetco instruction. Installed inclinometer and handle on 2\" fill up valve on CART. Simultaneously rigged up tugger in well bay area for ROV guide lines.\n", "dTimEnd": "2007-11-17T18:45:00+01:00", "dTimStart": "2007-11-17T17:45:00+01:00", "md": "84", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed pull test on CART tool. Removed C-plate. Ran conductor through rotary, and inserted master bushing.", "dTimEnd": "2007-11-17T19:15:00+01:00", "dTimStart": "2007-11-17T18:45:00+01:00", "md": "84", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Ran in with 30\" conductor on 5½\" HWDP from 84m to 105m. Attached wire sling to conductor housing for pulling arrangement if need it. \n", "dTimEnd": "2007-11-17T20:00:00+01:00", "dTimStart": "2007-11-17T19:15:00+01:00", "md": "105", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued run in with 30\" conductor on 5½\" HWDP from 105m to 135m, well head level.\n", "dTimEnd": "2007-11-17T21:00:00+01:00", "dTimStart": "2007-11-17T20:00:00+01:00", "md": "135", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Connected up to TDS and filled conductor at 900 lpm, 3,8 bars. Positive indication at shoe.\n", "dTimEnd": "2007-11-17T21:30:00+01:00", "dTimStart": "2007-11-17T21:00:00+01:00", "md": "135", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Ran in with 30\" conductor on 5½\" HWDP from 135m to 147m. Entered the template.\n", "dTimEnd": "2007-11-17T21:45:00+01:00", "dTimStart": "2007-11-17T21:30:00+01:00", "md": "147", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued RIH with 30\" conductor on 5½\" HWDP from 147m to 220.8m.\n", "dTimEnd": "2007-11-17T23:00:00+01:00", "dTimStart": "2007-11-17T21:45:00+01:00", "md": "220.8", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up side entry sub and made up to TDS.\n", "dTimEnd": "2007-11-17T23:30:00+01:00", "dTimStart": "2007-11-17T23:00:00+01:00", "md": "220.8", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Established circulating with 2\" valve open at CART tool. Hook load 110 MT. ROV confirmed returns at 2\" valve. \n", "dTimEnd": "2007-11-18T00:00:00+01:00", "dTimStart": "2007-11-17T23:30:00+01:00", "md": "220.8", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2007_11_19
NO 15/9-F-5
NO 15/9-F-5
name
2007-11-18T00:00:00+01:00
2007-11-19T00:00:00+01:00
normal
2018-05-03T13:52:59+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": ".9", "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2007-11-19T00:00:00+01:00", "dTimDiaHoleStart": "2007-11-15T21:30:00+01:00", "diaHole": "36", "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Drill 36\" top hole F-15. ", "hpht": "0", "md": "226", "mdCsgLast": "220.8", "mdDiaHoleStart": "144", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "0", "presTestType": null, "reportNo": "4", "ropCurrent": "-999.99", "strengthForm": "0", "sum24Hr": "Waited on cement to set. Released CART tool. Pulled same and rack back CART tool in derrick. Prepared for skidding and skid cantilever to F-15", "tightWell": "0", "tvd": "226", "tvdCsgLast": "220.8", "tvdStrengthForm": "0", "waterDepth": "91", "wellheadElevation": "0" } ]
[ { "dTim": "2007-11-18T23:00:00+01:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "226", "mudClass": "other", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Seawater", "visFunnel": "-999.99", "yp": "-999.99" }, { "dTim": "2007-11-18T22:00:00+01:00", "density": "1.4", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "226", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "125", "yp": "-999.99" }, { "dTim": "2007-11-18T22:30:00+01:00", "density": "1.05", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "226", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "108", "yp": "-999.99" } ]
[ { "dTim": "2007-11-19T00:00:00+01:00", "equivalentMudWeight": "103", "md": "226", "readingKind": "estimated" } ]
[]
[ { "comments": "Closed 2\" valve and established circulation through the 30\" shoe.\n", "dTimEnd": "2007-11-18T00:15:00+01:00", "dTimStart": "2007-11-18T00:00:00+01:00", "md": "220.8", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Verified setting depth with Digiquartz against F-7. Final 110 MT hook load. Checked centralization of conductor housing - OK. Inclination 0.22/0.28 degrees.\n", "dTimEnd": "2007-11-18T01:15:00+01:00", "dTimStart": "2007-11-18T00:15:00+01:00", "md": "220.8", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Established circulation at 2500 lpm, 3,8 bars, 112 MT hook load. ROV confirmed 2\" valve not to be leaking and surveyed for returns, Observed returns from F-5 only. Meanwhile pressure tested cement line to 200 bars 10 min.\n", "dTimEnd": "2007-11-18T02:30:00+01:00", "dTimStart": "2007-11-18T01:15:00+01:00", "md": "220.8", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Mixed and pumped 55.7 m³ 1.52 sg Tuned Light XL cement slurry at 1100 lpm, 25 bars pump pressure. Confirmed returns to seabed. Displaced cement slurry with 6.7 m³ of SW at max rate using cement unit. FCP 7bars, 600lpm. Bled off pressure, 250 l. Checked for back-flow. Removed cmt hose and flushed through manifolds and hoses.\n", "dTimEnd": "2007-11-18T04:00:00+01:00", "dTimStart": "2007-11-18T02:30:00+01:00", "md": "220.8", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited on cement to set. Meanwhile prepared for wire change on FWD PRS, General maintenance. Started injecting slop into F-12 annulus.", "dTimEnd": "2007-11-18T06:00:00+01:00", "dTimStart": "2007-11-18T04:00:00+01:00", "md": "220.8", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited on cement to set. Meanwhile function tested rotating link adapter and torque wrench. Prepared cantilever for skidding to F-15. Performed general maintenance on the rig floor. Injected slop into F-12 injection annulus.\n", "dTimEnd": "2007-11-18T16:00:00+01:00", "dTimStart": "2007-11-18T06:00:00+01:00", "md": "220.8", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Confirmed inclinometer before release of CART. Released CART tool. Broke out and laid out the side entry sub and two 5½\" pups. Racked back one stand. Dropped one sponge ball and flushed landing string and inner string with sea water. Continued pull out with landing string. With CART in rotary removed 2\" valve handle and inclinometer. Function tested CART.\n\nInclinometer measurements CART:\nBefore release, Top: -0.27 Bottom: 0.24\n\nDigiquartz measurement of 30\" conductor two measurements after releasing CART: \nF-5 96584mm F-7 96606mm = F-5 23mm deeper\nF-5 96603mm F-7 96602mm = F-5 1mm high\n", "dTimEnd": "2007-11-18T18:00:00+01:00", "dTimStart": "2007-11-18T16:00:00+01:00", "md": "143", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke out X/O and racked back the CART tool in derrick. Laid out the aluminium inner string. Held tool box with night shift prior to handling of the CART tool and aluminium inner string. \n", "dTimEnd": "2007-11-18T20:30:00+01:00", "dTimStart": "2007-11-18T18:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Prepared for skidding. Meanwhile installed CTS funnel on F-14. Picked up new 36\" HO.\n", "dTimEnd": "2007-11-18T23:30:00+01:00", "dTimStart": "2007-11-18T20:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to skidding of the cantilever from F-5 to F-15", "dTimEnd": "2007-11-18T23:45:00+01:00", "dTimStart": "2007-11-18T23:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2007_12_18
NO 15/9-F-5
NO 15/9-F-5
name
2007-12-17T00:00:00+01:00
2007-12-18T00:00:00+01:00
normal
2018-05-03T13:52:59+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2007-12-18T00:00:00+01:00", "dTimDiaHoleStart": "2007-12-17T01:30:00+01:00", "diaHole": "36", "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Drilled 17 1/2\" section from 233 m to 710 m MD.", "hpht": "0", "md": "226", "mdCsgLast": "220.8", "mdDiaHoleStart": "226", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "0", "presTestType": null, "reportNo": "5", "ropCurrent": "-999.99", "strengthForm": "0", "sum24Hr": "MU and RIH with 17 1/2\" BHA. Performed slip & cut. Drilled out 30\" shoe. Drilled 17 1/2\" section to 233 m MD. RU and ran single shot gyro survey.", "tightWell": "0", "tvd": "226", "tvdCsgLast": "220.8", "tvdStrengthForm": "0", "waterDepth": "91", "wellheadElevation": "0" } ]
[ { "dTim": "2007-12-17T23:00:00+01:00", "density": "1.05", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "-999.99", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "138", "yp": "-999.99" }, { "dTim": "2007-12-17T22:00:00+01:00", "density": "1.4", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "-999.99", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "132", "yp": "-999.99" } ]
[ { "dTim": "2007-12-18T00:00:00+01:00", "equivalentMudWeight": "1.03", "md": "226", "readingKind": "estimated" } ]
[]
[ { "comments": "Removed scaffolding from hatch opening on F-9 and installed hatch covers. Removed hatch cover from F-5. Prepared for skidding.", "dTimEnd": "2007-12-17T03:30:00+01:00", "dTimStart": "2007-12-17T01:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to skidding rig from F-9 to F-5. Skidded rig 1.5 m port and 2.25 m aft.", "dTimEnd": "2007-12-17T05:00:00+01:00", "dTimStart": "2007-12-17T03:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Checked that all decks were in alignment. Rearranged hatches on all decks in WH module for F-9 and F-5. Installed scaffolding barriers.\n\nMeanwhile transported new 17 1/2\" BHA components to drill floor.", "dTimEnd": "2007-12-17T06:00:00+01:00", "dTimStart": "2007-12-17T05:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "PU and MU 17 1/2\" bit, motor, 17 1/4\" stab, GWD, power pulse and UBHO. RIH with 17 1/2\" BHA to 35 m.", "dTimEnd": "2007-12-17T11:00:00+01:00", "dTimStart": "2007-12-17T06:00:00+01:00", "md": "35", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Checked oil in PRS and serviced same; experienced communication problems to TDS.", "dTimEnd": "2007-12-17T11:30:00+01:00", "dTimStart": "2007-12-17T11:00:00+01:00", "md": "35", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Troubleshot lost communication to TDS. Found faulty profibus connector. MU temporary solution.", "dTimEnd": "2007-12-17T13:00:00+01:00", "dTimStart": "2007-12-17T11:30:00+01:00", "md": "35", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "MU and RIH with 17 1/2\" BHA from 35 m to 158 m. Sat UHBO sleeve to high side scribe line. Stabbed into CTS on top of conductor housing while observing with ROV.", "dTimEnd": "2007-12-17T17:00:00+01:00", "dTimStart": "2007-12-17T13:00:00+01:00", "md": "158", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box meeting with both shifts before cutting drill line. Performed cut & slip.\n\nMeanwhile changed out faulty profibus connector on top drive.", "dTimEnd": "2007-12-17T20:00:00+01:00", "dTimStart": "2007-12-17T17:00:00+01:00", "md": "158", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued performing cut & slip.\n\nMeanwhile changed out faulty profibus connector on top drive.", "dTimEnd": "2007-12-17T22:00:00+01:00", "dTimStart": "2007-12-17T20:00:00+01:00", "md": "158", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued RIH from 158 m to 195 m. Washed down from 195 m with 2000 lpm / 50 bar / 20 RPM. Tagged cement at 218 m. Connected CTS hose to ROV and started pumping with dredge pump.", "dTimEnd": "2007-12-17T23:15:00+01:00", "dTimStart": "2007-12-17T22:00:00+01:00", "md": "218", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled out 30\" shoe and rathole from 218 m to 219.5 m MD. Drilling parameters : Flow 3500 lpm / SPP 87 bar / Rotation 40 rpm / Torque 1-3 kNm / WOB 0-3 MT. Reamed back inside shoe for every 2 m drilled. Pumped 10 m3 his-vis sweep as required to clean the hole.", "dTimEnd": "2007-12-18T00:00:00+01:00", "dTimStart": "2007-12-17T23:15:00+01:00", "md": "219.5", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2007_12_19
NO 15/9-F-5
NO 15/9-F-5
name
2007-12-18T00:00:00+01:00
2007-12-19T00:00:00+01:00
normal
2018-05-03T13:52:59+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2007-12-19T00:00:00+01:00", "dTimDiaHoleStart": "2007-12-18T02:30:00+01:00", "diaHole": "17.5", "diaPilot": null, "distDrill": "88", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Drill 17 1/2\" section from 475 m to 1005 m MD.", "hpht": "0", "md": "314", "mdCsgLast": "220.8", "mdDiaHoleStart": "226", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "0", "presTestType": null, "reportNo": "6", "ropCurrent": "-999.99", "strengthForm": "0", "sum24Hr": "Drilled 17 1/2\" section from 233 m to 273 m MD. POOH to change gMWD. Drilled 17 1/2\" section from 273 m to 280 m MD. Pulled back into 30\" conductor shoe to wait for ESD pre-testing. Drilled 17 1/2\" section from 280 m to 475 m MD.", "tightWell": "0", "tvd": "314", "tvdCsgLast": "220.8", "tvdStrengthForm": "0", "waterDepth": "91", "wellheadElevation": "0" } ]
[ { "dTim": "2007-12-18T23:00:00+01:00", "density": "1.05", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "-999.99", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "138", "yp": "-999.99" }, { "dTim": "2007-12-18T22:00:00+01:00", "density": "1.4", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "-999.99", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "132", "yp": "-999.99" } ]
[ { "dTim": "2007-12-19T00:00:00+01:00", "equivalentMudWeight": "1.03", "md": "226", "readingKind": "estimated" } ]
[ { "azi": "252.35", "dTim": "2007-12-19T00:00:00+01:00", "incl": ".4", "md": "170.1", "tvd": "170.1" }, { "azi": "255.69", "dTim": "2007-12-19T00:00:00+01:00", "incl": ".43", "md": "176", "tvd": "176" }, { "azi": "182.97", "dTim": "2007-12-19T00:00:00+01:00", "incl": ".18", "md": "215.5", "tvd": "215.5" }, { "azi": "195.36", "dTim": "2007-12-19T00:00:00+01:00", "incl": "1.06", "md": "259.7", "tvd": "259.7" }, { "azi": "197.9", "dTim": "2007-12-19T00:00:00+01:00", "incl": "2.2", "md": "299.9", "tvd": "299.9" }, { "azi": "188.95", "dTim": "2007-12-19T00:00:00+01:00", "incl": "2.73", "md": "340.5", "tvd": "340.4" }, { "azi": "174.53", "dTim": "2007-12-19T00:00:00+01:00", "incl": "6.86", "md": "381.1", "tvd": "380.9" }, { "azi": "177.26", "dTim": "2007-12-19T00:00:00+01:00", "incl": "8.36", "md": "421.1", "tvd": "420.6" }, { "azi": "274.17", "dTim": "2007-12-19T00:00:00+01:00", "incl": ".45", "md": "160.1", "tvd": "160.1" } ]
[ { "comments": "Drilled out 30\" shoe and rathole from 217 m to 226 m MD. Drilling parameters : Flow 3500 lpm / SPP 87 bar / Rotation 40 rpm / Torque 1-3 kNm / WOB 1-3 MT. Reamed back inside shoe for every 2 m drilled. Pumped 10 m3 his-vis sweep as required to clean the hole.\n\nReamed hole and shoe track 3 times. No obstruction. Pulled through shoe track with no rotation. No obstruction. Pumped 10 m3 hi-vis and circulated BU while reciprocating 17 1/2\" BHA. Up weight 105 MT / down weight 100 MT.", "dTimEnd": "2007-12-18T02:30:00+01:00", "dTimStart": "2007-12-18T00:00:00+01:00", "md": "226", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled 17 1/2\" section from 226 m to 233 m MD. Drilling parameters : Flow 3100 lpm / SPP 72 bar / WOB 1-3 MT / Torque 1-5 kNm / String RPM 40 / Bit RPM 133. ROP 10 m/hr. Pumped 10 m3 hi-vis sweep for every singel drilled. Performed gMWD survey on connection. Used sling and tugger on centralizer deck on drillpipe to stabilize same before taking survey.\n\nSliding intervals: 230 - 233 m\n\nGot good gMWD survey on 215.5 m: Inc 0.18 AZ 182.97. Made two attempts to get gMWD survey at 222.5 m. No sucess.", "dTimEnd": "2007-12-18T04:15:00+01:00", "dTimStart": "2007-12-18T02:30:00+01:00", "md": "233", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled 17 1/2\" BHA back inside shoe at 214 m. Held tool box meeting and RU to run wireline gyro.", "dTimEnd": "2007-12-18T05:00:00+01:00", "dTimStart": "2007-12-18T04:15:00+01:00", "md": "214", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "-", "dTimEnd": "2007-12-18T06:00:00+01:00", "dTimStart": "2007-12-18T05:00:00+01:00", "md": "214", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH single shot gyro from 176 m MD.", "dTimEnd": "2007-12-18T06:30:00+01:00", "dTimStart": "2007-12-18T06:00:00+01:00", "md": "214", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled 17 1/2\" section from 233 m to 273 m MD. Drilling parameters : Flow 3000-3400 lpm / SPP 67-88 bar / WOB 2-6 MT / Torque 2-4 kNm / String RPM 40 / Bit RPM 133. ROP 11-20 m/hr. Average ROP 12 m/hr. Pumped 10 m3 hi-vis sweep for every singel drilled. Used sling and tugger on centralizer deck on drillpipe to stabilize same before taking survey.\n\nSliding intervals: 230 - 250 m\n\nAttempted to get gMWD survey at 261.5 m. No sucess.", "dTimEnd": "2007-12-18T09:45:00+01:00", "dTimStart": "2007-12-18T06:30:00+01:00", "md": "273", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Displaced open hole to 1.40 sg bentonite mud, 10 m3 at 2000 lpm / 55 bar.", "dTimEnd": "2007-12-18T10:00:00+01:00", "dTimStart": "2007-12-18T09:45:00+01:00", "md": "273", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "POOH with 17 1/2\" drilling BHA from 273 m to 23 m. Stopped with bit inside 30\" conductor to inspect TDS and derrick for loose items.", "dTimEnd": "2007-12-18T13:00:00+01:00", "dTimStart": "2007-12-18T10:00:00+01:00", "md": "23", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Removed gMWD probe . Lifted probe to drill floor and installed same.", "dTimEnd": "2007-12-18T15:00:00+01:00", "dTimStart": "2007-12-18T13:00:00+01:00", "md": "23", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "MU and RIH with 17 1/2\" BHA from 23 to 196 m MD.", "dTimEnd": "2007-12-18T17:00:00+01:00", "dTimStart": "2007-12-18T15:00:00+01:00", "md": "196", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued RIH from 196 m to 273 m. Washed down from 196 m with 2000 lpm / 50 bar. Reamed shoe. No obstructions observed. Connected CTS hose to ROV and started pumping with dredge pump.", "dTimEnd": "2007-12-18T18:00:00+01:00", "dTimStart": "2007-12-18T17:00:00+01:00", "md": "273", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Drilled 17 1/2\" section from 273 m to 280 m MD. Drilling parameters : Flow 3000 lpm / SPP 65 bar / WOB 2 MT / Bit RPM 90. ROP 10 m/hr. Pumped 10 m3 hi-vis sweep for every singel drilled. Performed gyro MWD orientation OK. Stopped drilling due to preparations for upcoming ESD test.\n\nSliding intervals: 273 - 280 m", "dTimEnd": "2007-12-18T19:00:00+01:00", "dTimStart": "2007-12-18T18:00:00+01:00", "md": "280", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pumped 10 m3 hi-vis sweep at 280 m to clean the hole. Displaced open hole to 1.40 sg bentonite mud, 15 m3 at 2000 lpm / 55 bar. POOH with 17 1/2\" drilling BHA from 280 m to inside 30\" conductor shoe at 195 m.", "dTimEnd": "2007-12-18T20:00:00+01:00", "dTimStart": "2007-12-18T19:00:00+01:00", "md": "214", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed ESD pre- testing and had power shut down on rig.", "dTimEnd": "2007-12-18T21:00:00+01:00", "dTimStart": "2007-12-18T20:00:00+01:00", "md": "214", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 17 1/2\" BHA from 195 to 280 m MD. Took survey to link up toolface. Connected CTS hose to ROV and started pumping with dredge pump.", "dTimEnd": "2007-12-18T22:00:00+01:00", "dTimStart": "2007-12-18T21:00:00+01:00", "md": "280", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled 17 1/2\" section from 280 m to 314 m MD. Drilling parameters : Flow 3200 lpm / SPP 74-78 bar / WOB 2-6 MT / Torque 3-4 kNm / String RPM 40 / Bit RPM 136. ROP 15-40 m/hr, average ROP 17 m/ hrs. Pumped 10 m3 hi-vis sweep for every singel drilled. Performed gMWD survey on connections. Used sling and tugger on centralizer deck on drillpipe to stabilize same before taking survey.\n\nSliding intervals: 280 - 288 m\n 305 - 314 m\n", "dTimEnd": "2007-12-19T00:00:00+01:00", "dTimStart": "2007-12-18T22:00:00+01:00", "md": "314", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2007_12_20
NO 15/9-F-5
NO 15/9-F-5
name
2007-12-19T00:00:00+01:00
2007-12-20T00:00:00+01:00
normal
2018-05-03T13:52:59+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2007-12-20T00:00:00+01:00", "dTimDiaHoleStart": "2007-12-18T02:30:00+01:00", "diaHole": "17.5", "diaPilot": null, "distDrill": "564", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Drill 17 1/2\" section from 1101 m to TD at 1400 m MD. Circulate well clean and displace to 1.40 bentonite mud. POOH and LD 17 1/2\" BHA.", "hpht": "0", "md": "878", "mdCsgLast": "220.8", "mdDiaHoleStart": "226", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "0", "presTestType": null, "reportNo": "7", "ropCurrent": "-999.99", "strengthForm": "0", "sum24Hr": "Drilled 17 1/2\" section from 475 m to 1101 m MD.", "tightWell": "0", "tvd": "860.3", "tvdCsgLast": "220.8", "tvdStrengthForm": "0", "waterDepth": "91", "wellheadElevation": "0" } ]
[ { "dTim": "2007-12-19T23:00:00+01:00", "density": "1.05", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "-999.99", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "138", "yp": "-999.99" }, { "dTim": "2007-12-19T22:00:00+01:00", "density": "1.4", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "-999.99", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "132", "yp": "-999.99" } ]
[ { "dTim": "2007-12-20T00:00:00+01:00", "equivalentMudWeight": "1.03", "md": "1101", "readingKind": "estimated" } ]
[ { "azi": "180.69", "dTim": "2007-12-20T00:00:00+01:00", "incl": "9.85", "md": "460.8", "tvd": "459.8" }, { "azi": "184.73", "dTim": "2007-12-20T00:00:00+01:00", "incl": "11.44", "md": "501.3", "tvd": "499.5" }, { "azi": "176.71", "dTim": "2007-12-20T00:00:00+01:00", "incl": "11.39", "md": "527.2", "tvd": "525" }, { "azi": "166.98", "dTim": "2007-12-20T00:00:00+01:00", "incl": "11.52", "md": "581.7", "tvd": "578.3" }, { "azi": "158.21", "dTim": "2007-12-20T00:00:00+01:00", "incl": "12.78", "md": "608.2", "tvd": "604.3" }, { "azi": "148.21", "dTim": "2007-12-20T00:00:00+01:00", "incl": "13.86", "md": "648.3", "tvd": "643.3" }, { "azi": "138.85", "dTim": "2007-12-20T00:00:00+01:00", "incl": "14.25", "md": "702.5", "tvd": "695.9" }, { "azi": "119.16", "dTim": "2007-12-20T00:00:00+01:00", "incl": "20.5", "md": "783.4", "tvd": "773.1" }, { "azi": "116.17", "dTim": "2007-12-20T00:00:00+01:00", "incl": "22.87", "md": "823.5", "tvd": "810.4" }, { "azi": "116.41", "dTim": "2007-12-20T00:00:00+01:00", "incl": "24.41", "md": "849.7", "tvd": "834.4" }, { "azi": "115.25", "dTim": "2007-12-20T00:00:00+01:00", "incl": "26.73", "md": "890.1", "tvd": "870.8" }, { "azi": "115.65", "dTim": "2007-12-20T00:00:00+01:00", "incl": "23.58", "md": "944.3", "tvd": "919.9" }, { "azi": "119.07", "dTim": "2007-12-20T00:00:00+01:00", "incl": "21.2", "md": "984.4", "tvd": "956.9" }, { "azi": "123.29", "dTim": "2007-12-20T00:00:00+01:00", "incl": "18.83", "md": "1025.4", "tvd": "995.5" }, { "azi": "129.97", "dTim": "2007-12-20T00:00:00+01:00", "incl": "17.16", "md": "743.4", "tvd": "735.2" } ]
[ { "comments": "Drilled 17 1/2\" section from 314 m to 475 m MD. Drilling parameters : Flow 3200-4000 lpm / SPP 74-160 bar / WOB 3-8 MT / Torque 2-5 kNm / String RPM 40 / Bit RPM 136-160. ROP 40-65 m/hr, average ROP 26.8 m/ hrs. Pumped 10 m3 hi-vis sweep for every singel drilled. Performed gMWD survey on connections. Used sling and tugger on centralizer deck on drillpipe to stabilize same before taking survey.\n\nSliding intervals: 314 - 328 m\n 355 - 380 m\n 395 - 407 m\n 435 - 447 m", "dTimEnd": "2007-12-19T06:00:00+01:00", "dTimStart": "2007-12-19T00:00:00+01:00", "md": "475", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled 17 1/2\" section from 475 m to 556 m MD. Drilling parameters : Flow 4000 lpm / SPP 114 bar / WOB 3-4 MT / Torque 2-5 kNm / String RPM 40 / Bit RPM 136-160. ROP +/-35 m/hr, average ROP 18.0 m/ hrs. Pumped 10 m3 hi-vis sweep for every single drilled. Performed gMWD survey on connections. Used sling and tugger on centralizer deck on drillpipe to stabilize same before taking survey. Up weight 112 MT / down weight 107 MT.\n\nAt 556 m made 3 attempts to take gMWD survey. Decided to drill on with MWD inc and azimuth. \n\nSliding intervals: 475 - 487 m\n 516 - 529 m\n", "dTimEnd": "2007-12-19T10:30:00+01:00", "dTimStart": "2007-12-19T06:00:00+01:00", "md": "556", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Could not open PS-21 slips due to connection time-out on auxillary SBC computer.", "dTimEnd": "2007-12-19T11:00:00+01:00", "dTimStart": "2007-12-19T10:30:00+01:00", "md": "556", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Drilled 17 1/2\" section from 556 m to 878 m MD (=Top Utsira). Drilling parameters : Flow 3500-4000 lpm / SPP 114-130 bar / WOB 8-10 MT / Torque 2-3 kNm / String RPM 40 / Bit RPM 105-160. ROP 30-40 m/hr, average ROP 24.8 m/ hrs. Pumped 10 m3 hi-vis sweep for every single drilled. Performed MWD survey on connections. Up weight 120 MT / down weight 112 MT.\n\nSliding intervals: 556 - 571 m\n 596 - 611 m\n 636 - 656 m\n 676 - 696 m\n 717 - 740 m\n 756 - 779 m\n 797 - 817 m\n 838 - 858 m\n", "dTimEnd": "2007-12-20T00:00:00+01:00", "dTimStart": "2007-12-19T11:00:00+01:00", "md": "878", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2007_12_21
NO 15/9-F-5
NO 15/9-F-5
name
2007-12-20T00:00:00+01:00
2007-12-21T00:00:00+01:00
normal
2018-05-03T13:53:00+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2007-12-21T00:00:00+01:00", "dTimDiaHoleStart": "2007-12-18T02:30:00+01:00", "diaHole": "17.5", "diaPilot": null, "distDrill": "537", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Complete handling of 17½\" BHA. Rig up for running 13 3/8\" casing on 18 3/4\" well head. Start RIH with 13 3/8\" casing.", "hpht": "0", "md": "1415", "mdCsgLast": "220.8", "mdDiaHoleStart": "226", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "0", "presTestType": null, "reportNo": "8", "ropCurrent": "-999.99", "strengthForm": "0", "sum24Hr": "Drilled 17 1/2\" section from 1101 m to 1415 m MD. Circulated well clean. Displaced well to 1.40 SG mud. POOH with 17½\" BHA. Had tight spot at 1123 m, rotated through. Tight spots at 796, 775, 519 and 481m, pulled through with 10-15 MT overpull. Rack back BHA.", "tightWell": "0", "tvd": "1346", "tvdCsgLast": "220.8", "tvdStrengthForm": "0", "waterDepth": "91", "wellheadElevation": "0" } ]
[ { "dTim": "2007-12-20T15:00:00+01:00", "density": "1.05", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "1322", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "139", "yp": "-999.99" }, { "dTim": "2007-12-20T19:00:00+01:00", "density": "1.4", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "1415", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "132", "yp": "-999.99" } ]
[ { "dTim": "2007-12-21T00:00:00+01:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[ { "azi": "121.18", "dTim": "2007-12-21T00:00:00+01:00", "incl": "16.01", "md": "1065.1", "tvd": "1033.3" }, { "azi": "117.23", "dTim": "2007-12-21T00:00:00+01:00", "incl": "16.28", "md": "1105.3", "tvd": "1072" }, { "azi": "112.92", "dTim": "2007-12-21T00:00:00+01:00", "incl": "19.97", "md": "1145.4", "tvd": "1110.1" }, { "azi": "107.56", "dTim": "2007-12-21T00:00:00+01:00", "incl": "24.46", "md": "1185.6", "tvd": "1147.3" }, { "azi": "99.65", "dTim": "2007-12-21T00:00:00+01:00", "incl": "28.06", "md": "1226.5", "tvd": "1184" }, { "azi": "102.38", "dTim": "2007-12-21T00:00:00+01:00", "incl": "31.94", "md": "1266.8", "tvd": "1218.8" }, { "azi": "108.35", "dTim": "2007-12-21T00:00:00+01:00", "incl": "29.21", "md": "1307.8", "tvd": "1254.1" }, { "azi": "105.01", "dTim": "2007-12-21T00:00:00+01:00", "incl": "27.27", "md": "1348", "tvd": "1289.6" }, { "azi": "107.83", "dTim": "2007-12-21T00:00:00+01:00", "incl": "30.79", "md": "1397.4", "tvd": "1332.8" } ]
[ { "comments": "Drilled 17 1/2\" section from 878 m to 1101 m MD. Base Utsira 1064,5 mMD. Drilling parameters : Flow 3450-4000 lpm / SPP 115-132 bar / WOB 0-12 MT / Torque 4-10 kNm / String RPM 40 / Bit RPM 104-160. ROP 25-100 m/hr, average ROP 37.2 m/ hrs. Pumped 10 m3 hi-vis sweep for every single drilled. Performed gMWD survey on connections. Up weight 138 MT / down weight 118 MT.\n\nSliding intervals: 878 - 888 m\n 918 - 928 m\n 958 - 973 m\n 999 - 1019 m\n 1039 - 1065 m\n 1079 - 1101 m\n", "dTimEnd": "2007-12-20T06:00:00+01:00", "dTimStart": "2007-12-20T00:00:00+01:00", "md": "1101", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled 17 1/2\" section from 1101 m to 1415 m MD. Top Skade 1225 mMD. Base Skade 1316 mMD.\nDrilling parameters : Flow 3500-4130 lpm / SPP 106-148 bar / WOB 1-10 MT / Torque 6-13 kNm / ECD 1.01 - 1.09 SG/ String RPM 40/Bit RPM 136-160. ROP 1-100 m/hr, average ROP 26.2 m/ hrs. Pumped 10 m3 hi-vis sweep for every single drilled. Performed gMWD survey on connections. Up weight 149 MT / down weight 123 MT.\n\nMax ECD in Skade 1.09 SG\n\nSurvey. Inc. Azi.\n1131.84 18.41 118.87\n1164.55 21.19 116.01\n1171.98 22.67 114.88\n1212.44 26.61 110.18\n1252.67 30.29 110.42\n1293.19 29.76 111.71\n1333.68 28.07 113.27", "dTimEnd": "2007-12-20T18:00:00+01:00", "dTimStart": "2007-12-20T06:00:00+01:00", "md": "1415", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "At TD. Pumped 30 m³ Hi-vis followed by 30 m³ sea water, followed by another 30 m³ of Hi-vis, at 3500 lpm while reciprocating drill string.", "dTimEnd": "2007-12-20T18:30:00+01:00", "dTimStart": "2007-12-20T18:00:00+01:00", "md": "1414", "phase": "fixed", "proprietaryCode": "drilling -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Displaced out pill with sea water 1 x BU, 3500 lpm 110 bars. Reciprocating the string.", "dTimEnd": "2007-12-20T19:30:00+01:00", "dTimStart": "2007-12-20T18:30:00+01:00", "md": "1414", "phase": "fixed", "proprietaryCode": "drilling -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Displaced hole to 1.40 SG at 3500-4500 lpm, SPP 170-230 bars.", "dTimEnd": "2007-12-20T20:45:00+01:00", "dTimStart": "2007-12-20T19:30:00+01:00", "md": "1414", "phase": "fixed", "proprietaryCode": "drilling -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with 17½\" BHA from 1415 m to 1123 m. Took weight of 20 MT overpull. RIH with two jnts. POOH with rotation on the string, passed obstruction with 5 MT overpull.", "dTimEnd": "2007-12-20T22:15:00+01:00", "dTimStart": "2007-12-20T20:45:00+01:00", "md": "1123", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued POOH with 17½\" BHA from 1123 m to 720 m. Tight spots at 796 m and 775 m, pulled through with 10 -15 MT overpull.", "dTimEnd": "2007-12-21T00:00:00+01:00", "dTimStart": "2007-12-20T22:15:00+01:00", "md": "720", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2007_12_22
NO 15/9-F-5
NO 15/9-F-5
name
2007-12-21T00:00:00+01:00
2007-12-22T00:00:00+01:00
normal
2018-05-03T13:53:00+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2007-12-22T00:00:00+01:00", "dTimDiaHoleStart": "2007-12-18T02:30:00+01:00", "diaHole": "17.5", "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "RIH and install the 18 3/4\" Well Head and cement same. Release landing string and POOH and lay out same. Prepare and skid Cantiler over F-15. ", "hpht": "0", "md": "1415", "mdCsgLast": "1404.7", "mdDiaHoleStart": "226", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "0", "presTestType": null, "reportNo": "9", "ropCurrent": "-999.99", "strengthForm": "0", "sum24Hr": "Racked back the 17½\" BHA. Rigged up the 13 3/8\" casing handling equipment and FAC tool. RIH with 13 3/8\" casing from to 1250 m, filling every casing joint. Started changing to 5½\" handling equipment.", "tightWell": "0", "tvd": "1346", "tvdCsgLast": "1340.3", "tvdStrengthForm": "0", "waterDepth": "91", "wellheadElevation": "0" } ]
[ { "dTim": "2007-12-21T19:00:00+01:00", "density": "1.4", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "1415", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "132", "yp": "-999.99" }, { "dTim": "2007-12-21T15:00:00+01:00", "density": "1.05", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "1322", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "139", "yp": "-999.99" } ]
[ { "dTim": "2007-12-22T00:00:00+01:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[]
[ { "comments": "Continued POOH with 17½\" BHA from 720 m to 122 m. Tight spots at 519 m and 481 m, pulled through with 10 -15 MT overpull.", "dTimEnd": "2007-12-21T02:30:00+01:00", "dTimStart": "2007-12-21T00:00:00+01:00", "md": "196", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed PS-21 slip and installed master bushing. Held tool box take prior to handling the 17½\" BHA.", "dTimEnd": "2007-12-21T03:15:00+01:00", "dTimStart": "2007-12-21T02:30:00+01:00", "md": "122", "phase": "fixed", "proprietaryCode": "drilling -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up to TDS and displaced string to sea water.", "dTimEnd": "2007-12-21T03:45:00+01:00", "dTimStart": "2007-12-21T03:15:00+01:00", "md": "122", "phase": "fixed", "proprietaryCode": "drilling -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued POOH BHA from 122 m to 35 m.", "dTimEnd": "2007-12-21T05:00:00+01:00", "dTimStart": "2007-12-21T03:45:00+01:00", "md": "35", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Prepared for racking back the UBHO.", "dTimEnd": "2007-12-21T06:00:00+01:00", "dTimStart": "2007-12-21T05:00:00+01:00", "md": "35", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Racked back the 17½\" BHA.\n", "dTimEnd": "2007-12-21T07:00:00+01:00", "dTimStart": "2007-12-21T06:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cleaned and cleared the rig floor.\n", "dTimEnd": "2007-12-21T07:15:00+01:00", "dTimStart": "2007-12-21T07:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to rig up 13 3/8\" casing handling equipment.\n", "dTimEnd": "2007-12-21T07:30:00+01:00", "dTimStart": "2007-12-21T07:15:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged down the 5½\" handling equipment. Rigged up the 13 3/8\" casing handling equipment and FAC tool and function tested same. Meanwhile moved the CTS funnel from F-5 to F-15.\n", "dTimEnd": "2007-12-21T11:15:00+01:00", "dTimStart": "2007-12-21T07:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to run in hole with 13 3/8\" casing.\n", "dTimEnd": "2007-12-21T11:45:00+01:00", "dTimStart": "2007-12-21T11:15:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up shoe, intermediate and float collar and Baker locked same. Confirmed float OK.\n", "dTimEnd": "2007-12-21T13:15:00+01:00", "dTimStart": "2007-12-21T11:45:00+01:00", "md": "27", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 13 3/8\" casing from 27 m to 819 m, filling every casing joint.", "dTimEnd": "2007-12-22T00:00:00+01:00", "dTimStart": "2007-12-21T13:15:00+01:00", "md": "819", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2007_12_23
NO 15/9-F-5
NO 15/9-F-5
name
2007-12-22T00:00:00+01:00
2007-12-23T00:00:00+01:00
normal
2018-05-03T13:53:00+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2007-12-23T00:00:00+01:00", "dTimDiaHoleStart": "2007-12-18T02:30:00+01:00", "diaHole": "17.5", "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Drill 26\" hole in F-15 Y1.", "hpht": "0", "md": "1415", "mdCsgLast": "1404.7", "mdDiaHoleStart": "226", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "0", "presTestType": null, "reportNo": "10", "ropCurrent": "-999.99", "strengthForm": "0", "sum24Hr": "RIH with 13 3/8\" casing to 1404,7 m. Installed 18 3/8\" WH. Cemented casing. Laid out landing string. ", "tightWell": "0", "tvd": "1346", "tvdCsgLast": "1340.3", "tvdStrengthForm": "0", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2007-12-22T19:00:00+01:00", "density": "1.4", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "1415", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "132", "yp": "-999.99" }, { "dTim": "2007-12-22T15:00:00+01:00", "density": "1.05", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "1322", "mudClass": "water based", "presBopRating": "0", "pv": "-999.99", "tempHthp": null, "type": "Spud Mud", "visFunnel": "139", "yp": "-999.99" } ]
[ { "dTim": "2007-12-23T00:00:00+01:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[]
[ { "comments": "Continued RIH with 13 3/8\" casing from 819 m to 1250 m, filling every casing joint.", "dTimEnd": "2007-12-22T04:45:00+01:00", "dTimStart": "2007-12-22T00:00:00+01:00", "md": "1250", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to change surface handling equipment and picking up the 18 3/4\" Well Head.", "dTimEnd": "2007-12-22T05:00:00+01:00", "dTimStart": "2007-12-22T04:45:00+01:00", "md": "1250", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Changing to 5½\" handling equipment.", "dTimEnd": "2007-12-22T06:00:00+01:00", "dTimStart": "2007-12-22T05:00:00+01:00", "md": "1250", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged up 5½\" handling equipment.\n", "dTimEnd": "2007-12-22T07:00:00+01:00", "dTimStart": "2007-12-22T06:00:00+01:00", "md": "1250", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to pick up CART.\n", "dTimEnd": "2007-12-22T07:15:00+01:00", "dTimStart": "2007-12-22T07:00:00+01:00", "md": "1250", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up 18 3/4\" WH housing/CART assembly. Made up to 13 3/8\" casing. \n", "dTimEnd": "2007-12-22T07:45:00+01:00", "dTimStart": "2007-12-22T07:15:00+01:00", "md": "1250", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged down casing tong and PS-30 13 3/8\" slips. Cleared rig floor.\n", "dTimEnd": "2007-12-22T08:45:00+01:00", "dTimStart": "2007-12-22T07:45:00+01:00", "md": "1250", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lowered CART below rotary, removed cap and filled up CART with sea water.\n", "dTimEnd": "2007-12-22T09:15:00+01:00", "dTimStart": "2007-12-22T08:45:00+01:00", "md": "1270", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to install the master bushing, and installed same.\n", "dTimEnd": "2007-12-22T10:00:00+01:00", "dTimStart": "2007-12-22T09:15:00+01:00", "md": "1270", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 5½\" HWDP landing string as per tally, picked up 2 x HWDP and cement head and made up same. Installed Lo-torque valve and cement hose. Up/down weight 180/125 MT. Landed 18 3/4\" WH into 30\" conductor by setting down casing string weight, plus 5 MT of landed string weight and engaged the lock ring. Performed over pull test to 25 MT. \n", "dTimEnd": "2007-12-22T12:00:00+01:00", "dTimStart": "2007-12-22T10:00:00+01:00", "md": "1404.7", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Established circulation in steps with SW through top drive to 2300 lpm 21 bars.\n", "dTimEnd": "2007-12-22T13:15:00+01:00", "dTimStart": "2007-12-22T12:00:00+01:00", "md": "1404.7", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Confirmed line up and leak tested line up to 200 bars 5 min.\n", "dTimEnd": "2007-12-22T13:30:00+01:00", "dTimStart": "2007-12-22T13:15:00+01:00", "md": "1404.7", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Mixed and pumped 161 m³ 1.52 sg lead at 1300 lpm / 24 bar followed by 20 m³ 1.92 sg tail slurry at 900 lpm / 34 bar. ROV observed returns only came up F-5. \nDisplaced and sheared wiper plug by pumping 3000 litres SW, plug sheared at pressure/volume: 132 bar/ 1200 ltr. Continued to displace cement with seawater at 3000 l/min using mud pumps. FCP 90 bars, bumped plug and applied 160 bars to plug. Pump efficiency : 95.4 %. Bled off pressure, 1500 litres bled back to the cement unit. Disconnected cement hose after pressure had been bled off.", "dTimEnd": "2007-12-22T17:45:00+01:00", "dTimStart": "2007-12-22T13:30:00+01:00", "md": "1404.7", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Reduced overpull on landing string to neutral. ROV observed CART. Released CART according to Vetco, 5 turns right hand.\n", "dTimEnd": "2007-12-22T18:00:00+01:00", "dTimStart": "2007-12-22T17:45:00+01:00", "md": "1404.7", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to lay out cement head. Removed cement hose and Lo-torque valve, broke out cement head. Dropped 2 sponge balls and flushed landing string.", "dTimEnd": "2007-12-22T19:30:00+01:00", "dTimStart": "2007-12-22T18:00:00+01:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with landing string and racked back same. Laid out CART.\n", "dTimEnd": "2007-12-22T20:00:00+01:00", "dTimStart": "2007-12-22T19:30:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed hatch covers on wellhead and moon pool.\n\nCONTINUED OPERATIONS ON WELL F-15 Y1\n", "dTimEnd": "2007-12-22T21:45:00+01:00", "dTimStart": "2007-12-22T20:00:00+01:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_07_11
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-10T00:00:00+02:00
2008-07-11T00:00:00+02:00
normal
2018-05-03T13:53:00+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-11T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-10T18:00:00+02:00", "diaHole": "17.5", "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Flush and function test TBC on rig floor. Wait for production to bean up F-14. Stop production on F-14 and F-12 for heavy lift. Run HPDR until tensioner joint.", "hpht": "0", "md": "1415", "mdCsgLast": "1404.7", "mdDiaHoleStart": "1415", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "0", "presTestType": null, "reportNo": "11", "ropCurrent": "-999.99", "strengthForm": "0", "sum24Hr": "Skidded rig from F-14 to F-5. RU to run HPDR. PU TBC and stress joint. ", "tightWell": "0", "tvd": "1346", "tvdCsgLast": "1340.3", "tvdStrengthForm": "0", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-10T23:59:00+02:00", "density": "1.37", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "1415", "mudClass": "oil based", "presBopRating": "0", "pv": "25", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "7.5" } ]
[ { "dTim": "2008-07-11T00:00:00+02:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[]
[ { "comments": "Cleaned and cleared rig floor of WL equipment. Held tool box meeting prior to skidding the cantiliver from F-14 to F-5. Prepared to skid rig. Started to skid rig to F-5.\n\nMeanwhile RU to pump through KWV on F-14.", "dTimEnd": "2008-07-10T19:45:00+02:00", "dTimStart": "2008-07-10T18:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued skidding cantiliver from F-14 to F-5. \nMeanwhile performed line test against KWV on F-14 30/345 bar 5/10 min. Equalized and opened HMV and DHSV by pressuring up to 67 bar using baseoil and cmt unit according to F-14 initial start up procedure.", "dTimEnd": "2008-07-10T21:15:00+02:00", "dTimStart": "2008-07-10T19:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued skidding cantiliver from F-14 to F-5. Had rig shut-down.", "dTimEnd": "2008-07-10T21:45:00+02:00", "dTimStart": "2008-07-10T21:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Changed burst disk in turbine cooling system and rectified problem. Re-sat all rig systems.", "dTimEnd": "2008-07-10T23:30:00+02:00", "dTimStart": "2008-07-10T21:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued skidding cantiliver from F-14 to F-5.", "dTimEnd": "2008-07-11T00:00:00+02:00", "dTimStart": "2008-07-10T23:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_07_12
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-11T00:00:00+02:00
2008-07-12T00:00:00+02:00
normal
2018-05-03T13:53:00+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-12T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-10T18:00:00+02:00", "diaHole": "17.5", "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "PU landing string, land TBC, lock and confirm with overpull. Install tensioner ring, boat collision stool and tensioner ring. Transfer tension. MU BOP joint with claxton tool. ", "hpht": "0", "md": "1415", "mdCsgLast": "1404.7", "mdDiaHoleStart": "1415", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "0", "presTestType": null, "reportNo": "12", "ropCurrent": "-999.99", "strengthForm": "0", "sum24Hr": "Flushed and function tested TBC on rig floor. Waited for production to bean up F-14. Stop production on F-14 and F-12 for heavy lift. Ran HPDR until tensioner joint.", "tightWell": "0", "tvd": "1346", "tvdCsgLast": "1340.3", "tvdStrengthForm": "0", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[]
[ { "dTim": "2008-07-12T00:00:00+02:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[]
[ { "comments": "Continued skidding cantiliver from F-14 to F-5. Skidded 3 m port and 2.25 m aft.", "dTimEnd": "2008-07-11T00:15:00+02:00", "dTimStart": "2008-07-11T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "moving -- skid", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed master bushings and installed safety guard. RU to install riser spider.", "dTimEnd": "2008-07-11T01:30:00+02:00", "dTimStart": "2008-07-11T00:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Equalized and opened HMV and DHSV by pressuring up to 63 bar using baseoil and cmt unit to start up on F-14 after shut-down.", "dTimEnd": "2008-07-11T02:15:00+02:00", "dTimStart": "2008-07-11T01:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to install riser spider. Function tested riser spider and installed hole cover. Installed and function tested BX-elevator.", "dTimEnd": "2008-07-11T03:00:00+02:00", "dTimStart": "2008-07-11T02:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box meeting prior to lifting TBC riser joint to drill floor. Installed Vetco equipment on rig floor. Lifted riser simultaniously with crane and TDS until it was vertical. Removed slings.\n", "dTimEnd": "2008-07-11T05:30:00+02:00", "dTimStart": "2008-07-11T03:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed protection from connector. Prepared to bring Vetco hot stabs from moonpool to rig floor to be able to function test TBC.", "dTimEnd": "2008-07-11T06:00:00+02:00", "dTimStart": "2008-07-11T05:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Flushed and function tested TBC.\n\nMeanwhile removed cradle and trolly from HTS. Removed special tool and dressed fox hole for MU 12 1/4\" BHA.", "dTimEnd": "2008-07-11T10:00:00+02:00", "dTimStart": "2008-07-11T06:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited on production to bean up F-14. \n\nMeanwhile:\n- lifted tension cylinders for F-9 to rig floor and placed them next to riser spider for easy acess when lifting them down to WH.\n- pressure tested standpipe manifolds\n- PU and MU drill collars from deck.\n", "dTimEnd": "2008-07-11T13:00:00+02:00", "dTimStart": "2008-07-11T10:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited on production to stop production on F-14 and F-12 for heavy lift. \n\nMeanwhile continued PU and MU drill collars from deck and pressure testing standpipe manifolds.\n", "dTimEnd": "2008-07-11T14:45:00+02:00", "dTimStart": "2008-07-11T13:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed hatches on F-5 and F-10. Lowered tension cylinders for F-9 through rotary down to WH and retrieved actuator for F-14.", "dTimEnd": "2008-07-11T16:30:00+02:00", "dTimStart": "2008-07-11T14:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed tension deck hatches from F-5 and F-10. RU guide line tuggers in moonpool.\n\nMeanwhile re-instated cradle and trolly to HTS for riser handling.", "dTimEnd": "2008-07-11T19:00:00+02:00", "dTimStart": "2008-07-11T16:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk with night crew. PU and ran HPDR doubles from surface to 50 m. Removed lifting sub on HPDR in riser spider and MU flange connection. Installed protection caps on flange nuts using Bandak tool. Tested flanges to 3000 psi/5 min. Installed fairings around flanges. Verified that tension ring was in place on top of the centralizer deck opening.\n\nMeanwhile installed guide wires at template using ROV.", "dTimEnd": "2008-07-12T00:00:00+02:00", "dTimStart": "2008-07-11T19:00:00+02:00", "md": "50", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_07_13
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-12T00:00:00+02:00
2008-07-13T00:00:00+02:00
normal
2018-05-03T13:53:00+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-13T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-10T18:00:00+02:00", "diaHole": "17.5", "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "NU BOP/diverter and pressure test BOP/diverter/connector/20\" csg. MU and RIH with 12 1/4\" BHA. RIH with 12 1/4\" BHA on 5 1/2\" DP to 1370 m MDRT.", "hpht": "0", "md": "1415", "mdCsgLast": "1404.7", "mdDiaHoleStart": "1415", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "0", "presTestType": null, "reportNo": "13", "ropCurrent": "-999.99", "strengthForm": "0", "sum24Hr": "PU landing string, landed TBC, locked and confirmed with overpull. Started production on F-12. Installed centralizers, tensioner ring and boat collision stool. Transfered tension from TDS to tension cylinders. Installed half-moon hatch on F-5. Erected scaffolding tower around Claxton tool. Integrity tested HPDR 20/195 bar for 5/10 min. Ok. Disconnected and LD Claxton tool and landing string. Started to NU BOP/diverter.", "tightWell": "0", "tvd": "1346", "tvdCsgLast": "1340.3", "tvdStrengthForm": "0", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-12T02:00:00+02:00", "density": "1.33", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "oil based", "presBopRating": "0", "pv": "26", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "3" } ]
[ { "dTim": "2008-07-13T00:00:00+02:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[]
[ { "comments": "Continued to PU and run HPDR doubles from 50 to 103 m. Removed lifting sub on HPDR in riser spider and MU flange connection. Installed protection caps on flange nuts using Bandak tool. Tested flanges to 3000 psi/5 min. Installed fairings around flanges. \n\nMeanwhile leak tested kill manifold 30/345 bar for 5/10 min and choke/kill manifold 30/345 bar for 5/10 min.", "dTimEnd": "2008-07-12T06:00:00+02:00", "dTimStart": "2008-07-12T00:00:00+02:00", "md": "103", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to MU flange connection. Installed protection caps on flange nuts using Bandak tool. Tested flanges to 3000 psi/5 min. Installed fairings around flanges. PU riser string using TDS and RD riser spider. Lowered HPDR so that Claxton tool was below rotary and installed outer ring and master bushings. PU and MU one std of 5 1/2\" DP.\n", "dTimEnd": "2008-07-12T09:00:00+02:00", "dTimStart": "2008-07-12T06:00:00+02:00", "md": "127", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with HPDR from 127 m to just over connector at 138 m. Entered guide funnel. Removed guide funnel from well head. Turned riser clockwise until hot stab was oriented in the right direction. Landed TBC on WH with 15 MT. Launched hot stab and locked connector onto WH. Applied 10 MT overpull on riser to confirm H4-MUSL connector.", "dTimEnd": "2008-07-12T11:45:00+02:00", "dTimStart": "2008-07-12T09:00:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed centralisers, tension ring and boat collison stool.\n\nMeanwhile performed line test on kill line to F-12 to 30/200 bar for 5/10 min. Equalized and opened F-12 DHSV.", "dTimEnd": "2008-07-12T14:00:00+02:00", "dTimStart": "2008-07-12T11:45:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Retrieved hot stab on TBC and replaced with dummy. Retrieved guide wires from template.", "dTimEnd": "2008-07-12T15:30:00+02:00", "dTimStart": "2008-07-12T14:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Re-installed hatch on F-10.", "dTimEnd": "2008-07-12T16:30:00+02:00", "dTimStart": "2008-07-12T15:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Attempted to install half-moon hatches on F-5 around BOP joint. Removed master bushings and retracted blocks to line up hatches without sucess.", "dTimEnd": "2008-07-12T19:00:00+02:00", "dTimStart": "2008-07-12T16:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rig shut down due to production. Meanwhile held tool box talk prior to pressuring up tension cylinders.", "dTimEnd": "2008-07-12T19:15:00+02:00", "dTimStart": "2008-07-12T19:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited for production operator to transfer weight from HPDR to tension cylinders.\n\nMeanwhile carried out housekeeping on centralizer deck.", "dTimEnd": "2008-07-12T20:00:00+02:00", "dTimStart": "2008-07-12T19:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Released tension on TDS and adjusted pressure on tension cylinders to 37 bar.", "dTimEnd": "2008-07-12T20:15:00+02:00", "dTimStart": "2008-07-12T20:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed half-moon hatch cover on F-5. Erected 3 m scaffolding tower around Claxton tool in moonpool to be able to insert Veco 1502 Male cap.\n\nMeanwhile pressured up to 90 bars on all 4 tension cylinders to obtain riser tension of 150 MT. Held tool box talk prior to equalizing DHSV on F-14.", "dTimEnd": "2008-07-12T22:30:00+02:00", "dTimStart": "2008-07-12T20:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to erect scaffolding tower around Claxton tool in moonpool to be able to insert Veco 1502 Male cap.\n\nMeanwhile equalized and opened DHSV by pressuring up to 88 bar using baseoil and cmt unit to start up production on F-14.", "dTimEnd": "2008-07-12T23:45:00+02:00", "dTimStart": "2008-07-12T22:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to erect scaffolding tower around Claxton tool in moonpool to be able to insert Veco 1502 Male cap.", "dTimEnd": "2008-07-13T00:00:00+02:00", "dTimStart": "2008-07-12T23:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_07_14
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-13T00:00:00+02:00
2008-07-14T00:00:00+02:00
normal
2018-05-03T13:53:00+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-14T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-10T18:00:00+02:00", "diaHole": "17.5", "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Continue MU and RIH with 12 1/4\" BHA from 92 m to 140 m. RIH with 12 1/4\" BHA on 5 1/2\" DP from 140 m to 1340 m MDRT. Perform cut & slip. Drill shoe track and displace to 1.35 sg OBM.", "hpht": "0", "md": "1415", "mdCsgLast": "1404.7", "mdDiaHoleStart": "1415", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "0", "presTestType": null, "reportNo": "14", "ropCurrent": "-999.99", "strengthForm": "0", "sum24Hr": "NU BOP/diverter and pressure tested BOP/diverter/connector to 345 bar/10 min. Ok. Serviced and tested TDS. MU and RIH with 12 1/4\" BHA from surface to 92 m. Rig shut down at 5:45 hrs.", "tightWell": "0", "tvd": "1346", "tvdCsgLast": "1340.3", "tvdStrengthForm": "0", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-13T02:00:00+02:00", "density": "1.33", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "oil based", "presBopRating": "0", "pv": "26", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "3" } ]
[ { "dTim": "2008-07-14T00:00:00+02:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[]
[ { "comments": "Continued to erect scaffolding tower around Claxton tool in moonpool to be able to insert Veco 1502 Male cap.", "dTimEnd": "2008-07-13T00:15:00+02:00", "dTimStart": "2008-07-13T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Filled riser with 8.7 m3 SW and installed Veco 1502 Male cap.", "dTimEnd": "2008-07-13T01:00:00+02:00", "dTimStart": "2008-07-13T00:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RU and performed integrity test of riser system through TDS and Claxton tool using cmt unit. Leak tested HPDR/well to 20/195 bar for 5/10 min. Ok. Pumped 1275 ltrs at 700 lpm and bled back 1200 ltrs.", "dTimEnd": "2008-07-13T02:15:00+02:00", "dTimStart": "2008-07-13T01:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Disconnected Claxton tool. Could not RB std of 5 1/2\" DP due to PRS not working.\n\nMeanwhile carried out maintenance on FWD iron-roughneck and prepared 12 1/4\" BHA.", "dTimEnd": "2008-07-13T03:00:00+02:00", "dTimStart": "2008-07-13T02:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Re-sat AFT PRS after shut-down.", "dTimEnd": "2008-07-13T03:30:00+02:00", "dTimStart": "2008-07-13T03:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "RB std of 5 1/2\" DP and removed Claxton tool from rig floor. Re-installed master bushings.", "dTimEnd": "2008-07-13T04:00:00+02:00", "dTimStart": "2008-07-13T03:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to nipple up BOP/diverter. Moved BOP to top of HPDR and started to nipple up BOP.\n\nMeanwhile pressure tested 5 1/2\" TIW and grey valve to 30/345 bar for 5/10 min.", "dTimEnd": "2008-07-13T06:00:00+02:00", "dTimStart": "2008-07-13T04:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to nipple up BOP and focused on tools aloft. Moved BOP to top of HPDR and started to nipple up BOP onto NT2 connector. Installed slick joint.", "dTimEnd": "2008-07-13T11:45:00+02:00", "dTimStart": "2008-07-13T06:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed overshot and diverter. POOH and LO diverter RT. Removed diverter inserts and installed outer ring and master bushings. Cleared rig floor of excess equipment. Meanwhile flogged bolts on slick joint.", "dTimEnd": "2008-07-13T15:30:00+02:00", "dTimStart": "2008-07-13T11:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Filled riser with SW using cmt unit and held tool box talk prior to MU test plug assembly. Had problem with BX-elevators.", "dTimEnd": "2008-07-13T16:00:00+02:00", "dTimStart": "2008-07-13T15:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop activities", "state": "ok", "stateDetailActivity": "success" }, { "comments": "BX-elevator would not close. Changed out rental elevators for rig elevators.", "dTimEnd": "2008-07-13T17:00:00+02:00", "dTimStart": "2008-07-13T16:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Checked dies on PRS prior to PU 5 1/2\" DP. PU and MU BOP test plug assembly. RIH with BOP test plug on 5 1/2\" DP from surface to 139.4 m.", "dTimEnd": "2008-07-13T19:30:00+02:00", "dTimStart": "2008-07-13T17:00:00+02:00", "md": "139.4", "phase": "fixed", "proprietaryCode": "drilling -- bop activities", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up and pressure tested NT2 connector / riser to 30/345 bar for 5/10 min. Ok. Lined up and pressure tested lower IBOP, upper IBOP and kelly hose to 30/345 bar for 5/10 min. Ok. Performed accumulator test.\n\nMeanwhile serviced both FWD and AFT PRS. Serviced and inspected TDS.", "dTimEnd": "2008-07-14T00:00:00+02:00", "dTimStart": "2008-07-13T19:30:00+02:00", "md": "139.4", "phase": "fixed", "proprietaryCode": "drilling -- bop activities", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_07_15
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-14T00:00:00+02:00
2008-07-15T00:00:00+02:00
normal
2018-05-03T13:53:00+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-15T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-10T18:00:00+02:00", "diaHole": "17.5", "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Continue drilling shoe track on 12 1/4\" section. Drill 3 m new formation and take FIT. Drill 12 1/4\" hole section from 1408 m to 1800 m MD.", "hpht": "0", "md": "1415", "mdCsgLast": "1404.7", "mdDiaHoleStart": "1415", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "0", "presTestType": null, "reportNo": "15", "ropCurrent": "-999.99", "strengthForm": "0", "sum24Hr": "Continued MU and RIH with 12 1/4\" BHA from 92 m to 140 m. RIH with 12 1/4\" BHA on 5 1/2\" DP from 140 m to 1307 m MDRT. Performed cut & slip. Opened ASV and checked status on burst disk on F-14. Washed down and tagged cement at 1376.5 m MD. Drilled on cement plug/float and displaced to 1.35 sg OBM.", "tightWell": "0", "tvd": "1346", "tvdCsgLast": "1340.3", "tvdStrengthForm": "0", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-14T02:00:00+02:00", "density": "1.33", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "oil based", "presBopRating": "0", "pv": "26", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "3" } ]
[ { "dTim": "2008-07-15T00:00:00+02:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[]
[ { "comments": "RD and LO BOP test plug assembly. Function tested shear rams and recorded parameters.\n\nMeanwhile cleaned and cleared drill floor.", "dTimEnd": "2008-07-14T02:15:00+02:00", "dTimStart": "2008-07-14T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop activities", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk with focus on manual handling of BHA. PU and MU 12 1/4\" BHA from surface to 92 m.", "dTimEnd": "2008-07-14T05:45:00+02:00", "dTimStart": "2008-07-14T02:15:00+02:00", "md": "92", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rig shut down. Waiting on production to free electrican to re-set drill floor equipment.", "dTimEnd": "2008-07-14T06:00:00+02:00", "dTimStart": "2008-07-14T05:45:00+02:00", "md": "92", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waiting on production to free electrican to re-set drill floor equipment.", "dTimEnd": "2008-07-14T07:00:00+02:00", "dTimStart": "2008-07-14T06:00:00+02:00", "md": "92", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk with focus on manual handling of BHA. PU and MU 12 1/4\" BHA from 92 m to 140 m.", "dTimEnd": "2008-07-14T07:45:00+02:00", "dTimStart": "2008-07-14T07:00:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box meeting prior to equalizing and opening HMV on F-14.", "dTimEnd": "2008-07-14T08:00:00+02:00", "dTimStart": "2008-07-14T07:45:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "interruption -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 12 1/4\" BHA on 5 1/2\" DP from 140 m to 180 m. Broke off liner XO on btm of 5 1/2\" DP std. Removed master bushings and installed PS21 slips. Continued to RIH with 12 1/4\" BHA on 5 1/2\" DP from 180 m to 987 m filling every 10 stds. \n\nMeanwhile equalized and opened HMV on F-14.", "dTimEnd": "2008-07-14T10:45:00+02:00", "dTimStart": "2008-07-14T08:00:00+02:00", "md": "987", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "MU TDS and tested MWD tools at 2400 lpm / 48 bar. Removed PS21 slips and installed master bushings. Installed TIW.", "dTimEnd": "2008-07-14T11:45:00+02:00", "dTimStart": "2008-07-14T10:45:00+02:00", "md": "987", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed slip and cut.", "dTimEnd": "2008-07-14T14:45:00+02:00", "dTimStart": "2008-07-14T11:45:00+02:00", "md": "987", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to perform slip and cut.", "dTimEnd": "2008-07-14T15:15:00+02:00", "dTimStart": "2008-07-14T14:45:00+02:00", "md": "987", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed TIW and master bushings. Installed PS21 slips. RIH with 12 1/4\" BHA on 5 1/2\" DP from 987 m to 1307 m.", "dTimEnd": "2008-07-14T16:45:00+02:00", "dTimStart": "2008-07-14T15:15:00+02:00", "md": "1307", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "MU TDS and performed choke drill. Operation transfered to F-99.", "dTimEnd": "2008-07-14T17:30:00+02:00", "dTimStart": "2008-07-14T16:45:00+02:00", "md": "1307", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Perform choke drill.", "dTimEnd": "2008-07-15T00:00:00+02:00", "dTimStart": "2008-07-14T23:30:00+02:00", "md": "1307", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_07_16
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-15T00:00:00+02:00
2008-07-16T00:00:00+02:00
normal
2018-05-03T13:53:00+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-16T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-15T18:30:00+02:00", "diaHole": "12.25", "diaPilot": null, "distDrill": "107", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Drill 12 1/4\" hole section from 1653 m to 2400 m MD", "hpht": "0", "md": "1522", "mdCsgLast": "1404.7", "mdDiaHoleStart": "1418", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "1415", "presTestType": "formation integrity test", "reportNo": "16", "ropCurrent": "-999.99", "strengthForm": "1.6", "sum24Hr": "Continued drilling shoe track/float in 12 1/4\" section. Drilled 3 m new formation and took FIT. Drilled 12 1/4\" hole section from 1415 m to 1653 m MD.", "tightWell": "0", "tvd": "1438.6", "tvdCsgLast": "1340.3", "tvdStrengthForm": "1346", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-15T22:00:00+02:00", "density": "1.35", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "1519", "mudClass": "oil based", "presBopRating": "0", "pv": "29", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "10" }, { "dTim": "2008-07-15T02:00:00+02:00", "density": "1.33", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "-999.99", "mudClass": "oil based", "presBopRating": "0", "pv": "24", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "9" }, { "dTim": "2008-07-15T13:00:00+02:00", "density": "1.35", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "1404", "mudClass": "oil based", "presBopRating": "0", "pv": "29", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "10.5" } ]
[ { "dTim": "2008-07-16T00:00:00+02:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[ { "azi": "114.02", "dTim": "2008-07-16T00:00:00+02:00", "incl": "31.63", "md": "1496.7", "tvd": "1417.8" }, { "azi": "113.32", "dTim": "2008-07-16T00:00:00+02:00", "incl": "31.62", "md": "1538.4", "tvd": "1453.3" }, { "azi": "110.43", "dTim": "2008-07-16T00:00:00+02:00", "incl": "32.72", "md": "1578.1", "tvd": "1487" }, { "azi": "107.71", "dTim": "2008-07-16T00:00:00+02:00", "incl": "33.5", "md": "1618.4", "tvd": "1520.7" }, { "azi": "114.7", "dTim": "2008-07-16T00:00:00+02:00", "incl": "31", "md": "1457.1", "tvd": "1384" } ]
[ { "comments": "Continued to RIH with 12 1/4\" BHA on 5 1/2\" DP from 1307 m to 1351 m. Down weight 108 MT. Held tool box talk prior to displacing well to 1.35 sg OBM.\n\nMade up TDS and broke circulation. Washed down from 1351 m at 2300 lpm / SPP 43 bar and tagged cement plug at 1376,5 m MD.", "dTimEnd": "2008-07-15T01:30:00+02:00", "dTimStart": "2008-07-15T00:00:00+02:00", "md": "1376.5", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled on cement plug/float at 1376,5 m MD and displaced to 1.35 sg OBM. Drilling parameters : Flow 2800 lpm / SPP 114 bar / String RPM 20-30 / WOB 4-5 MT / Torque 8-10 kNm / ECD 1.36. Picked off bottom every 10-15 min to clean bit. \n\nMeanwhile MU and RB 10 3/4\" csg. stds.\n", "dTimEnd": "2008-07-15T02:45:00+02:00", "dTimStart": "2008-07-15T01:30:00+02:00", "md": "1376.5", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled on cement plug/float at 1376,5 m MD. Drilling parameters : Flow 2800 lpm / SPP 114 bar / String RPM 20-30 / WOB 5-10 MT / Torque 8-12 kNm / ECD 1.36. Picked off bottom every 10-15 min to clean bit. \n\nMeanwhile MU and RB 10 3/4\" csg. stds. A total of 3 stds 10 3/4\" csg RB in derrick.", "dTimEnd": "2008-07-15T06:00:00+02:00", "dTimStart": "2008-07-15T02:45:00+02:00", "md": "1376.5", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled on cement plug/float at 1376,5 m MD. Drilling parameters : Flow 2800 lpm / SPP 111 bar / String RPM 40-70 / WOB 1-11 MT / Torque 2-20 kNm / ECD 1.36 sg EMW. Picked off bottom every 10-15 min to clean bit. \n\nMeanwhile MU and RB 10 3/4\" csg. stds.", "dTimEnd": "2008-07-15T11:00:00+02:00", "dTimStart": "2008-07-15T06:00:00+02:00", "md": "1376.5", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled out shoe track from 1376.5 m to 1415 m MD. Drilling parameters : Flow 2800 lpm / SPP 112 bar / String RPM 70 / WOB 2-6 MT / Torque 9-20 kNm / ECD 1.36 sg EMW. Reamed through shoe every 2 m drilled.\n\nMeanwhile MU and RB 10 3/4\" csg. stds.", "dTimEnd": "2008-07-15T15:00:00+02:00", "dTimStart": "2008-07-15T11:00:00+02:00", "md": "1415", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled 3 m new formation in 12 1/4\" hole section from 1415 m to 1418 m MD. Drilling parameters : Flow 2800 lpm / SPP 112 bar / String RPM 70 / WOB 2 MT / Torque 9-10 kNm / ECD 1.36 sg EMW. \n\nMeanwhile MU and RB 10 3/4\" csg. stds.", "dTimEnd": "2008-07-15T15:30:00+02:00", "dTimStart": "2008-07-15T15:00:00+02:00", "md": "1418", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Spotted 5 m3 LCM pill in open hole/TD; Flow 2800 lpm / SPP 112 bar / String RPM 10 / Torque 9 kNm. Reduced flow to 1600 lpm going through MWD tools. Circulated and POOH until bit just below 13 3/8\" csg shoe; Flow 2800 lpm / SPP 112 bar / String RPM 10 / Torque 9 kNm. \n\nMeanwhile held toolbox prior to performing FIT and MU and RB 10 3/4\" csg. stds.", "dTimEnd": "2008-07-15T16:15:00+02:00", "dTimStart": "2008-07-15T15:30:00+02:00", "md": "1415", "phase": "fixed", "proprietaryCode": "formation evaluation -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Closed BOP and lined up to perform FIT. Performed line test to 100 bar / 5 min against IBOP and Kill HCR. Performed FIT and pressured up at 50 lpm to 33 bar (36 bar on cmt unit) using 298 ltrs SW. Bled back 230 ltrs. \n\nMeanwhile MU and RB 10 3/4\" csg. stds.", "dTimEnd": "2008-07-15T17:45:00+02:00", "dTimStart": "2008-07-15T16:15:00+02:00", "md": "1415", "phase": "fixed", "proprietaryCode": "formation evaluation -- rft/fit", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Filled trip tanks with 1.35 sg OBM and displaced choke and kill manifolds to mud.\n\nMeanwhile MU and RB 10 3/4\" csg. stds. A total of 12 stds 10 3/4\" csg RB in derrick.", "dTimEnd": "2008-07-15T18:30:00+02:00", "dTimStart": "2008-07-15T17:45:00+02:00", "md": "1415", "phase": "fixed", "proprietaryCode": "drilling -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Established parameteres and started drilling 12 1/4\" hole section from 1418 m to 1522 m MD. Drilling parameters : Flow 3250-3300 lpm / SPP 153-159 bar / String RPM 120 / WOB 2-4 MT / Torque 11-15 kNm / ECD 1.37 sg EMW / ROP 30-50 m/hr. \n\nMeanwhile MU and RB 9 5/8\" csg. stds.", "dTimEnd": "2008-07-16T00:00:00+02:00", "dTimStart": "2008-07-15T18:30:00+02:00", "md": "1522", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_07_17
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-16T00:00:00+02:00
2008-07-17T00:00:00+02:00
normal
2018-05-03T13:53:00+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-17T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-15T18:30:00+02:00", "diaHole": "12.25", "diaPilot": null, "distDrill": "334", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Wait with BHA inside 13 3/8\" csg until drill flor is clear from exhaust fumes. RIH with 12 1/4\" BHA to 1895 m and drill 12 1/4\" hole section from 1895 m to 2300 m MD.", "hpht": "0", "md": "1886", "mdCsgLast": "1404.7", "mdDiaHoleStart": "1418", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "1415", "presTestType": "formation integrity test", "reportNo": "17", "ropCurrent": "-999.99", "strengthForm": "1.6", "sum24Hr": "Drilled 12 1/4\" hole section from 1653 m to 1895 m MD and sorted out problems with mill pump and slurry system. RECORDED ON F-99: Circulated hole clean, flow checked and POOH with 12 1/4\" BHA from 1884 m to inside 13 3/8\" csg shoe at 1381 m due to exhaust fumes on drill floor. Circulated inside 13 3/8\" csg shoe to keep MWD batteries alive.", "tightWell": "0", "tvd": "1741", "tvdCsgLast": "1340.3", "tvdStrengthForm": "1346", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-16T04:00:00+02:00", "density": "1.34", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "1613", "mudClass": "oil based", "presBopRating": "0", "pv": "22", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "20" }, { "dTim": "2008-07-16T11:00:00+02:00", "density": "1.35", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "1750", "mudClass": "oil based", "presBopRating": "0", "pv": "28", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "16" }, { "dTim": "2008-07-16T21:30:00+02:00", "density": "1.35", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "1835", "mudClass": "oil based", "presBopRating": "0", "pv": "28", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "16" } ]
[ { "dTim": "2008-07-17T00:00:00+02:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[ { "azi": "102.78", "dTim": "2008-07-17T00:00:00+02:00", "incl": "34.8", "md": "1699.7", "tvd": "1588" }, { "azi": "101.4", "dTim": "2008-07-17T00:00:00+02:00", "incl": "35.74", "md": "1739.5", "tvd": "1620.5" }, { "azi": "103.57", "dTim": "2008-07-17T00:00:00+02:00", "incl": "35.57", "md": "1778.9", "tvd": "1652.5" }, { "azi": "106.1", "dTim": "2008-07-17T00:00:00+02:00", "incl": "35.63", "md": "1820.4", "tvd": "1686.3" }, { "azi": "107.95", "dTim": "2008-07-17T00:00:00+02:00", "incl": "35.61", "md": "1860.9", "tvd": "1719.2" }, { "azi": "105.53", "dTim": "2008-07-17T00:00:00+02:00", "incl": "34.09", "md": "1658.2", "tvd": "1553.8" } ]
[ { "comments": "Drilled 12 1/4\" hole section from 1522 m to 1653 m MD. Drilling parameters : Flow 3300-3500 lpm / SPP 159-179 bar / String RPM 120 / WOB 2-4 MT / Torque 13-17 kNm / ECD 1.37-1.38 sg EMW / Drilled with limited ROP 20-40 m/hr due to problems transfering slurry from milling tank through active tank to holding tank. \n\nMeanwhile MU and RB 9 5/8\" csg. stds. A total of 14 stds 9 5/8\" csg RB in derrick.", "dTimEnd": "2008-07-16T06:00:00+02:00", "dTimStart": "2008-07-16T00:00:00+02:00", "md": "1653", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled 12 1/4\" hole section from 1653 m to 1672 m MD. Drilling parameters : Flow 3500 lpm / SPP 179 bar / String RPM 120 / WOB 2-4 MT / Torque 13-17 kNm / ECD 1.38 sg EMW / Drilled with limited ROP 20-40 m/hr due to problems transfering slurry from milling tank through active tank to holding tank. Stopped drilling to investigate TDS.\n\nMeanwhile MU and RB 9 5/8\" csg. stds.", "dTimEnd": "2008-07-16T06:45:00+02:00", "dTimStart": "2008-07-16T06:00:00+02:00", "md": "1672", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Investigated leak in TDS. Found small leak on lower side of washpipe. Decided to continue operation and keep observing TDS.\n\nMeanwhile MU and RB 9 5/8\" csg. stds.", "dTimEnd": "2008-07-16T07:15:00+02:00", "dTimStart": "2008-07-16T06:45:00+02:00", "md": "1672", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Drilled 12 1/4\" hole section from 1672 m to 1793 m MD. Drilling parameters : Flow 3500 lpm / SPP 172-174 bar / String RPM 120-150 / WOB 3-4 MT / Torque 12-19 kNm / ECD 1.37-1.38 sg EMW. Unable to drill on because holding tank was full (unable to inject slurry because it did not meet viscosity requirement) and cuttings screw going to skip clogged up.\n\nMeanwhile MU and RB 9 5/8\" csg. stds.", "dTimEnd": "2008-07-16T12:00:00+02:00", "dTimStart": "2008-07-16T07:15:00+02:00", "md": "1793", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Circulated while reciprocating drill string; Circulation parameters : Flow 2800 lpm / SPP 117 bar / String RPM 50 / Torque 8-12 kNm / ECD 1.36 sg EMW due to problems with mill pump and slurry system. \n\nMeanwhile MU and RB 9 5/8\" csg. stds.", "dTimEnd": "2008-07-16T15:30:00+02:00", "dTimStart": "2008-07-16T12:00:00+02:00", "md": "1793", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Drilled 12 1/4\" hole section from 1793 m to 1862 m MD. Drilling parameters : Flow 3500 lpm / SPP 176 bar / String RPM 150 / WOB 3-6 MT / Torque 12-20 kNm / ECD 1.38 sg EMW. Unable to drill on due to line from shaker to mill tank, line from mill tank to active tank and cuttings screw going to skip clogged up.\n\nMeanwhile MU and RB 9 5/8\" csg. stds.\n", "dTimEnd": "2008-07-16T18:00:00+02:00", "dTimStart": "2008-07-16T15:30:00+02:00", "md": "1862", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Circulated while reciprocating drill string; Circulation parameters : Flow 1000-2000 lpm / SPP 22-30 bar / String RPM 50 / Torque 5-9 kNm / ECD 1.37 sg EMW due to problems with mill pump and slurry system. \n\nMeanwhile MU and RB 9 5/8\" csg. stds.", "dTimEnd": "2008-07-16T22:30:00+02:00", "dTimStart": "2008-07-16T18:00:00+02:00", "md": "1862", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Drilled 12 1/4\" hole section from 1862 m to 1886 m MD. Drilling parameters : Flow 3500 lpm / SPP 184 bar / String RPM 150 / WOB 1-3 MT / Torque 9-17 kNm / ECD 1.38 sg EMW. Drilled with limited ROP 20 m/hr to observe proper operation of mill pump and slurry system.\n\nMeanwhile MU and RB 9 5/8\" csg. stds.", "dTimEnd": "2008-07-17T00:00:00+02:00", "dTimStart": "2008-07-16T22:30:00+02:00", "md": "1886", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_07_18
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-17T00:00:00+02:00
2008-07-18T00:00:00+02:00
normal
2018-05-03T13:53:01+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-18T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-15T18:30:00+02:00", "diaHole": "12.25", "diaPilot": null, "distDrill": "93", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Continue drilling 12¼\" hole section to TD.", "hpht": "0", "md": "1979", "mdCsgLast": "1404.7", "mdDiaHoleStart": "1418", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "1415", "presTestType": "formation integrity test", "reportNo": "18", "ropCurrent": "-999.99", "strengthForm": "1.6", "sum24Hr": "Unable to work at drill floor due to exhaust fumes (RECORDED ON F-99). Continued drilling 12¼\" hole section from 1895 m to 2145 m.", "tightWell": "0", "tvd": "1814", "tvdCsgLast": "1340.3", "tvdStrengthForm": "1346", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-17T22:00:00+02:00", "density": "1.35", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "1925", "mudClass": "oil based", "presBopRating": "0", "pv": "25", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "15" }, { "dTim": "2008-07-17T14:00:00+02:00", "density": "1.35", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "1894", "mudClass": "oil based", "presBopRating": "0", "pv": "28", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "16" }, { "dTim": "2008-07-17T04:00:00+02:00", "density": "1.35", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "1894", "mudClass": "oil based", "presBopRating": "0", "pv": "28", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "16" } ]
[ { "dTim": "2008-07-18T00:00:00+02:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[ { "azi": "110.77", "dTim": "2008-07-18T00:00:00+02:00", "incl": "36.22", "md": "1901.1", "tvd": "1751.8" }, { "azi": "113.23", "dTim": "2008-07-18T00:00:00+02:00", "incl": "36.46", "md": "1941.6", "tvd": "1784.4" }, { "azi": "114.94", "dTim": "2008-07-18T00:00:00+02:00", "incl": "35.93", "md": "1982.2", "tvd": "1817.1" }, { "azi": "115.29", "dTim": "2008-07-18T00:00:00+02:00", "incl": "35.4", "md": "2022.2", "tvd": "1849.7" }, { "azi": "115.18", "dTim": "2008-07-18T00:00:00+02:00", "incl": "34.51", "md": "2062.4", "tvd": "1882.6" }, { "azi": "113.36", "dTim": "2008-07-18T00:00:00+02:00", "incl": "32.88", "md": "2102.9", "tvd": "1916.2" } ]
[ { "comments": "Drilled 12 1/4\" hole section from 1886 m to 1895 m MD. Drilling parameters : Flow 3500 lpm / SPP 184 bar / String RPM 150 / WOB 2-3 MT / Torque 14-20 kNm / ECD 1.37 sg EMW. Drilled with limited ROP 20 m/hr to observe proper operation of mill pump and slurry system. Stopped drilling due to exhaust fumes on drillfloor. RU cascade system on drill floor.\n\nMeanwhile shut down csg. equipment. A total of 29 stds 9 5/8\" csg RB in derrick.", "dTimEnd": "2008-07-17T00:15:00+02:00", "dTimStart": "2008-07-17T00:00:00+02:00", "md": "1895", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk regarding, CRI & slurry system, servicing the TDS and start to RIH with drilling BHA and continue drilling 12¼\" hole.\n", "dTimEnd": "2008-07-17T14:45:00+02:00", "dTimStart": "2008-07-17T14:15:00+02:00", "md": "1383", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Serviced the TDS.\n", "dTimEnd": "2008-07-17T15:15:00+02:00", "dTimStart": "2008-07-17T14:45:00+02:00", "md": "1383", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Checked surface equipment prior to RIH with drilling BHA.\n", "dTimEnd": "2008-07-17T15:45:00+02:00", "dTimStart": "2008-07-17T15:15:00+02:00", "md": "1383", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH from 1383m to 1551m. Performed kick drill 29 sec. Continued RIH from 1551m to 1876m.\n", "dTimEnd": "2008-07-17T18:00:00+02:00", "dTimStart": "2008-07-17T15:45:00+02:00", "md": "1876", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up to TDS and filled the pipe. Performed survey at 1876m. Washed down and tagged bottom at 1895m.", "dTimEnd": "2008-07-17T19:00:00+02:00", "dTimStart": "2008-07-17T18:00:00+02:00", "md": "1895", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled 12¼\" hole section from 1895 m to 1955 m MD. Drilling parameters : Flow 3500 lpm / SPP 180 bar / String RPM 150 / WOB 2-5 MT / Torque 9-21 kNm / ECD 1.37-1.38 sg EMW / ROP 25-40 m/hour\nProblems pumping slurry from active tank to Slurry holding tank due to high viscosity.\n\nSimultaneously MU and RB 9 5/8\" csg. stds.\n", "dTimEnd": "2008-07-17T22:15:00+02:00", "dTimStart": "2008-07-17T19:00:00+02:00", "md": "1955", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Racked back one stand and circulated at reduced rate 30 rpm, 50 rpm, 1100 lpm. Due to cuttings ditch to holding tank blocked.\n", "dTimEnd": "2008-07-17T22:45:00+02:00", "dTimStart": "2008-07-17T22:15:00+02:00", "md": "1955", "phase": "fixed", "proprietaryCode": "drilling -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Contined drilling 12¼\" hole section from 1955 m to 1979 m MD. Drilling parameters : Flow 3500 lpm / SPP 180 bar / String RPM 150 / WOB 4-7 MT / Torque 8-22 kNm / ECD 1.37-1.38 sg EMW / ROP 25-35 m/hour\n\nSimultaneously MU and RB 9 5/8\" csg. stds.\n", "dTimEnd": "2008-07-18T00:00:00+02:00", "dTimStart": "2008-07-17T22:45:00+02:00", "md": "1979", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_07_19
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-18T00:00:00+02:00
2008-07-19T00:00:00+02:00
normal
2018-05-03T13:53:01+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-19T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-15T18:30:00+02:00", "diaHole": "12.25", "diaPilot": null, "distDrill": "501", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Continue drilling 12¼\" hole section to TD. Circulate hole clean. Drop Gyro. Start POOH.", "hpht": "0", "md": "2480", "mdCsgLast": "1404.7", "mdDiaHoleStart": "1418", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "1415", "presTestType": "formation integrity test", "reportNo": "19", "ropCurrent": "-999.99", "strengthForm": "1.6", "sum24Hr": "Continued drilling 12¼\" hole section. At 2405 m MD BHA torqued up and stalled out. Fired jars two times and came free. Continued drilling 12¼\" hole section from to 2601 m.", "tightWell": "0", "tvd": "2233", "tvdCsgLast": "1340.3", "tvdStrengthForm": "1346", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-18T11:00:00+02:00", "density": "1.42", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "2255", "mudClass": "oil based", "presBopRating": "345", "pv": "30", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "14.5" }, { "dTim": "2008-07-18T22:00:00+02:00", "density": "1.43", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "2428", "mudClass": "oil based", "presBopRating": "345", "pv": "34", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "15.5" }, { "dTim": "2008-07-18T16:00:00+02:00", "density": "1.42", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "2395", "mudClass": "oil based", "presBopRating": "345", "pv": "31", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "14" }, { "dTim": "2008-07-18T04:00:00+02:00", "density": "1.35", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "2050", "mudClass": "oil based", "presBopRating": "345", "pv": "30", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "12.5" } ]
[ { "dTim": "2008-07-19T00:00:00+02:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[ { "azi": "111.59", "dTim": "2008-07-19T00:00:00+02:00", "incl": "32.33", "md": "2143.5", "tvd": "1950.4" }, { "azi": "104.39", "dTim": "2008-07-19T00:00:00+02:00", "incl": "32.76", "md": "2224.1", "tvd": "2018.4" }, { "azi": "101.58", "dTim": "2008-07-19T00:00:00+02:00", "incl": "32.82", "md": "2264.4", "tvd": "2052.3" }, { "azi": "98.6", "dTim": "2008-07-19T00:00:00+02:00", "incl": "33.11", "md": "2304.7", "tvd": "2086.1" }, { "azi": "96.67", "dTim": "2008-07-19T00:00:00+02:00", "incl": "32.94", "md": "2345.4", "tvd": "2120.2" }, { "azi": "95.08", "dTim": "2008-07-19T00:00:00+02:00", "incl": "33.28", "md": "2385.6", "tvd": "2153.9" }, { "azi": "94.12", "dTim": "2008-07-19T00:00:00+02:00", "incl": "33.15", "md": "2426", "tvd": "2187.7" }, { "azi": "93.34", "dTim": "2008-07-19T00:00:00+02:00", "incl": "32.82", "md": "2466.3", "tvd": "2221.5" }, { "azi": "92.44", "dTim": "2008-07-19T00:00:00+02:00", "incl": "32.06", "md": "2506.6", "tvd": "2255.5" }, { "azi": "89.92", "dTim": "2008-07-19T00:00:00+02:00", "incl": "31.58", "md": "2546.8", "tvd": "2289.7" }, { "azi": "108.38", "dTim": "2008-07-19T00:00:00+02:00", "incl": "32.57", "md": "2183.5", "tvd": "1984.2" } ]
[ { "comments": "Contined drilling 12¼\" hole section from 1979 m to 2145 m MD. Drilling parameters : Flow 3500 lpm / SPP 180 bar / String RPM 150 / WOB 2-11 MT / Torque 10-22 kNm / ECD 1.37-1.395 sg EMW / ROP 30-45 m/hour.\nAt 2000m started to increase the mud weigth. Took survey after every connection.\n\nSimultaneously MU and RB 9 5/8\" csg. stds. Total in derrick 36 stds.\n", "dTimEnd": "2008-07-18T06:00:00+02:00", "dTimStart": "2008-07-18T00:00:00+02:00", "md": "2145", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued drilling 12¼\" hole section from 2145 m to 2405 m MD. Drilling parameters : Flow 3500 lpm / SPP 190 bar / String RPM 150 / WOB 2-8 MT / Torque 14-21 kNm / ECD 1.462-1.465 sg EMW / ROP 5-46 m/hour.\nTook survey after every connection.\n\nSimultaneously MU and RB 9 5/8\" csg. stds.\n", "dTimEnd": "2008-07-18T17:00:00+02:00", "dTimStart": "2008-07-18T06:00:00+02:00", "md": "2405", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "BHA torqued up and stalled out. Released torque and pulled with 50 MT overpull. Attempted to free pipe by rotation. No indication that hole had packed off. Had full circulation. Fired jars two times and came free. Established rotation at full circulation 3500 lpm, to circulate clean the BHA. Experienced sticky tendencies when going down to 2402m. \n", "dTimEnd": "2008-07-18T18:00:00+02:00", "dTimStart": "2008-07-18T17:00:00+02:00", "md": "2399", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Racked back one stand and reamed one stand at 3500 lpm 140 rpm up and 40 rpm down.\n", "dTimEnd": "2008-07-18T20:00:00+02:00", "dTimStart": "2008-07-18T18:00:00+02:00", "md": "2399", "phase": "fixed", "proprietaryCode": "drilling -- ream", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued drilling 12¼\" hole section from 2405 m to 2480 m MD. Drilling parameters : Flow 3500 lpm / SPP 202 bar / String RPM 150 / WOB 2-4 MT / Torque 18-22 kNm / ECD 1.459-1.465 sg EMW / ROP 15-31 m/hour.\nTook survey after every connection\n\nSimultaneously MU and RB 9 5/8\" csg. stds.", "dTimEnd": "2008-07-19T00:00:00+02:00", "dTimStart": "2008-07-18T20:00:00+02:00", "md": "2480", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_07_20
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-19T00:00:00+02:00
2008-07-20T00:00:00+02:00
normal
2018-05-03T13:53:01+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-20T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-15T18:30:00+02:00", "diaHole": "12.25", "diaPilot": null, "distDrill": "420", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Continue drilling 12¼\" hole section to TD. Circulate well clean. Drop Gyro. POOH with 12¼\" drilling BHA. R/U for RIH with 9 5/8\" x 10 3/4\" casing.", "hpht": "0", "md": "2900", "mdCsgLast": "1404.7", "mdDiaHoleStart": "1418", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "1415", "presTestType": "formation integrity test", "reportNo": "20", "ropCurrent": "-999.99", "strengthForm": "1.6", "sum24Hr": "Continued drilling 12¼\" hole section from 2641m to 2918 m. ", "tightWell": "0", "tvd": "2592", "tvdCsgLast": "1340.3", "tvdStrengthForm": "1346", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-19T22:00:00+02:00", "density": "1.43", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "2866", "mudClass": "oil based", "presBopRating": "345", "pv": "34", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "11" }, { "dTim": "2008-07-19T16:00:00+02:00", "density": "1.42", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "2744", "mudClass": "oil based", "presBopRating": "345", "pv": "30", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "11" }, { "dTim": "2008-07-19T11:00:00+02:00", "density": "1.42", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "2680", "mudClass": "oil based", "presBopRating": "345", "pv": "29", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "12" }, { "dTim": "2008-07-19T04:00:00+02:00", "density": "1.42", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "2562", "mudClass": "oil based", "presBopRating": "345", "pv": "32", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "14" } ]
[ { "dTim": "2008-07-20T00:00:00+02:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[ { "azi": "87.44", "dTim": "2008-07-20T00:00:00+02:00", "incl": "31.15", "md": "2587.3", "tvd": "2324.3" }, { "azi": "84.66", "dTim": "2008-07-20T00:00:00+02:00", "incl": "31.01", "md": "2626.8", "tvd": "2358.1" }, { "azi": "85.09", "dTim": "2008-07-20T00:00:00+02:00", "incl": "30.97", "md": "2667.8", "tvd": "2393.2" }, { "azi": "80.78", "dTim": "2008-07-20T00:00:00+02:00", "incl": "30.65", "md": "2789.4", "tvd": "2497.7" }, { "azi": "78.69", "dTim": "2008-07-20T00:00:00+02:00", "incl": "30.89", "md": "2829.6", "tvd": "2532.2" }, { "azi": "77.5", "dTim": "2008-07-20T00:00:00+02:00", "incl": "30.86", "md": "2866.9", "tvd": "2564.2" }, { "azi": "86.17", "dTim": "2008-07-20T00:00:00+02:00", "incl": "31.16", "md": "2708.1", "tvd": "2427.8" }, { "azi": "84.35", "dTim": "2008-07-20T00:00:00+02:00", "incl": "30.63", "md": "2748.4", "tvd": "2462.3" } ]
[ { "comments": "Continued drilling 12¼\" hole section from 2480 m to 2601 m MD. Drilling parameters : Flow 3500 lpm / SPP 202 bar / String RPM 150 / WOB 4-9 MT / Torque 15-28 kNm / ECD 1.456-1.459 sg EMW / ROP 20-30 m/hour.\nTook survey after every connection\nStringer at 2518m - 2523.5m MD and 2587m - 2588 m MD.\n\nSimultaneously MU and RB 9 5/8\" csg. stds. Total in derrick 50 stds.\n", "dTimEnd": "2008-07-19T06:00:00+02:00", "dTimStart": "2008-07-19T00:00:00+02:00", "md": "2", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued drilling 12¼\" hole section from 2601 m to 2641 m MD. Drilling parameters : Flow 3500 lpm / SPP 210 bar / String RPM 150 / WOB 3-8 MT / Torque 20-28 kNm / ECD 1.457-1.461 sg EMW / ROP 19-32 m/hour\n\nSimultaneously MU and RB 9 5/8\" csg. stds.\n\nGeoservices unit shut down.\n", "dTimEnd": "2008-07-19T08:15:00+02:00", "dTimStart": "2008-07-19T06:00:00+02:00", "md": "2641", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up and circulated and reciprocated the string. Geo-services unit did shut down\ndue to air tight door was not shut probably. Geo-services purged and re-booted the unit.\n", "dTimEnd": "2008-07-19T09:00:00+02:00", "dTimStart": "2008-07-19T08:15:00+02:00", "md": "2641", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued drilling 12¼\" hole section from 2641 m to 2860 m MD. Drilling parameters : Flow 3500 lpm / SPP 210 bar / String RPM 160 / WOB 2-4 MT / Torque 18-31 kNm / ECD 1.458-1.463 sg EMW / ROP 20-40 m/hour.\nGeo-Services unit was down until 11:30. Observed gas level manually in unit.\nTook survey after every connecting\nLost power to both mud pumps. Picked off bottom.\n\nSimultaneously MU and RB 9 5/8\" csg. stds. \n", "dTimEnd": "2008-07-19T21:15:00+02:00", "dTimStart": "2008-07-19T09:00:00+02:00", "md": "2860", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Due to generator tripped in process module, power supply was cut out to both mud pumps. Generator back on line and both mud pumps up running.", "dTimEnd": "2008-07-19T21:45:00+02:00", "dTimStart": "2008-07-19T21:15:00+02:00", "md": "2860", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued drilling 12¼\" hole section from 2860 m to 2898 m MD. Drilling parameters : Flow 3500 lpm / SPP 210 bar / String RPM 160 / WOB 3-8 MT / Torque 23-35 kNm / ECD 1.462-1.463 sg EMW / ROP 6-35 m/hour.", "dTimEnd": "2008-07-19T23:30:00+02:00", "dTimStart": "2008-07-19T21:45:00+02:00", "md": "2898", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Tagged hard formation at 2898m MD. Continued drilling 12¼\" hole section from 2898 m to 2900 m MD. Drilling parameters : Flow 3500 lpm / SPP 210 bar / String RPM 80 / WOB 10 MT / Torque 23-35 kNm / ECD 1.462-1.463 sg EMW / ROP 1-4 m/hour.", "dTimEnd": "2008-07-20T00:00:00+02:00", "dTimStart": "2008-07-19T23:30:00+02:00", "md": "2900", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_07_21
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-20T00:00:00+02:00
2008-07-21T00:00:00+02:00
normal
2018-05-03T13:53:01+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-21T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-15T18:30:00+02:00", "diaHole": "12.25", "diaPilot": null, "distDrill": "27", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Service TDS. Derrick inspection. R/U for RIH with 9 5/8\" x 10¼\" casing. RIH with 9 5/8\" x 10¼\" casing.", "hpht": "0", "md": "2927", "mdCsgLast": "1404.7", "mdDiaHoleStart": "1418", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "1415", "presTestType": "formation integrity test", "reportNo": "21", "ropCurrent": "-999.99", "strengthForm": "1.6", "sum24Hr": "Continued drilling 12¼\" hole section from 2818m to 2927 m. Circulated well clean. Dropped the Gyro. POOH with 12¼\" drilling BHA, laid out same. Abandoned the drill floor due to exhaust fumes from the gas turbines. ", "tightWell": "0", "tvd": "2614", "tvdCsgLast": "1340.3", "tvdStrengthForm": "1346", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-20T22:00:00+02:00", "density": "1.43", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "2927", "mudClass": "oil based", "presBopRating": "345", "pv": "25", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "12.5" }, { "dTim": "2008-07-20T12:00:00+02:00", "density": "1.43", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "2927", "mudClass": "oil based", "presBopRating": "345", "pv": "25", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "12.5" }, { "dTim": "2008-07-20T04:00:00+02:00", "density": "1.42", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "2911", "mudClass": "oil based", "presBopRating": "345", "pv": "32", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "14" } ]
[ { "dTim": "2008-07-21T00:00:00+02:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[ { "azi": "76.7", "dTim": "2008-07-21T00:00:00+02:00", "incl": "31.86", "md": "2913.3", "tvd": "2603.9" }, { "azi": "77.01", "dTim": "2008-07-21T00:00:00+02:00", "incl": "31.2", "md": "2904.4", "tvd": "2596.3" } ]
[ { "comments": "Continued drilling 12¼\" hole section from 2900 m to 2918 m MD. Drilling parameters : Flow 3500 lpm / SPP 210 bar / String RPM 160 / WOB 8-10 MT / Torque 12-35 kNm / ECD 1.445-1.450 sg EMW / ROP .5-5 m/hour.", "dTimEnd": "2008-07-20T06:00:00+02:00", "dTimStart": "2008-07-20T00:00:00+02:00", "md": "2918", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued drilling 12¼\" hole section from 2918 m to 2927 m MD. Drilling parameters : Flow 3500 lpm / SPP 217 bars / String RPM 160 / WOB 3-8 MT / Torque 14-35 kNm / ECD 1.445-1.451 sg EMW / ROP 1-4 m/hour.\n", "dTimEnd": "2008-07-20T10:15:00+02:00", "dTimStart": "2008-07-20T06:00:00+02:00", "md": "2927", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Circulated well clean while reciprocating the string. 3500 lpm 220 bars.\n", "dTimEnd": "2008-07-20T12:30:00+02:00", "dTimStart": "2008-07-20T10:15:00+02:00", "md": "2922", "phase": "fixed", "proprietaryCode": "drilling -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled one stand wet.\n", "dTimEnd": "2008-07-20T12:45:00+02:00", "dTimStart": "2008-07-20T12:30:00+02:00", "md": "2878", "phase": "fixed", "proprietaryCode": "drilling -- survey", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Dropped the Gyro at 1300 hours. Made up to TDS and rotated the string at 10 rpm.\n", "dTimEnd": "2008-07-20T13:00:00+02:00", "dTimStart": "2008-07-20T12:45:00+02:00", "md": "2878", "phase": "fixed", "proprietaryCode": "drilling -- survey", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Flow checked well, well static. Meanwhile held tool box talk prior to POOH with 12¼\" drilling BHA. Installed wiper rubber, checked dies in PS 21 slips.\n", "dTimEnd": "2008-07-20T13:30:00+02:00", "dTimStart": "2008-07-20T13:00:00+02:00", "md": "2878", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with 12¼\" drilling BHA wet from 2927m to 2722 m. Oberved no drag.\n", "dTimEnd": "2008-07-20T14:30:00+02:00", "dTimStart": "2008-07-20T13:30:00+02:00", "md": "2722", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Flow checked well, well static.\n", "dTimEnd": "2008-07-20T14:45:00+02:00", "dTimStart": "2008-07-20T14:30:00+02:00", "md": "2722", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up TDS and pumped 5m³ 1.65 SG slug. Continued POOH with 12¼\" drilling BHA from 2722m to 1391m inside the shoe. Oberved no drag.\n", "dTimEnd": "2008-07-20T18:00:00+02:00", "dTimStart": "2008-07-20T14:45:00+02:00", "md": "1391", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Flow checked well, well static.\n", "dTimEnd": "2008-07-20T18:15:00+02:00", "dTimStart": "2008-07-20T18:00:00+02:00", "md": "1391", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued POOH with 12¼\" drilling BHA from 1391m to 526 m.\n", "dTimEnd": "2008-07-20T19:00:00+02:00", "dTimStart": "2008-07-20T18:15:00+02:00", "md": "526", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed kick drill. Informed drill crew about the use of escape mask.\n", "dTimEnd": "2008-07-20T19:15:00+02:00", "dTimStart": "2008-07-20T19:00:00+02:00", "md": "526", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued POOH with 12¼\" drilling BHA from 526m to 135m.\n", "dTimEnd": "2008-07-20T20:15:00+02:00", "dTimStart": "2008-07-20T19:15:00+02:00", "md": "135", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Laid out 12¼\" drilling BHA.", "dTimEnd": "2008-07-21T00:00:00+02:00", "dTimStart": "2008-07-20T20:15:00+02:00", "md": "26", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_07_22
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-21T00:00:00+02:00
2008-07-22T00:00:00+02:00
normal
2018-05-03T13:53:01+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-22T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-15T18:30:00+02:00", "diaHole": "12.25", "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "RIH with 9 5/8\" x 10 3/4\" casing. Circulate prior to cement job. ", "hpht": "0", "md": "2927", "mdCsgLast": "1404.7", "mdDiaHoleStart": "1418", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "1415", "presTestType": "formation integrity test", "reportNo": "22", "ropCurrent": "-999.99", "strengthForm": "1.6", "sum24Hr": "Resumed work after waiting for exhaust fumes to clear rig floor. Retrieved wear bushing. R/U for RIH with 9 5/8\" x 10 3/4\" casing. Serviced TDS. Derrick inspection. Changed dies in AFT & FWD PRS's. RIH with Shoe track.", "tightWell": "0", "tvd": "2614", "tvdCsgLast": "1340.3", "tvdStrengthForm": "1346", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-21T22:00:00+02:00", "density": "1.42", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "2927", "mudClass": "oil based", "presBopRating": "345", "pv": "25", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "12.5" }, { "dTim": "2008-07-21T13:00:00+02:00", "density": "1.42", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "2927", "mudClass": "oil based", "presBopRating": "345", "pv": "25", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "12.5" } ]
[ { "dTim": "2008-07-22T00:00:00+02:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[]
[ { "comments": "Continued laying out 12¼\" drilling BHA, Bit and Powerdrive.", "dTimEnd": "2008-07-21T00:30:00+02:00", "dTimStart": "2008-07-21T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cleared and cleaned drill floor.\n", "dTimEnd": "2008-07-21T00:45:00+02:00", "dTimStart": "2008-07-21T00:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk and picked up and made up jet sub and wear bushing RT. Stopped operations due to exhaust fumes on drill floor. Waiting time recorded on F-99.\n", "dTimEnd": "2008-07-21T01:30:00+02:00", "dTimStart": "2008-07-21T00:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk and continued making up wear bushing RT. RIH and retrieved the wear bushing at 139 m. Washed the WH. POOH with wear bushing.", "dTimEnd": "2008-07-21T19:00:00+02:00", "dTimStart": "2008-07-21T16:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to service TDS, derrick inspection and change dies in AFT PRS.", "dTimEnd": "2008-07-21T19:15:00+02:00", "dTimStart": "2008-07-21T19:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Laid out the wear bushing and the RT.\n", "dTimEnd": "2008-07-21T19:30:00+02:00", "dTimStart": "2008-07-21T19:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed derrick inspection.\n", "dTimEnd": "2008-07-21T20:15:00+02:00", "dTimStart": "2008-07-21T19:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Serviced the TDS and inspected for loose items.\n", "dTimEnd": "2008-07-21T20:45:00+02:00", "dTimStart": "2008-07-21T20:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Changed dies in AFT PRS and inspected rollers in AFT and FWD PRS's.\n", "dTimEnd": "2008-07-21T21:45:00+02:00", "dTimStart": "2008-07-21T20:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cleared and cleaned rig floor.\n", "dTimEnd": "2008-07-21T22:15:00+02:00", "dTimStart": "2008-07-21T21:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed 5½\" elevators and bails from the rig floor.\n", "dTimEnd": "2008-07-21T22:30:00+02:00", "dTimStart": "2008-07-21T22:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up FAC tool to TDS. Installed casing bails.\n", "dTimEnd": "2008-07-21T23:45:00+02:00", "dTimStart": "2008-07-21T22:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged up casing elevator.\n", "dTimEnd": "2008-07-22T00:00:00+02:00", "dTimStart": "2008-07-21T23:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_07_23
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-22T00:00:00+02:00
2008-07-23T00:00:00+02:00
normal
2018-05-03T13:53:01+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-23T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-15T18:30:00+02:00", "diaHole": "12.25", "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "RIH on 5½\" HWDP landing string, PU cmt head, land out 9 5/8\" x 10 3/4\" casing. Circulate, pump & displace cement, pressure test on plug bump. Set seal assy & pressure test, POOH L/D RT.", "hpht": "0", "md": "2927", "mdCsgLast": "1404.7", "mdDiaHoleStart": "1418", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "1415", "presTestType": "formation integrity test", "reportNo": "23", "ropCurrent": "-999.99", "strengthForm": "1.6", "sum24Hr": "RIH with 9 5/8\" x 10 3/4\" casing to 2778m . Change to 5 1/2\" handling. MU hanger joint. R/D casing handling equipment. RIH with 10 3/4\" x 9 5/8\" csg on 5 1/2\" HWDP landing string from 2785m to 2861 m MD.", "tightWell": "0", "tvd": "2614", "tvdCsgLast": "1340.3", "tvdStrengthForm": "1346", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-22T22:00:00+02:00", "density": "1.42", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "2927", "mudClass": "oil based", "presBopRating": "345", "pv": "26", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "11" }, { "dTim": "2008-07-22T12:00:00+02:00", "density": "1.42", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "2927", "mudClass": "oil based", "presBopRating": "345", "pv": "25", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "12.5" } ]
[ { "dTim": "2008-07-23T00:00:00+02:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[]
[ { "comments": "Function tested casing elevator.\n", "dTimEnd": "2008-07-22T00:15:00+02:00", "dTimStart": "2008-07-22T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged up casing tong. Retrieved master bushing and installed automatic casing slips. \n", "dTimEnd": "2008-07-22T03:00:00+02:00", "dTimStart": "2008-07-22T00:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to RIH with 9 5/8\" casing and change out dies in FWD PRS.\n", "dTimEnd": "2008-07-22T03:15:00+02:00", "dTimStart": "2008-07-22T03:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Changed dies in FWD PRS.\n", "dTimEnd": "2008-07-22T04:15:00+02:00", "dTimStart": "2008-07-22T03:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up the shoe and checked the integrity. Picked up Intermediate jnt., Float jnt. and Baker locked the Shoe track. \n", "dTimEnd": "2008-07-22T06:00:00+02:00", "dTimStart": "2008-07-22T04:15:00+02:00", "md": "38", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 9 5/8\" casing from 38m to 1010m. Filled every stand with FAC tool. Broke circulation 550 lpm 23 bars.\n", "dTimEnd": "2008-07-22T12:15:00+02:00", "dTimStart": "2008-07-22T06:00:00+02:00", "md": "1010", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued RIH with 9 5/8\" casing from 1010m to shoe at 1397m. Filled every stand with FAC tool. Broke circulation 550 lpm 25 bars.\n", "dTimEnd": "2008-07-22T14:15:00+02:00", "dTimStart": "2008-07-22T12:15:00+02:00", "md": "1397", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued RIH with 9 5/8\" casing from 1397m to 1994m. Filled every stand with FAC tool. Broke circulation 550 lpm 27 bars.\n", "dTimEnd": "2008-07-22T17:00:00+02:00", "dTimStart": "2008-07-22T14:15:00+02:00", "md": "1994", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued RIH with 9 5/8\" casing from 1994m to 2305m. Filled every stand with FAC tool. Took weight. \n", "dTimEnd": "2008-07-22T18:30:00+02:00", "dTimStart": "2008-07-22T17:00:00+02:00", "md": "2305", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Worked string up/down free.\n", "dTimEnd": "2008-07-22T18:45:00+02:00", "dTimStart": "2008-07-22T18:30:00+02:00", "md": "2305", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk and changed out inserts of Odfjel elevator from 9 5/8\" to 10 3/4\".\n", "dTimEnd": "2008-07-22T20:30:00+02:00", "dTimStart": "2008-07-22T18:45:00+02:00", "md": "2305", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up and made up X-O 9 5/8\" x 10 3/4\".\n", "dTimEnd": "2008-07-22T20:45:00+02:00", "dTimStart": "2008-07-22T20:30:00+02:00", "md": "2305", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk and changed out inserts in of FMS slip and in the casing tong from 9 5/8\" to 10 3/4\".\n", "dTimEnd": "2008-07-22T21:45:00+02:00", "dTimStart": "2008-07-22T20:45:00+02:00", "md": "2305", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued RIH with 10 3/4\" casing from 2323m to 2608m. Filled every stand with FAC tool.\n", "dTimEnd": "2008-07-23T00:00:00+02:00", "dTimStart": "2008-07-22T21:45:00+02:00", "md": "2608", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_07_24
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-23T00:00:00+02:00
2008-07-24T00:00:00+02:00
normal
2018-05-03T13:53:01+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-24T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-15T18:30:00+02:00", "diaHole": "12.25", "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Complete BOP test. M/U RIH 8½\" BHA. Drill shoe track, clean rathole, 3m new formation. Perform FIT with 1.30 SG mud. Drill 8½\" to ~3150m, raise MW to 1.45SG. ", "hpht": "0", "md": "2927", "mdCsgLast": "2921", "mdDiaHoleStart": "1418", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "1415", "presTestType": "formation integrity test", "reportNo": "24", "ropCurrent": "-999.99", "strengthForm": "1.6", "sum24Hr": "Ran 9 5/8\" x 10 3/4\" casing to 2921m and cemented casing. Pressure tested casing to 345 bar 15 min. Commenced BOP test.", "tightWell": "0", "tvd": "2614", "tvdCsgLast": "2608.6", "tvdStrengthForm": "1346", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-23T22:00:00+02:00", "density": "1.42", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "2927", "mudClass": "oil based", "presBopRating": "345", "pv": "26", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "11.5" }, { "dTim": "2008-07-23T12:00:00+02:00", "density": "1.42", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "2927", "mudClass": "oil based", "presBopRating": "345", "pv": "25", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "12.5" } ]
[ { "dTim": "2008-07-24T00:00:00+02:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[]
[ { "comments": "Continued RIH with 10 3/4\" casing from 2608m to 2778m. Filled every stand with FAC tool.", "dTimEnd": "2008-07-23T01:15:00+02:00", "dTimStart": "2008-07-23T00:00:00+02:00", "md": "2778", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged down Odfjel elevator, FAC tool and long bails. Counted casing on cantilever and back-up sub's.", "dTimEnd": "2008-07-23T02:15:00+02:00", "dTimStart": "2008-07-23T01:15:00+02:00", "md": "2778", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up and rigged up drilling bails and 5½\" elevators.\n", "dTimEnd": "2008-07-23T03:45:00+02:00", "dTimStart": "2008-07-23T02:15:00+02:00", "md": "2778", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up and made up 10 3/4\" casing hanger / PADPRT assy.\n", "dTimEnd": "2008-07-23T04:00:00+02:00", "dTimStart": "2008-07-23T03:45:00+02:00", "md": "2778", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged down Odfjel slip and extension ring. Installed master bushing.\n", "dTimEnd": "2008-07-23T04:45:00+02:00", "dTimStart": "2008-07-23T04:00:00+02:00", "md": "2785", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged down Odfjel casing tong.", "dTimEnd": "2008-07-23T05:30:00+02:00", "dTimStart": "2008-07-23T04:45:00+02:00", "md": "2785", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 10 3/4\" x 9 5/8\" csg on 5 1/2\" HWDP landing string from 2785m to 2861m MD. Filled every stand.", "dTimEnd": "2008-07-23T06:00:00+02:00", "dTimStart": "2008-07-23T05:30:00+02:00", "md": "2861", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 10 3/4\" x 9 5/8\" csg on 5½\" HWDP landing string. P/U M/U cement head to top drive.\n", "dTimEnd": "2008-07-23T07:00:00+02:00", "dTimStart": "2008-07-23T06:00:00+02:00", "md": "2916", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke circ & picked up in stage to 2000 LPM, 77 bars, took losses, reduced to 1000 LPM - loss free rate. Total lost 11m³.\n", "dTimEnd": "2008-07-23T08:30:00+02:00", "dTimStart": "2008-07-23T07:00:00+02:00", "md": "2916", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Landed off csg as per Vetco procedure.\n", "dTimEnd": "2008-07-23T08:45:00+02:00", "dTimStart": "2008-07-23T08:30:00+02:00", "md": "2921", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up pumps to 1000 LPM & Circ one casing volume 5800 stks pumped. Simultaneously held tool box talk prior cmt job.\n", "dTimEnd": "2008-07-23T11:15:00+02:00", "dTimStart": "2008-07-23T08:45:00+02:00", "md": "2921", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pumped 8 m³ base oil from pit 14, 1000 LPM. Pump 20 m³ spacer 1.50 SG from pit 12, 1000 LPM. \n", "dTimEnd": "2008-07-23T12:00:00+02:00", "dTimStart": "2008-07-23T11:15:00+02:00", "md": "2921", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Displaced spacer in surface lines with 3m³ OBM & closed IBOP. Opened Lo-torq valve on cmt head and dropped 1 3/4\" ball.\n", "dTimEnd": "2008-07-23T12:15:00+02:00", "dTimStart": "2008-07-23T12:00:00+02:00", "md": "2921", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Mixed and pumped 17.3 m³ 1.90 SG cement according to Halliburton procedure. Bottom plug sheared at 80 bars.\n", "dTimEnd": "2008-07-23T13:00:00+02:00", "dTimStart": "2008-07-23T12:15:00+02:00", "md": "2921", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Displaced cmt to rig floor with 500 liters water, released dart and continued pumping 2500 liter water behind cement, dart sheared top wiper plug @ 205 bars. \n", "dTimEnd": "2008-07-23T13:15:00+02:00", "dTimStart": "2008-07-23T13:00:00+02:00", "md": "2921", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Displaced cmt with rig pumps 1000 LPM, at 2700 stk lost suction to MP changed from pit #7 to pit # 9 losses approx. 3 m³. Increased rate to 1500 LPM at 3200 stks. At 4082 stks btm plug sheared @ 135 bars. FCP 43 bars @ 1000 LPM, bumped plug at 4909 stks final pressure 113 bars. 96% pump efficiency.\n", "dTimEnd": "2008-07-23T15:15:00+02:00", "dTimStart": "2008-07-23T13:15:00+02:00", "md": "2921", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressure tested casing to 345 bars 15 min.\n", "dTimEnd": "2008-07-23T15:45:00+02:00", "dTimStart": "2008-07-23T15:15:00+02:00", "md": "2921", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Checked for back flow, float holding. Disconnected cmt hoses and flushed lines.\n", "dTimEnd": "2008-07-23T16:30:00+02:00", "dTimStart": "2008-07-23T15:45:00+02:00", "md": "2921", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rotated 4 turns to right to engage MS1 Seal. Engaged and set MS1 seal as per Vetco procedure, 35 bars/207 bars 10 min. \n", "dTimEnd": "2008-07-23T17:45:00+02:00", "dTimStart": "2008-07-23T16:30:00+02:00", "md": "2921", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Leak tested MS1 seal 35/345bars 5/10 min.\n", "dTimEnd": "2008-07-23T18:15:00+02:00", "dTimStart": "2008-07-23T17:45:00+02:00", "md": "2921", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Released PADPRT, 4 turns to right\n", "dTimEnd": "2008-07-23T18:30:00+02:00", "dTimStart": "2008-07-23T18:15:00+02:00", "md": "136", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "L/O cmt head", "dTimEnd": "2008-07-23T19:30:00+02:00", "dTimStart": "2008-07-23T18:30:00+02:00", "md": "136", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Dropped Halliburton sponge balls 2 ea and flush string using mud 1770 lpm. POOH PADPRT. \n", "dTimEnd": "2008-07-23T21:15:00+02:00", "dTimStart": "2008-07-23T19:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Out of hole with PADPRT inspected same. Laid out same.", "dTimEnd": "2008-07-23T21:45:00+02:00", "dTimStart": "2008-07-23T21:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "MU Wear Bushing RT, RIH and installed wear bushing according to Vetco procedures.", "dTimEnd": "2008-07-23T23:30:00+02:00", "dTimStart": "2008-07-23T21:45:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Commenced BOP test.", "dTimEnd": "2008-07-24T00:00:00+02:00", "dTimStart": "2008-07-23T23:30:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop activities", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_07_25
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-24T00:00:00+02:00
2008-07-25T00:00:00+02:00
normal
2018-05-03T13:53:01+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-25T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-15T18:30:00+02:00", "diaHole": "12.25", "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Change out the Wash pipe on the TDS. Displace to 1.30 SG as drilling shoe track, clean rathole, 3m new formation. Perform FIT with 1.30 SG mud. Drill 8½\" to ~3150m, raise MW in steps to 1.45SG. ", "hpht": "0", "md": "2927", "mdCsgLast": "2921", "mdDiaHoleStart": "1418", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "1415", "presTestType": "formation integrity test", "reportNo": "25", "ropCurrent": "-999.99", "strengthForm": "1.6", "sum24Hr": "Completed BOP test. M/U and RIH with 8½\" BHA from surface to 2551m. Commenced changing out the Wash pipe on the TDS.", "tightWell": "0", "tvd": "2614", "tvdCsgLast": "2608.6", "tvdStrengthForm": "1346", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-24T22:00:00+02:00", "density": "1.42", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "2927", "mudClass": "oil based", "presBopRating": "345", "pv": "26", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "11.5" }, { "dTim": "2008-07-24T12:00:00+02:00", "density": "1.42", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "2927", "mudClass": "oil based", "presBopRating": "345", "pv": "25", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "12.5" } ]
[ { "dTim": "2008-07-25T00:00:00+02:00", "equivalentMudWeight": "1.03", "md": "1415", "readingKind": "estimated" } ]
[]
[ { "comments": "Continued performing BOP test.\nSimultaneously cleaned out filters on mud pumps and cleaned out mill tank.", "dTimEnd": "2008-07-24T06:00:00+02:00", "dTimStart": "2008-07-24T00:00:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop activities", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued test BOP 25/345bar 5/10 min, as per MCN test procedure.\n", "dTimEnd": "2008-07-24T08:45:00+02:00", "dTimStart": "2008-07-24T06:00:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop activities", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cleared & cleaned around RT.\n", "dTimEnd": "2008-07-24T09:00:00+02:00", "dTimStart": "2008-07-24T08:45:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Released wear bushing RT. POOH wear bushing RT from 138m to 5m, strapped pipe. Measured Datum 138,87m.\n", "dTimEnd": "2008-07-24T11:00:00+02:00", "dTimStart": "2008-07-24T09:00:00+02:00", "md": "5", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk and laid out wear bushing.\n", "dTimEnd": "2008-07-24T12:00:00+02:00", "dTimStart": "2008-07-24T11:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cleared & cleaned around RT.\n", "dTimEnd": "2008-07-24T12:30:00+02:00", "dTimStart": "2008-07-24T12:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to M/U 8½\" BHA.\n", "dTimEnd": "2008-07-24T12:45:00+02:00", "dTimStart": "2008-07-24T12:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "M/U 8½\" BHA from surface to 61m.\n", "dTimEnd": "2008-07-24T16:15:00+02:00", "dTimStart": "2008-07-24T12:45:00+02:00", "md": "61", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk and installed radioactive source.\n", "dTimEnd": "2008-07-24T16:45:00+02:00", "dTimStart": "2008-07-24T16:15:00+02:00", "md": "61", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued M/U 8½\" BHA from 61m to 70m.\n", "dTimEnd": "2008-07-24T17:15:00+02:00", "dTimStart": "2008-07-24T16:45:00+02:00", "md": "70", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Changed to 5\" handling equipment & checked PRS dies.\n", "dTimEnd": "2008-07-24T17:30:00+02:00", "dTimStart": "2008-07-24T17:15:00+02:00", "md": "70", "phase": "fixed", "proprietaryCode": "drilling -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued M/U 8½\" BHA from 70m to 90m.\n", "dTimEnd": "2008-07-24T18:45:00+02:00", "dTimStart": "2008-07-24T17:30:00+02:00", "md": "90", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Dressed auto slips to 5\".\n", "dTimEnd": "2008-07-24T19:30:00+02:00", "dTimStart": "2008-07-24T18:45:00+02:00", "md": "116", "phase": "fixed", "proprietaryCode": "drilling -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 8½\" BHA on 5\" DP from 116m to 1216m. Tested MWD tools at 484m. Filled the pipe every 500m. \n", "dTimEnd": "2008-07-25T00:00:00+02:00", "dTimStart": "2008-07-24T19:30:00+02:00", "md": "1216", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_07_26
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-25T00:00:00+02:00
2008-07-26T00:00:00+02:00
normal
2018-05-03T13:53:01+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-26T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-25T21:15:00+02:00", "diaHole": "8.5", "diaPilot": null, "distDrill": "18", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Drill 8½\" hole section from 3000m to 3440m.", "hpht": "0", "md": "2945", "mdCsgLast": "2921", "mdDiaHoleStart": "2930", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "26", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Changed out the Wash pipe on the TDS. RIH with 8½\" drilling BHA on 5½\" DP. Tagged TOC at 2892m. Drilled out shoe track from 2892m to 2927m + 3m new formation. Took FIT equivalent 1.65 SG, using 1.30 SG OBM. Continued drill 8½\" hole from 2930m to 3000m.\n \n", "tightWell": "0", "tvd": "2628.7", "tvdCsgLast": "2608.6", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-25T17:00:00+02:00", "density": "1.3", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "2930", "mudClass": "oil based", "presBopRating": "345", "pv": "23", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "7" }, { "dTim": "2008-07-25T10:00:00+02:00", "density": "1.42", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "2927", "mudClass": "oil based", "presBopRating": "345", "pv": "26", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "11.5" }, { "dTim": "2008-07-25T22:45:00+02:00", "density": "1.3", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "2935", "mudClass": "oil based", "presBopRating": "345", "pv": "24", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "7.5" } ]
[ { "dTim": "2008-07-26T00:00:00+02:00", "equivalentMudWeight": "1.03", "md": "3000", "readingKind": "estimated" } ]
[ { "azi": "76.45", "dTim": "2008-07-26T00:00:00+02:00", "incl": "32.38", "md": "2927.7", "tvd": "2614.2" }, { "azi": "71.62", "dTim": "2008-07-26T00:00:00+02:00", "incl": "34.03", "md": "2954.6", "tvd": "2636.7" } ]
[ { "comments": "Continued RIH with 8½\" BHA on 5\" DP from 1216m to 1339m.", "dTimEnd": "2008-07-25T00:15:00+02:00", "dTimStart": "2008-07-25T00:00:00+02:00", "md": "1339", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up 5\" x 5½\" XO. Changed to 5½\" DP handling equipment.", "dTimEnd": "2008-07-25T00:45:00+02:00", "dTimStart": "2008-07-25T00:15:00+02:00", "md": "1339", "phase": "fixed", "proprietaryCode": "drilling -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued RIH with 8½\" BHA on 5½\" DP from 1339m to 1502m. Observed problem with TDS control software.\nParallel activity: Started injecting slops into F-14 annulus.", "dTimEnd": "2008-07-25T01:30:00+02:00", "dTimStart": "2008-07-25T00:45:00+02:00", "md": "1502", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Electrician investigated, and rectified the error on TDS.", "dTimEnd": "2008-07-25T03:00:00+02:00", "dTimStart": "2008-07-25T01:30:00+02:00", "md": "1502", "phase": "fixed", "proprietaryCode": "interruption -- repair", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued RIH with 8½\" BHA on 5½\" DP from 1502m to 2551. Filled the pipe every 500m.", "dTimEnd": "2008-07-25T05:30:00+02:00", "dTimStart": "2008-07-25T03:00:00+02:00", "md": "2551", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Commenced changing out the Wash pipe on the TDS.", "dTimEnd": "2008-07-25T06:00:00+02:00", "dTimStart": "2008-07-25T05:30:00+02:00", "md": "2551", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued changing out the Wash pipe on the TDS. Held 15 min handover crew change.\n", "dTimEnd": "2008-07-25T07:45:00+02:00", "dTimStart": "2008-07-25T06:00:00+02:00", "md": "2551", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up to TDS. Filled pipe & established circulation prior to perform choke drill. \nSimultaneously serviced TDS.\n", "dTimEnd": "2008-07-25T08:30:00+02:00", "dTimStart": "2008-07-25T07:45:00+02:00", "md": "2551", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed choke drill.\n", "dTimEnd": "2008-07-25T09:00:00+02:00", "dTimStart": "2008-07-25T08:30:00+02:00", "md": "2551", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk and RIH 8½\" BHA from 2551m to 2874m.\n", "dTimEnd": "2008-07-25T09:45:00+02:00", "dTimStart": "2008-07-25T09:00:00+02:00", "md": "2874", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Established circulation 1600 lpm & washed down from 2874m to 2892m.\n", "dTimEnd": "2008-07-25T10:30:00+02:00", "dTimStart": "2008-07-25T09:45:00+02:00", "md": "2892", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Tagged TOC at 2892m, Drilled out float from 2893m to 2894m. Drilling parameters: Flow 1600 lpm / SPP 128 bar / String RPM 40 / TQ 16-19 kNm. \nSimultaneously displaced well to 1,30 SG OBM.\n", "dTimEnd": "2008-07-25T11:30:00+02:00", "dTimStart": "2008-07-25T10:30:00+02:00", "md": "2894", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled out shoe track from 2894m to 2921m. Drilling parameters: Flow 1600 lpm / SPP 140 bar / String RPM 40 / TQ 14-17 kNm. MUD weight 1.30 SG.\nReamed the shoe and pulled back through shoe with no rotation.\n", "dTimEnd": "2008-07-25T15:00:00+02:00", "dTimStart": "2008-07-25T11:30:00+02:00", "md": "2921", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cleaned out rat hole in 1-2 m intervals from 2921m to 2927m. Experienced pack off and TDS stalled, 2nd time as reaming into shoe with bit at shoe. Also saw pack off with bit on bottom, stopped pumping slump pipe opposite direction of movement, No losses seen after pack off.\n", "dTimEnd": "2008-07-25T16:30:00+02:00", "dTimStart": "2008-07-25T15:00:00+02:00", "md": "2927", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Drilled new formation from 2927m to 2930m. Cleaned out rate hole and verified no restrictions. Drilling parameters: Flow 1600 lpm / SPP 130 bar / String RPM 160 / WOB 1-3 MT / TQ 17-20 kNm. MUD weight 1.30 SG.\n", "dTimEnd": "2008-07-25T17:45:00+02:00", "dTimStart": "2008-07-25T16:30:00+02:00", "md": "2930", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Observed 120 litres gain in trip tank.", "dTimEnd": "2008-07-25T18:00:00+02:00", "dTimStart": "2008-07-25T17:45:00+02:00", "md": "2930", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Racked back one stand. Observed the well on trip tank, well static.\n", "dTimEnd": "2008-07-25T18:30:00+02:00", "dTimStart": "2008-07-25T18:00:00+02:00", "md": "2913", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged up pump in sub and surface lines for FIT test. \n", "dTimEnd": "2008-07-25T19:15:00+02:00", "dTimStart": "2008-07-25T18:30:00+02:00", "md": "2913", "phase": "fixed", "proprietaryCode": "formation evaluation -- rft/fit", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Took FIT equivalent to 1.65 SG, using 1.30 SG OBM. Pumped 80 lpm and applied 92 bars to the string and annulus. Shut down the pump. Downhole reading from Schlumberger equivalent to 1,658 SG.\n", "dTimEnd": "2008-07-25T20:00:00+02:00", "dTimStart": "2008-07-25T19:15:00+02:00", "md": "2913", "phase": "fixed", "proprietaryCode": "formation evaluation -- rft/fit", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged down pump in sub and surface lines. Lined up for drilling.\n", "dTimEnd": "2008-07-25T21:15:00+02:00", "dTimStart": "2008-07-25T20:00:00+02:00", "md": "2913", "phase": "fixed", "proprietaryCode": "formation evaluation -- rft/fit", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Took survey at 2913m and set tool\n", "dTimEnd": "2008-07-25T21:30:00+02:00", "dTimStart": "2008-07-25T21:15:00+02:00", "md": "2913", "phase": "fixed", "proprietaryCode": "drilling -- survey", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to drill 8½\" hole from 2930m to 2945m. Drilling parameters: Flow 2100 lpm / SPP 214 bars / String RPM 100 Bit 260 / WOB 8-13 MT / TQ 15-20 kNm / ROP 8 m/hour / ESD 1.393 SG / MUD weight 1.30 SG.\nObserved active pit did not drop as drilling ahead.\n", "dTimEnd": "2008-07-25T23:45:00+02:00", "dTimStart": "2008-07-25T21:30:00+02:00", "md": "2945", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up and took flow check on the trip tank, well static.\n", "dTimEnd": "2008-07-26T00:00:00+02:00", "dTimStart": "2008-07-25T23:45:00+02:00", "md": "2945", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" } ]
[ { "dTim": "2008-07-26T00:00:00+02:00", "lithology": "Limestone with minor Claystone", "mdBottom": "2960", "mdTop": "2940", "show": null, "tvdBottom": "2641", "tvdTop": "2624.5" }, { "dTim": "2008-07-26T00:00:00+02:00", "lithology": "Limestone with traces of Claystone", "mdBottom": "3020", "mdTop": "2960", "show": null, "tvdBottom": "2989", "tvdTop": "2641" } ]
15_9_F_5_2008_07_27
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-26T00:00:00+02:00
2008-07-27T00:00:00+02:00
normal
2018-05-03T13:53:01+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-27T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-25T21:15:00+02:00", "diaHole": "8.5", "diaPilot": null, "distDrill": "315", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Circulate well clean. POOH with 8½\" BHA. Change Powerdrive Xceed and lay out motor and C-link. RIH with 8½\" BHA.\n\n", "hpht": "0", "md": "3260", "mdCsgLast": "2921", "mdDiaHoleStart": "2930", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "27", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Continued drill 8½\" hole from 3000m to 3292m. Poor response from Xceed. Unable to keep well path. Circulated well clean.", "tightWell": "0", "tvd": "2885.7", "tvdCsgLast": "2608.6", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-26T04:00:00+02:00", "density": "1.3", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "2994", "mudClass": "oil based", "presBopRating": "345", "pv": "22", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "8.5" }, { "dTim": "2008-07-26T21:00:00+02:00", "density": "1.45", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "3236", "mudClass": "oil based", "presBopRating": "345", "pv": "24", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "11.5" }, { "dTim": "2008-07-26T16:30:00+02:00", "density": "1.45", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "3202", "mudClass": "oil based", "presBopRating": "345", "pv": "25", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "10.5" }, { "dTim": "2008-07-26T09:30:00+02:00", "density": "1.35", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "3090", "mudClass": "oil based", "presBopRating": "345", "pv": "24", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "9.5" } ]
[ { "dTim": "2008-07-27T00:00:00+02:00", "equivalentMudWeight": "1.28", "md": "3293.5", "readingKind": "estimated" } ]
[ { "azi": "76.7", "dTim": "2008-07-27T00:00:00+02:00", "incl": "31.86", "md": "2913.3", "tvd": "2602.1" }, { "azi": "76.45", "dTim": "2008-07-27T00:00:00+02:00", "incl": "32.38", "md": "2927.7", "tvd": "2614.2" }, { "azi": "71.62", "dTim": "2008-07-27T00:00:00+02:00", "incl": "34.03", "md": "2954.6", "tvd": "2636.7" }, { "azi": "61.44", "dTim": "2008-07-27T00:00:00+02:00", "incl": "36.51", "md": "2995.2", "tvd": "2669.9" }, { "azi": "48.33", "dTim": "2008-07-27T00:00:00+02:00", "incl": "37.73", "md": "3076.7", "tvd": "2735.1" }, { "azi": "43.61", "dTim": "2008-07-27T00:00:00+02:00", "incl": "37.11", "md": "3117.2", "tvd": "2767.2" }, { "azi": "34.79", "dTim": "2008-07-27T00:00:00+02:00", "incl": "35.73", "md": "3157.5", "tvd": "2799.7" }, { "azi": "28.91", "dTim": "2008-07-27T00:00:00+02:00", "incl": "34.2", "md": "3197", "tvd": "2832.1" }, { "azi": "21.36", "dTim": "2008-07-27T00:00:00+02:00", "incl": "31.59", "md": "3236.9", "tvd": "2865.6" }, { "azi": "19.04", "dTim": "2008-07-27T00:00:00+02:00", "incl": "30.18", "md": "3253.8", "tvd": "2880.1" }, { "azi": "55.01", "dTim": "2008-07-27T00:00:00+02:00", "incl": "36.77", "md": "3036.4", "tvd": "2703" } ]
[ { "comments": "Continued to drill 8½\" hole from 2945m to 2994m. Drilling parameters: Flow 2100 lpm / SPP 214-240 bars / String RPM 100-120 Bit 260-280 / WOB 8-13 MT / TQ 15-20 kNm / ROP 8-20 m/hour / ESD 1.379-1.393 SG / MUD weight 1.30 SG.\nProblems operating the AFT PRS.\nTook survey after every connection.\n", "dTimEnd": "2008-07-26T03:30:00+02:00", "dTimStart": "2008-07-26T00:00:00+02:00", "md": "2994", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Electrician investigated the error. Found that the pipe size setting of the AFT PRS was incorrect. As investigating the error of the AFT PRS. Reciprocated the string one jnt circulating 2100 lpm 206 bars.\nMeanwhile switch to the FWD PRS and picked up 5½\" DP.\n", "dTimEnd": "2008-07-26T04:15:00+02:00", "dTimStart": "2008-07-26T03:30:00+02:00", "md": "2994", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued to drill 8½\" hole from 2994m to 3000m. Drilling parameters: Flow 2100 lpm / SPP 214-240 bars / String RPM 100-120 Bit 260-280 / WOB 8-13 MT / TQ 19-21 kNm / ROP 4 m/hour / ESD 1.393-1.401 SG / \nIncreased MUD weight from 1.30 SG to 1.35 SG.\nTook survey after connection. Had to down link twices det proper Power setting from 50 to 35. Down linked Xceed to get tool face setting from 288 to 268.", "dTimEnd": "2008-07-26T06:00:00+02:00", "dTimStart": "2008-07-26T04:15:00+02:00", "md": "3000", "phase": "fixed", "proprietaryCode": "drilling -- survey", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to drill 8½\" hole from 3000m to 3155m. Drilling parameters: Flow 2100 lpm / SPP 240 bars / String RPM 130 Bit 290 / WOB 8-13 MT / TQ 16-30 kNm / ROP 40-50m/hour / ECD 1.419-1.569 SG / MUD weight 1.35-1.45 SG.\nTook survey after every connection. Reamed one single prior to connection.", "dTimEnd": "2008-07-26T12:00:00+02:00", "dTimStart": "2008-07-26T06:00:00+02:00", "md": "3155", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to drill 8½\" hole from 3155m to 3233m. Drilling parameters: Flow 2100 lpm / SPP 240-250 bars / String RPM 100-130 Bit 260-290 / WOB 6-11 MT / TQ 16-30 kNm / ROP 2-50m/hour / ECD 1.536-1.570 SG / MUD weight 1.45 SG.\nReamed one single prior to connection when high ROP.Took survey after every connection.\nProblems with CRI transfer pump on the active tank. \nParallel operation: Made up 7\" liner in stands and racked back in derrick.", "dTimEnd": "2008-07-26T19:00:00+02:00", "dTimStart": "2008-07-26T12:00:00+02:00", "md": "3233", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Found the housing of the CRI transfer pump washed out. Installed new housing. \nMeanwhile lined up to be able to operate the CRI system manually.\n", "dTimEnd": "2008-07-26T20:00:00+02:00", "dTimStart": "2008-07-26T19:00:00+02:00", "md": "3233", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued to drill 8½\" hole from 3233m to 3260m. Drilling parameters: Flow 2100 lpm / SPP 240-250 bars / String RPM 130-150 Bit 290-310 / WOB 6-16 MT / TQ 21-25 kNm / ROP 5-15m/hour / ECD 1.569-1.571 SG / MUD weight 1.45 SG.\nTook survey after connection. Down linked tool. \nCleaned in lower shaker. \nParallel operation: Made up 7\" liner in stands and racked back in derrick\n", "dTimEnd": "2008-07-27T00:00:00+02:00", "dTimStart": "2008-07-26T20:00:00+02:00", "md": "3260", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" } ]
[ { "dTim": "2008-07-27T00:00:00+02:00", "lithology": "Limestone grading to Marl with minor Claystone", "mdBottom": "3230", "mdTop": "3180", "show": null, "tvdBottom": "2860", "tvdTop": "2817" }, { "dTim": "2008-07-27T00:00:00+02:00", "lithology": "Limestone with minor Marl", "mdBottom": "3250", "mdTop": "3240", "show": null, "tvdBottom": "2877", "tvdTop": "2869" }, { "dTim": "2008-07-27T00:00:00+02:00", "lithology": "Marl with stringers of Limestone and Claystone", "mdBottom": "3292", "mdTop": "3260", "show": null, "tvdBottom": "2913.5", "tvdTop": "2885" } ]
15_9_F_5_2008_07_28
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-27T00:00:00+02:00
2008-07-28T00:00:00+02:00
normal
2018-05-03T13:53:01+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-28T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-25T21:15:00+02:00", "diaHole": "8.5", "diaPilot": null, "distDrill": "32", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "RIH with 8½\" BHA from 1844m to 3292m and continue drilling 8½ hole to 3600m\n", "hpht": "0", "md": "3292", "mdCsgLast": "2921", "mdDiaHoleStart": "2930", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "28", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "POOH with 8½\" BHA and changed with back-up. RIH with new 8½\" BHA, from surface to 1844m.\n", "tightWell": "0", "tvd": "2915", "tvdCsgLast": "2608.6", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-27T04:00:00+02:00", "density": "1.45", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "3292", "mudClass": "oil based", "presBopRating": "345", "pv": "27", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "10" }, { "dTim": "2008-07-27T22:00:00+02:00", "density": "1.46", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3293", "mudClass": "oil based", "presBopRating": "345", "pv": "24", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "12.5" }, { "dTim": "2008-07-27T15:00:00+02:00", "density": "1.46", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3293", "mudClass": "oil based", "presBopRating": "345", "pv": "25", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "11.5" } ]
[ { "dTim": "2008-07-28T00:00:00+02:00", "equivalentMudWeight": "1.28", "md": "3292.5", "readingKind": "estimated" } ]
[]
[ { "comments": "Continued to drill 8½\" hole from 3260m to 3293m. Drilling parameters: Flow 2100 lpm / SPP 240-260 bars / String RPM 130-150 Bit 290-310 / WOB 4-6 MT / TQ 22-27 kNm / ROP 7-25m/hour / ECD 1.569-1.582 SG / MUD weight 1.45 SG.\nTook survey after connection. Down linked tool. Poor response from Xceed. \nParallel operation: Made up 7\" liner in stands and racked back in derrick.", "dTimEnd": "2008-07-27T02:45:00+02:00", "dTimStart": "2008-07-27T00:00:00+02:00", "md": "3292", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Poor response from Xceed. Unable to keep well path. Discussed situation with Geologist in town and concluded to POOH and change BHA.", "dTimEnd": "2008-07-27T03:30:00+02:00", "dTimStart": "2008-07-27T02:45:00+02:00", "md": "3280", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Pulled back one stand and circulated well clean and 2100 lpm 230 bars. Reciprocated the string. \nParallel operation: Made up 7\" liner in stands and racked back in derrick. Total in derrick 9 stds.\n", "dTimEnd": "2008-07-27T06:00:00+02:00", "dTimStart": "2008-07-27T03:30:00+02:00", "md": "3240", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Flow checked well, well static.\n", "dTimEnd": "2008-07-27T06:15:00+02:00", "dTimStart": "2008-07-27T06:00:00+02:00", "md": "3240", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Commenced to POOH with 8½\" BHA wet.\n", "dTimEnd": "2008-07-27T07:00:00+02:00", "dTimStart": "2008-07-27T06:15:00+02:00", "md": "3157", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "M/U TDS and down linked the LWD tools.\n", "dTimEnd": "2008-07-27T07:45:00+02:00", "dTimStart": "2008-07-27T07:00:00+02:00", "md": "3157", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Lined up to trip tank & flow checked well on trip tank, well static.\n", "dTimEnd": "2008-07-27T08:15:00+02:00", "dTimStart": "2008-07-27T07:45:00+02:00", "md": "3157", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Pumped 10 m3 slug 1.65 SG.\n", "dTimEnd": "2008-07-27T08:45:00+02:00", "dTimStart": "2008-07-27T08:15:00+02:00", "md": "3157", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued POOH with 8½\" BHA from 3157m to 2914m, no restrictions seen when pulling into shoe.\n", "dTimEnd": "2008-07-27T09:45:00+02:00", "dTimStart": "2008-07-27T08:45:00+02:00", "md": "2914", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Flow checked well on trip tank, well static. Meanwhile service TDS.\n", "dTimEnd": "2008-07-27T10:15:00+02:00", "dTimStart": "2008-07-27T09:45:00+02:00", "md": "2914", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued POOH with 8½\" BHA from 2914m to 1340m on 5½\" DP. Trip time 700 m/hour.\n", "dTimEnd": "2008-07-27T12:30:00+02:00", "dTimStart": "2008-07-27T10:15:00+02:00", "md": "1340", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Changed to 5\" handling gear.\n", "dTimEnd": "2008-07-27T12:45:00+02:00", "dTimStart": "2008-07-27T12:30:00+02:00", "md": "1340", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued POOH with 8½\" BHA from 1340m to 140m on 5\" DP. Trip time 600 m/hour.\n", "dTimEnd": "2008-07-27T14:45:00+02:00", "dTimStart": "2008-07-27T12:45:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Flow checked well, well static. Meanwhile held tool box talk prior to L/O BHA.\n", "dTimEnd": "2008-07-27T15:00:00+02:00", "dTimStart": "2008-07-27T14:45:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Cleaned around rotary table.\n", "dTimEnd": "2008-07-27T15:15:00+02:00", "dTimStart": "2008-07-27T15:00:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Changed to master bushing & checked PRS dies.\n", "dTimEnd": "2008-07-27T15:45:00+02:00", "dTimStart": "2008-07-27T15:15:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "POOH with 8 1/2\" BHA from 140m to 61m.\n", "dTimEnd": "2008-07-27T16:15:00+02:00", "dTimStart": "2008-07-27T15:45:00+02:00", "md": "61", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Removed radioactive source from BHA.\n", "dTimEnd": "2008-07-27T16:45:00+02:00", "dTimStart": "2008-07-27T16:15:00+02:00", "md": "61", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued L/O BHA from 61m to surface.\n", "dTimEnd": "2008-07-27T18:45:00+02:00", "dTimStart": "2008-07-27T16:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Inspected bit & Xceed tool, decided to run back-up bit.", "dTimEnd": "2008-07-27T19:00:00+02:00", "dTimStart": "2008-07-27T18:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Held tool box talk and checked equipment.\n", "dTimEnd": "2008-07-27T19:30:00+02:00", "dTimStart": "2008-07-27T19:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Laid out Xceed and BHA components.\n", "dTimEnd": "2008-07-27T20:00:00+02:00", "dTimStart": "2008-07-27T19:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Picked up and made up new 8½\" BHA. RIH from surface to 42m.\n", "dTimEnd": "2008-07-27T22:30:00+02:00", "dTimStart": "2008-07-27T20:00:00+02:00", "md": "42", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Held tool box talk and erected barriers prior to handling radio active source.\n", "dTimEnd": "2008-07-27T22:45:00+02:00", "dTimStart": "2008-07-27T22:30:00+02:00", "md": "42", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Pulled BHA back to Ecoscope and inserted radioactive source. Ran back in to 42m.\n", "dTimEnd": "2008-07-27T23:00:00+02:00", "dTimStart": "2008-07-27T22:45:00+02:00", "md": "42", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Changed out handling gear from 5½\" to 5\".\n", "dTimEnd": "2008-07-27T23:15:00+02:00", "dTimStart": "2008-07-27T23:00:00+02:00", "md": "42", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued RIH with 8½\"BHA from derrick 5\" HWDP from 42m to 99m. Checked Totco ring.\n", "dTimEnd": "2008-07-28T00:00:00+02:00", "dTimStart": "2008-07-27T23:15:00+02:00", "md": "99", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" } ]
[]
15_9_F_5_2008_07_29
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-28T00:00:00+02:00
2008-07-29T00:00:00+02:00
normal
2018-05-03T13:53:02+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-29T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-25T21:15:00+02:00", "diaHole": "8.5", "diaPilot": null, "distDrill": "208", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Continue drilling 8½\" BHA from 3600m to TD. Take pressure points. Circulate well clean. Start to POOH with 8½\" BHA.\n", "hpht": "0", "md": "3500", "mdCsgLast": "2921", "mdDiaHoleStart": "2930", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "29", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "RIH with new 8½\" BHA to 3292m. Continued drilling 8½\" hole from 3292 to 3600m. Took pressure point at 3530m.", "tightWell": "0", "tvd": "3080", "tvdCsgLast": "2608.6", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-28T16:00:00+02:00", "density": "1.45", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "3321", "mudClass": "oil based", "presBopRating": "345", "pv": "26", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "9" }, { "dTim": "2008-07-28T20:00:00+02:00", "density": "1.45", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "3417", "mudClass": "oil based", "presBopRating": "345", "pv": "26", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "10" }, { "dTim": "2008-07-28T23:30:00+02:00", "density": "1.46", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "3495", "mudClass": "oil based", "presBopRating": "345", "pv": "28", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "9.5" } ]
[ { "dTim": "2008-07-29T00:00:00+02:00", "equivalentMudWeight": "1.28", "md": "3470", "readingKind": "estimated" }, { "dTim": "2008-07-29T00:00:00+02:00", "equivalentMudWeight": "1", "md": "3530", "readingKind": "measured" } ]
[ { "azi": "16.57", "dTim": "2008-07-29T00:00:00+02:00", "incl": "28.32", "md": "3278.3", "tvd": "2901.5" }, { "azi": "22.37", "dTim": "2008-07-29T00:00:00+02:00", "incl": "30.91", "md": "3319", "tvd": "2936.9" }, { "azi": "27.52", "dTim": "2008-07-29T00:00:00+02:00", "incl": "34.92", "md": "3359.2", "tvd": "2970.6" }, { "azi": "30.9", "dTim": "2008-07-29T00:00:00+02:00", "incl": "40.44", "md": "3398.5", "tvd": "3001.7" }, { "azi": "31.42", "dTim": "2008-07-29T00:00:00+02:00", "incl": "44.73", "md": "3439.6", "tvd": "3031.9" }, { "azi": "28.18", "dTim": "2008-07-29T00:00:00+02:00", "incl": "47.93", "md": "3479.3", "tvd": "3059.4" }, { "azi": "26.17", "dTim": "2008-07-29T00:00:00+02:00", "incl": "50.65", "md": "3520.4", "tvd": "3086.2" }, { "azi": "23.14", "dTim": "2008-07-29T00:00:00+02:00", "incl": "53.98", "md": "3559.9", "tvd": "3110.3" } ]
[ { "comments": "Installed autoslips.\n", "dTimEnd": "2008-07-28T00:15:00+02:00", "dTimStart": "2008-07-28T00:00:00+02:00", "md": "99", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued RIH with 8½ BHA on 5\" DP from 99m to 303m. Filled string every 300m. Trip time 407 m/hour.\n", "dTimEnd": "2008-07-28T00:45:00+02:00", "dTimStart": "2008-07-28T00:15:00+02:00", "md": "303", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Filled string, empty trip tank. Made up x-over to string and test MWD tools, 1600 lpm. Good. Removed x-over.\n", "dTimEnd": "2008-07-28T02:00:00+02:00", "dTimStart": "2008-07-28T00:45:00+02:00", "md": "303", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued RIH with 8½ BHA on 5\" DP from 303 to 1320m. Filled string every 300m. Monitored displacement on trip tank. Trip time 407 m/hour.\n", "dTimEnd": "2008-07-28T04:30:00+02:00", "dTimStart": "2008-07-28T02:00:00+02:00", "md": "1320", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Installed 5\" x 5½\" XO. Changed handling equipment to 5½\".\n", "dTimEnd": "2008-07-28T05:00:00+02:00", "dTimStart": "2008-07-28T04:30:00+02:00", "md": "1320", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued RIH with 8½ BHA on 5½\" DP from 1320 to 1844m. Filled string every 300m. Monitored displacement on trip tank. Trip time 524 m/hour.", "dTimEnd": "2008-07-28T06:00:00+02:00", "dTimStart": "2008-07-28T05:00:00+02:00", "md": "1844", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "RIH with 8½ BHA on 5½\" DP from 1844 to 2651m. Filled string every 300m. Monitored displacement on trip tank. Trip time 323 m/hour\n", "dTimEnd": "2008-07-28T08:30:00+02:00", "dTimStart": "2008-07-28T06:00:00+02:00", "md": "2651", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Serviced FWD PRS, due to unexplained noise.\n", "dTimEnd": "2008-07-28T09:15:00+02:00", "dTimStart": "2008-07-28T08:30:00+02:00", "md": "2651", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 8½ BHA on 5½\" DP from 2651 to 2920m. Filled string every 300m. Monitored displacement on trip tank. Trip time 359 m/hour\n", "dTimEnd": "2008-07-28T10:00:00+02:00", "dTimStart": "2008-07-28T09:15:00+02:00", "md": "2920", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Broke circulation at shoe and washed down from 2920m to 3259m.\n", "dTimEnd": "2008-07-28T10:30:00+02:00", "dTimStart": "2008-07-28T10:00:00+02:00", "md": "3259", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued RIH with 8½ BHA on 5½\" DP from 2920 to 3259m. Filled string every 300m. Monitored displacement on trip tank.\n", "dTimEnd": "2008-07-28T11:45:00+02:00", "dTimStart": "2008-07-28T10:30:00+02:00", "md": "3259", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Took connection and made up to TDS. Reamed from 3259m to 3294m and took survey with bit at 3293m.\n", "dTimEnd": "2008-07-28T13:00:00+02:00", "dTimStart": "2008-07-28T11:45:00+02:00", "md": "3294", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Tight hole after survey. Pulled with 40 MT overpull. Attempted to slump down pipe with rotation. Jared up with 240 MT and freed pipe. Established and rotation reamed slowly up.", "dTimEnd": "2008-07-28T13:30:00+02:00", "dTimStart": "2008-07-28T13:00:00+02:00", "md": "3293", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Reamed full stand from 3259m to 3294m.\n", "dTimEnd": "2008-07-28T14:00:00+02:00", "dTimStart": "2008-07-28T13:30:00+02:00", "md": "3294", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Took survey @ 3283m, good survey.\n", "dTimEnd": "2008-07-28T14:15:00+02:00", "dTimStart": "2008-07-28T14:00:00+02:00", "md": "3283", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued to drill 8½\" hole from 3292m to 3367m. Reamed Draupne transition zone from 3338m to 3300m. Drilling parameters: Flow 2100 lpm / SPP 210 bars / String RPM 130-180 / WOB 6-11 MT / TQ 24-38 kNm / ROP 17-40 m/hour / ECD 1.586-1.601 SG / MUD weight 1.45 SG.\nTook survey after every connection. Down linked tool.\nParallel operation: Made up 7\" liner in stands and racked back in derrick. \n", "dTimEnd": "2008-07-28T18:00:00+02:00", "dTimStart": "2008-07-28T14:15:00+02:00", "md": "3367", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Unexplained gain approx 300ltr. Spaced out & observed well on trip tank.\n", "dTimEnd": "2008-07-28T18:15:00+02:00", "dTimStart": "2008-07-28T18:00:00+02:00", "md": "3367", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Took SCRs as per below table @ 3366m.\n", "dTimEnd": "2008-07-28T18:30:00+02:00", "dTimStart": "2008-07-28T18:15:00+02:00", "md": "3366", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to drill 8½\" hole from 3367m to 3500m. Reamed Draupne transition zone from 3419m to 3388m. Drilling parameters: Flow 2100 lpm / SPP 205-209 bars / String RPM 180 / WOB 3-8 MT / TQ 20-26 kNm / ROP 30-50 m/hour / ECD 1.602-1.619 SG / MUD weight 1.45 SG.\nTook survey after every connection. Down linked tool.\nParallel operation: Made up 7\" liner in stands and racked back in derrick.", "dTimEnd": "2008-07-29T00:00:00+02:00", "dTimStart": "2008-07-28T18:30:00+02:00", "md": "3500", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" } ]
[ { "dTim": "2008-07-29T00:00:00+02:00", "lithology": "Interbedded Limestone and Marl with minor Claystone", "mdBottom": "3300", "mdTop": "3295", "show": null, "tvdBottom": "2946", "tvdTop": "2916" }, { "dTim": "2008-07-29T00:00:00+02:00", "lithology": "Carboncaceous Claystone with minor Marl and Claystone", "mdBottom": "3390", "mdTop": "3310", "show": null, "tvdBottom": "2996", "tvdTop": "2929" }, { "dTim": "2008-07-29T00:00:00+02:00", "lithology": "Carbonaceous Claystone with minor Claystone and Limestone", "mdBottom": "3470", "mdTop": "3400", "show": null, "tvdBottom": "3052", "tvdTop": "3003" }, { "dTim": "2008-07-29T00:00:00+02:00", "lithology": "Interbedded Claystone and Sandstone with Limestone", "mdBottom": "3512", "mdTop": "3480", "show": null, "tvdBottom": "3080.8", "tvdTop": "3059" }, { "dTim": "2008-07-29T00:00:00+02:00", "lithology": "Sandstone with minor Claystone, Limestone and Pyrite", "mdBottom": "3620", "mdTop": "3518", "show": null, "tvdBottom": "3085.9", "tvdTop": "3084.7" }, { "dTim": "2008-07-29T00:00:00+02:00", "lithology": "Sandstone with Claystone and Limestone ", "mdBottom": "3710", "mdTop": "3626", "show": null, "tvdBottom": "3197.1", "tvdTop": "3148.7" }, { "dTim": "2008-07-29T00:00:00+02:00", "lithology": "Interbedded Sandstone, Limestone and Claystone", "mdBottom": "3740", "mdTop": "3713", "show": null, "tvdBottom": "3215", "tvdTop": "3198.9" } ]
15_9_F_5_2008_07_30
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-29T00:00:00+02:00
2008-07-30T00:00:00+02:00
normal
2018-05-03T13:53:02+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": "4507.8", "avgTempBH": "100", "dTim": "2008-07-30T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-25T21:15:00+02:00", "diaHole": "8.5", "diaPilot": null, "distDrill": "192", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Continue POOH with 8½\" BHA. Lay out 8½\" BHA. Rig up for RIH with 7\" liner. Commence RIH with 7\" liner.", "hpht": "0", "md": "3792", "mdCsgLast": "2921", "mdDiaHoleStart": "2930", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "30", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Drilled 8½\" hole from 3600 to 3792m. Took pressure points at 3585.9m, 3648.9m, 3730.9m & 3720.9m. Circulated well clean. POOH wet with 8½\" BHA from 3792m to 3542m Attempted to take points at bit/probe depth 3694/3660m, 3677/3643m & 3556/3522m. StetScope did not perform.", "tightWell": "0", "tvd": "3247", "tvdCsgLast": "2608.6", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-29T04:00:00+02:00", "density": "1.45", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "3580", "mudClass": "oil based", "presBopRating": "345", "pv": "24", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "10.5" }, { "dTim": "2008-07-29T22:00:00+02:00", "density": "1.45", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3792", "mudClass": "oil based", "presBopRating": "345", "pv": "25", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "10" }, { "dTim": "2008-07-29T15:30:00+02:00", "density": "1.46", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "3725", "mudClass": "oil based", "presBopRating": "345", "pv": "29", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "11" }, { "dTim": "2008-07-29T10:00:00+02:00", "density": "1.45", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Flowline", "md": "3661", "mudClass": "oil based", "presBopRating": "345", "pv": "29", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "9.5" } ]
[ { "dTim": "2008-07-30T00:00:00+02:00", "equivalentMudWeight": ".99", "md": "3697", "readingKind": "measured" } ]
[ { "azi": "22.31", "dTim": "2008-07-30T00:00:00+02:00", "incl": "54.71", "md": "3601.7", "tvd": "3134.7" }, { "azi": "22.15", "dTim": "2008-07-30T00:00:00+02:00", "incl": "54.84", "md": "3642.1", "tvd": "3158" }, { "azi": "22.24", "dTim": "2008-07-30T00:00:00+02:00", "incl": "55.13", "md": "3682.4", "tvd": "3181.1" }, { "azi": "22.04", "dTim": "2008-07-30T00:00:00+02:00", "incl": "53.47", "md": "3722.9", "tvd": "3204.7" }, { "azi": "22.04", "dTim": "2008-07-30T00:00:00+02:00", "incl": "52.67", "md": "3761.8", "tvd": "3228.1" } ]
[ { "comments": "Continued to drill 8½\" hole from 3500m to 3580m. Drilling parameters: Flow 2100 lpm / SPP 205-209 bars / String RPM 180 / WOB 3-6 MT / TQ 26-28 kNm / ROP 30-50 m/hour / ECD 1.582-1.604 SG / MUD weight 1.45 SG.\nTook survey after every connection. Down linked tool.\nHeld tool box talk as drilling ahead prior taking pressure points.\nParallel operation: Made up 7\" liner in stands and racked back in derrick. \n", "dTimEnd": "2008-07-29T03:15:00+02:00", "dTimStart": "2008-07-29T00:00:00+02:00", "md": "3580", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Evaluated where to take pressure points. Down linked the StethoScop.\nMeanwhile reamed single between 3580 and 3566m in preparation for taking pressure point. 2100 lpm, 80 to 120 rpm. Downlinked to set tool (Stethoscope) to standby.\n", "dTimEnd": "2008-07-29T04:00:00+02:00", "dTimStart": "2008-07-29T03:15:00+02:00", "md": "3566", "phase": "fixed", "proprietaryCode": "drilling -- survey", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Send down link to set tool and took pressure point reading:\nBit depth 3565.5m, test depth 3530m.\n", "dTimEnd": "2008-07-29T05:00:00+02:00", "dTimStart": "2008-07-29T04:00:00+02:00", "md": "3565.5", "phase": "fixed", "proprietaryCode": "drilling -- survey", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to drill 8½\" hole from 3580m to 3600m. Drilling parameters: Flow 2100 lpm / SPP 210 bars / String RPM 180 / WOB 5 MT / TQ 26-28 kNm / ROP 16-42 m/hour / ECD 1.594 SG / MUD weight 1.45 SG.\nTook survey after connection. \nParallel operation: Made up 7\" liner in stands and racked back in derrick. Total 27 stds in derrick.\n", "dTimEnd": "2008-07-29T06:00:00+02:00", "dTimStart": "2008-07-29T05:00:00+02:00", "md": "3600", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to drill 8½\" hole from 3600m to 3620m. Drilling parameters: Flow 2100 lpm / SPP 212 bars / String RPM 130-180 / WOB 5-11 MT / TQ 25-30 kNm / ROP 40-50 m/hour / ECD 1.584-1.601 SG / MUD weight 1.45 SG.\nTook survey after connection. Down linked tool.\nStringer uncounted at 3593m\n", "dTimEnd": "2008-07-29T07:15:00+02:00", "dTimStart": "2008-07-29T06:00:00+02:00", "md": "3620", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Send down link to set tool and took pressure point reading:\nBit depth 3585.9m, test depth 3551m.", "dTimEnd": "2008-07-29T08:30:00+02:00", "dTimStart": "2008-07-29T07:15:00+02:00", "md": "3585.9", "phase": "fixed", "proprietaryCode": "drilling -- survey", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to drill 8½\" hole from 3620m to 3661m. Drilling parameters: Flow 2100 lpm / SPP 212 bars / String RPM 130 / WOB 5-11 MT / TQ 25-30 kNm / ROP 40-50 m/hour / ECD 1.584-1.601 SG / MUD weight 1.45 SG.\nTook survey after connection. Down linked tool.", "dTimEnd": "2008-07-29T10:15:00+02:00", "dTimStart": "2008-07-29T08:30:00+02:00", "md": "3661", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Unexplained gain. Lined up on trip tank & observed well, well static\n", "dTimEnd": "2008-07-29T10:30:00+02:00", "dTimStart": "2008-07-29T10:15:00+02:00", "md": "3661", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Send down link to set tool and took pressure point reading:\nBit depth 3648.9m, test depth 3624m.", "dTimEnd": "2008-07-29T11:30:00+02:00", "dTimStart": "2008-07-29T10:30:00+02:00", "md": "3648.9", "phase": "fixed", "proprietaryCode": "drilling -- survey", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to drill 8½\" hole from 3661m to 3742m. Drilling parameters: Flow 2100 lpm / SPP 206 bars / String RPM 130 / WOB 4-11 MT / TQ 19-30 kNm / ROP 4-40 m/hour / ECD 1.585-1.612 SG / MUD weight 1.45 SG.\nTook survey after every connection. Down linked tool.\nSlow drilling from 3712,8m to 3720m.\n", "dTimEnd": "2008-07-29T16:15:00+02:00", "dTimStart": "2008-07-29T11:30:00+02:00", "md": "3742", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Send down link to set tool and took pressure point reading:\nBit depth 3730.9m, test depth 3706m. Bit depth 3720.9m, test depth 3696m.", "dTimEnd": "2008-07-29T17:45:00+02:00", "dTimStart": "2008-07-29T16:15:00+02:00", "md": "3742", "phase": "fixed", "proprietaryCode": "drilling -- survey", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued to drill 8½\" hole from 3742m to 3792m. Drilling parameters: Flow 2100 lpm / SPP 206 bars / String RPM 130 / WOB 4-11 MT / TQ 19-30 kNm / ROP 4-40 m/hour / ECD 1.585-1.612 SG / MUD weight 1.45 SG.\nTook survey after connection. Down linked tool.\n", "dTimEnd": "2008-07-29T22:00:00+02:00", "dTimStart": "2008-07-29T17:45:00+02:00", "md": "3792", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Circulated cuttings clear of BHA, racked back one stand.\n", "dTimEnd": "2008-07-29T22:45:00+02:00", "dTimStart": "2008-07-29T22:00:00+02:00", "md": "3792", "phase": "fixed", "proprietaryCode": "drilling -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Circulated well clean while reciprocating the string. Circulation parameter: Flow 2100 lpm / SPP 190 bars / String RPM 120 / MUD weight 1.45 SG.\nCurculated a total of 3 buttoms up.\n", "dTimEnd": "2008-07-30T00:00:00+02:00", "dTimStart": "2008-07-29T22:45:00+02:00", "md": "3783", "phase": "fixed", "proprietaryCode": "drilling -- other", "state": "ok", "stateDetailActivity": "success" } ]
[ { "dTim": "2008-07-30T00:00:00+02:00", "lithology": "Sandstone and limestone with minor claystone and coal beds", "mdBottom": "3792", "mdTop": "3746", "show": null, "tvdBottom": null, "tvdTop": null } ]
15_9_F_5_2008_07_31
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-30T00:00:00+02:00
2008-07-31T00:00:00+02:00
normal
2018-05-03T13:53:02+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-07-31T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-30T18:45:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "M/U 7\" liner hanger. Continue RIH with 7\" liner on 5½\" DP. Install 7\" liner hanger. Cement 7\" liner hanger and set TSP packer.\n", "hpht": "0", "md": "3792", "mdCsgLast": "3790.1", "mdDiaHoleStart": "3792", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "31", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "POOH with 8½\" BHA. Laid out 8½\" BHA. Rigged up and RIH with 7\" liner from surface to 969m. Picked up 7\" liner hanger.\n\n\n", "tightWell": "0", "tvd": "3247", "tvdCsgLast": "3245.3", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-30T04:00:00+02:00", "density": "1.45", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3792", "mudClass": "oil based", "presBopRating": "345", "pv": "25", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "10" }, { "dTim": "2008-07-30T22:00:00+02:00", "density": "1.45", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3792", "mudClass": "oil based", "presBopRating": "345", "pv": "26", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "10" }, { "dTim": "2008-07-30T08:00:00+02:00", "density": "1.45", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3792", "mudClass": "oil based", "presBopRating": "345", "pv": "26", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "10" } ]
[ { "dTim": "2008-07-31T00:00:00+02:00", "equivalentMudWeight": "1.36", "md": "3792", "readingKind": "estimated" } ]
[]
[ { "comments": "Continued circulated well clean while reciprocating the string. Circulation parameter: Flow 2100 lpm / SPP 190 bars / String RPM 120 / MUD weight 1.45 SG.", "dTimEnd": "2008-07-30T01:15:00+02:00", "dTimStart": "2008-07-30T00:00:00+02:00", "md": "3783", "phase": "fixed", "proprietaryCode": "drilling -- other", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Flow checked well, well static.", "dTimEnd": "2008-07-30T01:30:00+02:00", "dTimStart": "2008-07-30T01:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH wet with 8½\" BHA from 3792m to 3700m.", "dTimEnd": "2008-07-30T02:15:00+02:00", "dTimStart": "2008-07-30T01:30:00+02:00", "md": "3541", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Send down link to set tool and took pressure point reading:\nBit depth 3694m, test depth 3660m. Bit depth 3677m, test depth 3643m. \nWere not able to achieve a good test in stead of StethoScope did not performed which could be interpreted as failure.\n", "dTimEnd": "2008-07-30T03:45:00+02:00", "dTimStart": "2008-07-30T02:15:00+02:00", "md": "3700", "phase": "fixed", "proprietaryCode": "drilling -- survey", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH wet with 8½\" BHA from 3700m to 3580m.", "dTimEnd": "2008-07-30T04:15:00+02:00", "dTimStart": "2008-07-30T03:45:00+02:00", "md": "3580", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Send down link to set tool and took pressure point reading:\nBit depth 3556m, test depth 3522m. \nWere not able to achieve a good test in stead of StethoScope did not performed which could be interpreted as failure.", "dTimEnd": "2008-07-30T06:00:00+02:00", "dTimStart": "2008-07-30T04:15:00+02:00", "md": "3580", "phase": "fixed", "proprietaryCode": "drilling -- survey", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Flow checked well, well static. Pumped 1.65 SG slug 5m³. \n", "dTimEnd": "2008-07-30T06:45:00+02:00", "dTimStart": "2008-07-30T06:00:00+02:00", "md": "3460", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with 8½\" BHA from 3460m to 2813m.\n", "dTimEnd": "2008-07-30T08:30:00+02:00", "dTimStart": "2008-07-30T06:45:00+02:00", "md": "2813", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Took foot print prior to run 7\" liner.\n", "dTimEnd": "2008-07-30T09:00:00+02:00", "dTimStart": "2008-07-30T08:30:00+02:00", "md": "2813", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Observed well on trip tank. Meanwhile serviced TDS and checked dies in PRS.\n", "dTimEnd": "2008-07-30T09:30:00+02:00", "dTimStart": "2008-07-30T09:00:00+02:00", "md": "2813", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH wet with 8½\" BHA form 2813m to 2530m. Trip time 1132 m/hour. \n", "dTimEnd": "2008-07-30T09:45:00+02:00", "dTimStart": "2008-07-30T09:30:00+02:00", "md": "2530", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pumped 1.65 SG slug 5m³. \n", "dTimEnd": "2008-07-30T10:15:00+02:00", "dTimStart": "2008-07-30T09:45:00+02:00", "md": "2530", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH wet with 8½\" BHA form 2530m to 1320m. Trip time 807 m/hour. \n", "dTimEnd": "2008-07-30T12:00:00+02:00", "dTimStart": "2008-07-30T10:15:00+02:00", "md": "1320", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Changed to 5\" handling equipment.\n", "dTimEnd": "2008-07-30T12:30:00+02:00", "dTimStart": "2008-07-30T12:00:00+02:00", "md": "1320", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH wet with 8½\" BHA form 1320m to 221m. Trip time 628 m/hour. \n", "dTimEnd": "2008-07-30T14:15:00+02:00", "dTimStart": "2008-07-30T12:30:00+02:00", "md": "221", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Flow checked well prior to pull the BHA. Erected barriers prior to handling radioactive source.\n", "dTimEnd": "2008-07-30T14:30:00+02:00", "dTimStart": "2008-07-30T14:15:00+02:00", "md": "221", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled the last 3 stds 5\" DP from 221m to 99m. Removed auto slips. Removed Totco ring and drift from top single of HWDP.\n", "dTimEnd": "2008-07-30T15:00:00+02:00", "dTimStart": "2008-07-30T14:30:00+02:00", "md": "99", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to POOH with BHA and lay out same..\n", "dTimEnd": "2008-07-30T15:15:00+02:00", "dTimStart": "2008-07-30T15:00:00+02:00", "md": "99", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH and laid out 8½\" BHA. Found damaged StethoScope seals.\n", "dTimEnd": "2008-07-30T18:15:00+02:00", "dTimStart": "2008-07-30T15:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- trip", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cleared and cleaned rig floor.\n", "dTimEnd": "2008-07-30T18:45:00+02:00", "dTimStart": "2008-07-30T18:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- drill", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged up from running 7\" liner.", "dTimEnd": "2008-07-30T21:30:00+02:00", "dTimStart": "2008-07-30T18:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk prior to RIH with 7\" liner.", "dTimEnd": "2008-07-30T21:45:00+02:00", "dTimStart": "2008-07-30T21:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up and made up shoe track. Checked the integrity of the shoe.\n", "dTimEnd": "2008-07-30T22:00:00+02:00", "dTimStart": "2008-07-30T21:45:00+02:00", "md": "10", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Waited on crane due to helicopter.\n", "dTimEnd": "2008-07-30T22:15:00+02:00", "dTimStart": "2008-07-30T22:00:00+02:00", "md": "10", "phase": "fixed", "proprietaryCode": "drilling -- wait", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up float jt & landing collar jt. RIH from 10m to 37m.\n", "dTimEnd": "2008-07-30T23:30:00+02:00", "dTimStart": "2008-07-30T22:15:00+02:00", "md": "37", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued RIH 7\" liner in stands from 37m to 130m. Filled every 2'ed stds.Trip time 186 m/hour (15.5 jnt/hour)\n", "dTimEnd": "2008-07-31T00:00:00+02:00", "dTimStart": "2008-07-30T23:30:00+02:00", "md": "130", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_08_01
NO 15/9-F-5
NO 15/9-F-5
name
2008-07-31T00:00:00+02:00
2008-08-01T00:00:00+02:00
normal
2018-05-03T13:53:02+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-08-01T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-30T18:45:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Circulate out excess cement. POOH with liner setting tool. Perform maintenance on TDS.", "hpht": "0", "md": "3792", "mdCsgLast": "3790.1", "mdDiaHoleStart": "3792", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": null, "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "32", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Made up liner hanger assy. RIH with liner hanger on 5 1/2\" DP and tagged TD at 3793 m MD. Set liner hanger and released RT. Conditioned mud. Cemented 7\" liner. Set TSP packer.Tested TSP packer to 280 bar. Circulated out excess cement. ", "tightWell": "0", "tvd": "3247", "tvdCsgLast": "3245.3", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-07-31T23:59:00+02:00", "density": "1.45", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3792", "mudClass": "oil based", "presBopRating": "345", "pv": "26", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "10" }, { "dTim": "2008-07-31T15:45:00+02:00", "density": "1.45", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3792", "mudClass": "oil based", "presBopRating": "345", "pv": "26", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "10" } ]
[]
[]
[ { "comments": "Continued RIH 7\" liner in stands from 130m to 355m. Filled every 2'ed stds.Trip time 150 m/hour (12.5 jnt/hour)\n", "dTimEnd": "2008-07-31T01:30:00+02:00", "dTimStart": "2008-07-31T00:00:00+02:00", "md": "355", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed pup jts & PIP tag from 355m to 364m\n", "dTimEnd": "2008-07-31T02:15:00+02:00", "dTimStart": "2008-07-31T01:30:00+02:00", "md": "364", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued RIH 7\" liner in stands from 364m to 863m. Filled every 2'ed stds. Trip time 222 m/hour (18.5 jnt/hour)\n", "dTimEnd": "2008-07-31T04:30:00+02:00", "dTimStart": "2008-07-31T02:15:00+02:00", "md": "863", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk and re-arranged 7\" liner stds FWD in set back area. To be able to reach with AFT PRS.\n", "dTimEnd": "2008-07-31T05:00:00+02:00", "dTimStart": "2008-07-31T04:30:00+02:00", "md": "863", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued RIH 7\" liner in stands from 863m to 969m. Filled every 2'ed stds. Trip time 212 m/hour. (17.5 jnt/hour)\n", "dTimEnd": "2008-07-31T05:30:00+02:00", "dTimStart": "2008-07-31T05:00:00+02:00", "md": "969", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tool box talk and picked up 7\" liner hanger.", "dTimEnd": "2008-07-31T06:00:00+02:00", "dTimStart": "2008-07-31T05:30:00+02:00", "md": "969", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up liner hanger assy to 7\" liner.", "dTimEnd": "2008-07-31T07:00:00+02:00", "dTimStart": "2008-07-31T06:00:00+02:00", "md": "969", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox handover meeting.", "dTimEnd": "2008-07-31T07:15:00+02:00", "dTimStart": "2008-07-31T07:00:00+02:00", "md": "969", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed masterbushing and bowls. Installed RA marker in pup joint below hanger. Ran Liner hanger assy through rotary. Checked shear pins on hanger.", "dTimEnd": "2008-07-31T07:30:00+02:00", "dTimStart": "2008-07-31T07:15:00+02:00", "md": "980", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Filled PBR with drillwater.", "dTimEnd": "2008-07-31T07:45:00+02:00", "dTimStart": "2008-07-31T07:30:00+02:00", "md": "988", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged down Odfjell tong and FMS. Changed eleavator inserts from 5\" to 5 1/2\".", "dTimEnd": "2008-07-31T08:30:00+02:00", "dTimStart": "2008-07-31T07:45:00+02:00", "md": "988", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up TDS and filled string with OBM from active.", "dTimEnd": "2008-07-31T08:45:00+02:00", "dTimStart": "2008-07-31T08:30:00+02:00", "md": "988", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk. Removed masterbshing and intalled automatic slips in rotary.", "dTimEnd": "2008-07-31T09:15:00+02:00", "dTimStart": "2008-07-31T08:45:00+02:00", "md": "988", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Ran 7\" liner / liner hanger on 5 1/2\" DP from 988 m to 1082 m MD. Picked up singles from cantilever (7 ea).", "dTimEnd": "2008-07-31T10:15:00+02:00", "dTimStart": "2008-07-31T09:15:00+02:00", "md": "1082", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Ran 7\" liner / liner hanger on 5 1/2\" DP from 1082 m to 2899 m MD.", "dTimEnd": "2008-07-31T15:15:00+02:00", "dTimStart": "2008-07-31T10:15:00+02:00", "md": "2899", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke circulation at 9 5/8\" casing shoe. Circulated 1 x liner volume (~20 m3) at 1150 lpm / 55 bar SPP. Took up/down weights 162/126 MT.", "dTimEnd": "2008-07-31T16:00:00+02:00", "dTimStart": "2008-07-31T15:15:00+02:00", "md": "2899", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Ran 7\" liner / liner hanger on 5 1/2 DP from 2899 m to 3746 m MD.", "dTimEnd": "2008-07-31T18:30:00+02:00", "dTimStart": "2008-07-31T16:00:00+02:00", "md": "3746", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up TDS and washed down 7\" liner from 3746 m to 3787 m MD at 500 lpm / 42 bar SPP. Meanwhile made up and tested cement hose to cement head laying on the HTS.", "dTimEnd": "2008-07-31T19:30:00+02:00", "dTimStart": "2008-07-31T18:30:00+02:00", "md": "3787", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up cement head with 6 m pup to string. Made up TDS to cement head. Took up/down weights 200/137 MT.", "dTimEnd": "2008-07-31T20:00:00+02:00", "dTimStart": "2008-07-31T19:30:00+02:00", "md": "3787", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH while circulating at 500 lpm and tagged TD at 3793,3 m with 10 MT.", "dTimEnd": "2008-07-31T20:15:00+02:00", "dTimStart": "2008-07-31T20:00:00+02:00", "md": "3793", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up ~1 m and to located liner hanger at setting depth. Increased rate in increments to 1000 lpm / SPP 76 bar. Set torque limit to 34 kNm. Commenced rotation and increased rotation in increments to 20 rpm. Rotating torque 23-26 kNm.", "dTimEnd": "2008-07-31T20:45:00+02:00", "dTimStart": "2008-07-31T20:15:00+02:00", "md": "3792", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Dropped liner hanger setting ball and chased same with 500 lpm.", "dTimEnd": "2008-07-31T21:15:00+02:00", "dTimStart": "2008-07-31T20:45:00+02:00", "md": "3792", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Observed pressure build up when setting ball seated after 712 strokes. Pressured up to 160 bar to set liner hanger and maintainted pressure for 2 min. Verified hanger set by slacking off weight to 105 MT (30 MT applied) - ok. Bled off stand pipe pressure. Released liner hanger running tool with 12 clockwise rotations. Took up/down weights 155/123 MT - running tool free.", "dTimEnd": "2008-07-31T22:00:00+02:00", "dTimStart": "2008-07-31T21:15:00+02:00", "md": "3792", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Sheared ball seat by applying pressure on DP. Ballseat sheared out at 251 bar.", "dTimEnd": "2008-07-31T22:15:00+02:00", "dTimStart": "2008-07-31T22:00:00+02:00", "md": "3792", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Stepped up rate in 500 lpm increments to check for stable returns / loss free rate. 500 lpm / 38 bar SPP. 1000 lpm / 66 bar SPP. 1500 lpm / 110 bar SPP. No losses observed.", "dTimEnd": "2008-07-31T23:00:00+02:00", "dTimStart": "2008-07-31T22:15:00+02:00", "md": "3792", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Decreasead rate to 1000 lpm and started rotating at 20 rpm. Torque 12-16 kNm. Increased rate to 1500 lpm and cirucalted bottoms up while rotating at 20 rpm. Meanwhile held prejob meeting prior to cementing.", "dTimEnd": "2008-08-01T00:00:00+02:00", "dTimStart": "2008-07-31T23:00:00+02:00", "md": "3792", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_08_02
NO 15/9-F-5
NO 15/9-F-5
name
2008-08-01T00:00:00+02:00
2008-08-02T00:00:00+02:00
normal
2018-05-03T13:53:02+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-08-02T00:00:00+02:00", "dTimDiaHoleStart": "2008-07-30T18:45:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Make up 7\" cleaning assemblies and RIH on 3 1/2\" DP singles to 920 m MD. Make up 9 5/8\" cleaning assemblies. Scrape VBM plug setting area. Make up 10 3/4\" cleaning assemblies.", "hpht": "0", "md": "3792", "mdCsgLast": "3790.1", "mdDiaHoleStart": "3792", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3754", "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "33", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Circulated out excess cement. Cleaned string with sponges. POOH with liner hanger running tool from 2820 m to 121 m MD. Broke pup from cement head. Pulled and laid out 7 ea singles. Laid out liner hanger running tool. Pressure tested casing/liner to 280 bar against shear ram. Cleaned BOP and drilling riser with jet sub and wellprotector. Prepared for running well cleaning string.", "tightWell": "0", "tvd": "3247", "tvdCsgLast": "3245.3", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-08-01T21:00:00+02:00", "density": "1.45", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3792", "mudClass": "oil based", "presBopRating": "345", "pv": "25", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "10.5" } ]
[]
[]
[ { "comments": "Circulated bottoms up at 1500 lpm while rotating string at 20 rpm.", "dTimEnd": "2008-08-01T00:30:00+02:00", "dTimStart": "2008-08-01T00:00:00+02:00", "md": "3792", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pumped 8 m3 baseoil followed by 15 m3 tuned spacer E+ and 3 m3 baseoil. Pumprate 1000-1500 lpm. Rotated string at 20 rpm. Released lower DP dart.", "dTimEnd": "2008-08-01T01:15:00+02:00", "dTimStart": "2008-08-01T00:30:00+02:00", "md": "3792", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up cement unit. Mixed and pumped 21,6 m3 1,90 sg cement at 840 lpm. Pump pressure 60-100 bar. Displaced cement with 890 litres of drillwater and closed lo-torque to cement head. Released upper DP dart.", "dTimEnd": "2008-08-01T02:00:00+02:00", "dTimStart": "2008-08-01T01:15:00+02:00", "md": "3792", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Displaced cement with 1,45 sg OBM using rig pumps. Pump rate 1200-1600 lpm. Observed shear of lower wiper plug at 432 strokes pumped, sheared out at 230 bar pressure. Observed bottom wiper plug in landing collar at 1254 strokes, sheared out at 74 bar. Observed no shear/pressure peak when upper dart landed in upper wiper plug. Observed pressure bulid up from 5 bar to 136 bar when cement entered annulus after ~1300 strokes. Reduced rate to 500 lpm after 2130 strokes. Bumped plug after 2228 strokes with 190 bar (FCP ~100 bar). Pump effciency 97,8%. No losses observed during displacement.", "dTimEnd": "2008-08-01T02:45:00+02:00", "dTimStart": "2008-08-01T02:00:00+02:00", "md": "3792", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Bled off pressure on standpipe to ~5 bar. Pressure increased to 16 bar in 10 min. Lined up to trip tank and observed for backflow. Observed ~50 liter increase in 20 min. Broke off cement hose on drillflloor and drained to trip tank. Observed flow from hose after draining cement head. Took 3 consecutive measurements on back flow rate - 33 sec/l - 37 sec/l - 40 sec/l - rate steadily decreasing - ok.", "dTimEnd": "2008-08-01T04:00:00+02:00", "dTimStart": "2008-08-01T02:45:00+02:00", "md": "3792", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up string to engage TSP packer actutating dogs. Set down 30 MT to set TSP packer. Observed dual shear - ok.", "dTimEnd": "2008-08-01T04:30:00+02:00", "dTimStart": "2008-08-01T04:00:00+02:00", "md": "3792", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up cement unit to BOP kill inlet. Closed BOP. Pressure tested TSP packer to 280 bar / 10 min. Pressure drop 1,8 bar (0,64%) with improving trend.", "dTimEnd": "2008-08-01T05:30:00+02:00", "dTimStart": "2008-08-01T04:30:00+02:00", "md": "3792", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Circulated out excess cement.", "dTimEnd": "2008-08-01T06:00:00+02:00", "dTimStart": "2008-08-01T05:30:00+02:00", "md": "2820", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Circulated out excess cement at 2000 lpm.", "dTimEnd": "2008-08-01T07:00:00+02:00", "dTimStart": "2008-08-01T06:00:00+02:00", "md": "2820", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Ran liner hanger running tool back into PBR to position coupling for breaking out cement head.", "dTimEnd": "2008-08-01T07:15:00+02:00", "dTimStart": "2008-08-01T07:00:00+02:00", "md": "2820", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk for laying out cement head.", "dTimEnd": "2008-08-01T07:30:00+02:00", "dTimStart": "2008-08-01T07:15:00+02:00", "md": "2820", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Disconnected lo-torques, cement hose and hydraulic control lines from cement head. Broke and laid out cement head with 6 m DP pup.", "dTimEnd": "2008-08-01T08:00:00+02:00", "dTimStart": "2008-08-01T07:30:00+02:00", "md": "2812", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Inserted sponge balls. Made up TDS and pulled free of PBR with liner hanger running tool. Circulated 1,5 x string volume at 2000 lpm / SPP 68 bar to clean DP.", "dTimEnd": "2008-08-01T08:45:00+02:00", "dTimStart": "2008-08-01T08:00:00+02:00", "md": "2785", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with liner hanger running tool on 5 1/2\" DP from 2785 m to 121 m MD. Tripping speed 888 m/hrs.", "dTimEnd": "2008-08-01T11:45:00+02:00", "dTimStart": "2008-08-01T08:45:00+02:00", "md": "121", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Function tested BOP. Meanwhile held toolbox talk for breaking cement head.", "dTimEnd": "2008-08-01T12:00:00+02:00", "dTimStart": "2008-08-01T11:45:00+02:00", "md": "121", "phase": "fixed", "proprietaryCode": "drilling -- bop activities", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up cement head with 6 m pup from HTS and made up same to string to ease breaking out pup joint. Broke off 6 m pup joint. Laid out cement head.", "dTimEnd": "2008-08-01T12:15:00+02:00", "dTimStart": "2008-08-01T12:00:00+02:00", "md": "121", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with liner hanger running tool on 5 1/2\" DP from 121 m to 27 m MD. Laid out 7 x ea 5 1/2\" DP singles.", "dTimEnd": "2008-08-01T13:45:00+02:00", "dTimStart": "2008-08-01T12:15:00+02:00", "md": "27", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Took time out for safety meeting adressing forthcomming operations with manrider.", "dTimEnd": "2008-08-01T14:15:00+02:00", "dTimStart": "2008-08-01T13:45:00+02:00", "md": "27", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed automatic slips. Pulled liner hanger running tool through rotary. Reset tool according to Weatherford instructions. Laid out and inspected tool - ok.\n\n****Operations transferred to F-99*****", "dTimEnd": "2008-08-01T15:15:00+02:00", "dTimStart": "2008-08-01T14:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_08_03
NO 15/9-F-5
NO 15/9-F-5
name
2008-08-02T00:00:00+02:00
2008-08-03T00:00:00+02:00
normal
2018-05-03T13:53:02+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-08-03T00:00:00+02:00", "dTimDiaHoleStart": "2008-08-02T01:15:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Scrape packer setting area. Dress and polish PBR. Inflow test liner using well commissioner and base oil. Pump wash pills, clean well and displace to packer fluid. Clean surface lines and pits. Pressure test well to 345 bar.", "hpht": "0", "md": "3792", "mdCsgLast": "3790.1", "mdDiaHoleStart": "3792", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3754", "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "34", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Made up and ran 7\" x 9 5/8\" x 10 3/4\" cleaning string from surface to 3654 m MD.", "tightWell": "0", "tvd": "3247", "tvdCsgLast": "3245.3", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-08-02T15:30:00+02:00", "density": "1.44", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3792", "mudClass": "oil based", "presBopRating": "345", "pv": "26", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "10" }, { "dTim": "2008-08-02T22:30:00+02:00", "density": "1.45", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3792", "mudClass": "oil based", "presBopRating": "345", "pv": "25", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "10.5" } ]
[]
[]
[ { "comments": "Picked up well protector assy and hung off same in rotary. RIH with well protector on 5 1/2\" DP to 170 m MD. Made up magnet / 11\" jet-sub assy.", "dTimEnd": "2008-08-02T02:15:00+02:00", "dTimStart": "2008-08-02T01:15:00+02:00", "md": "170", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH and Jetted accross BOP with 1500 lpm / 10 bar SPP.", "dTimEnd": "2008-08-02T02:30:00+02:00", "dTimStart": "2008-08-02T02:15:00+02:00", "md": "190", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Spaced out and located jet sub underneath BOP. Functioned BOP pipe rams and annular.", "dTimEnd": "2008-08-02T02:45:00+02:00", "dTimStart": "2008-08-02T02:30:00+02:00", "md": "190", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Reciprocated string and made 3 passes across BOP with jet sub.", "dTimEnd": "2008-08-02T03:00:00+02:00", "dTimStart": "2008-08-02T02:45:00+02:00", "md": "190", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH on 5 1/2\" DP from 190 m to 310 m MD. Made up TDS to each stand. Washed drilling riser with 1800-3000 lpm while running in.", "dTimEnd": "2008-08-02T04:00:00+02:00", "dTimStart": "2008-08-02T03:00:00+02:00", "md": "310", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with wellprotector / jet sub on 5 1/2\" DP from 310 m MD to surface. Laid out jet sub and well protector. Recovered approx 300 g swarf and cuttings in well protector (1-5 cm).", "dTimEnd": "2008-08-02T05:30:00+02:00", "dTimStart": "2008-08-02T04:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged up for running 3 1/2\" DP. Changed dies in IR. Changed inserts in DP elevator. Prepared PS-21 slips. Lifted cleaning assy #1 and #2 onto HTS.", "dTimEnd": "2008-08-02T06:00:00+02:00", "dTimStart": "2008-08-02T05:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Changed dies in IR. Cleared and tidied drillfloor. Picked up and hung off cleaning assy #1 - 6\" PDC bit and pup in manual slips. Picked up and made up cleaning assy #2 - 7\" razor back / well sweep magnets.", "dTimEnd": "2008-08-02T07:00:00+02:00", "dTimStart": "2008-08-02T06:00:00+02:00", "md": "12", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox / handover meeting.", "dTimEnd": "2008-08-02T07:30:00+02:00", "dTimStart": "2008-08-02T07:00:00+02:00", "md": "12", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Reconfigured HTS rollers on cantilever. Removed masterbushing and installed PS-21 slips in rotary.", "dTimEnd": "2008-08-02T07:45:00+02:00", "dTimStart": "2008-08-02T07:30:00+02:00", "md": "12", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up 3 1/2\" singles from deck and RIH with cleaning assemblies from 12 m to 559 m MD. Observed that a 3 1/2\" DP single was caught by the PDM and dislogded on the HTS rolles.", "dTimEnd": "2008-08-02T11:00:00+02:00", "dTimStart": "2008-08-02T07:45:00+02:00", "md": "559", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Took time out for safety. Investigated situation. Probable cause was that the pipe was staggered relative to the rest when being picked up, or that it had bounced off the rollers when the PDM grip was released.", "dTimEnd": "2008-08-02T12:15:00+02:00", "dTimStart": "2008-08-02T11:00:00+02:00", "md": "559", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued picking up 3 1/2\" singles and RIH with cleaning assemblies from 559 m to 910 m MD.", "dTimEnd": "2008-08-02T14:15:00+02:00", "dTimStart": "2008-08-02T12:15:00+02:00", "md": "910", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk. Changed from 3 1/2\" to 5 1/2\" handing equipment. Changed die-holders and dies in IR. Placed cleaning assy #3 - top-dress/polish mill / well commissioner / 9 5/8\" razor back / wellsweep magnets, on HTS.", "dTimEnd": "2008-08-02T14:45:00+02:00", "dTimStart": "2008-08-02T14:15:00+02:00", "md": "910", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up and made up celaning assembly #3. Picked up and made up cleaning assembly #4 - MFCT / well patroller / wellsweep magnets.", "dTimEnd": "2008-08-02T15:45:00+02:00", "dTimStart": "2008-08-02T14:45:00+02:00", "md": "950", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up stand of 5 1/2\" DP. Made up TDS. Broke circulation and stepped up pumps to 1000 lpm / 88 bar SPP. Took up/down weights 82/85 MT.", "dTimEnd": "2008-08-02T16:00:00+02:00", "dTimStart": "2008-08-02T15:45:00+02:00", "md": "991", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk prior to slip and cut drill line.", "dTimEnd": "2008-08-02T16:30:00+02:00", "dTimStart": "2008-08-02T16:00:00+02:00", "md": "991", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Hung off travelling block. Slipped and cut drill line according to Mærsk procedure. Meanwhile worked on AFT PRS.", "dTimEnd": "2008-08-02T20:30:00+02:00", "dTimStart": "2008-08-02T16:30:00+02:00", "md": "991", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up travelling block.", "dTimEnd": "2008-08-02T20:45:00+02:00", "dTimStart": "2008-08-02T20:30:00+02:00", "md": "991", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Calibrated travelling block.", "dTimEnd": "2008-08-02T21:00:00+02:00", "dTimStart": "2008-08-02T20:45:00+02:00", "md": "991", "phase": "fixed", "proprietaryCode": "interruption -- maintain", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with cleaning assemblies on 5 1/2\" DP from 991 m to 1554 m MD. Meanwhile rigged up casing tong for doing paralell operations.", "dTimEnd": "2008-08-02T22:30:00+02:00", "dTimStart": "2008-08-02T21:00:00+02:00", "md": "1554", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Scraped and cleaned VBM plug setting depth in 9 5/8\" casing at 640 m MD +/- 15 m. Made 2 passes with scrapers circulating at 1900 lpm / SPP 270 bar. Observed hydraulic leakaged from elevator.", "dTimEnd": "2008-08-02T23:00:00+02:00", "dTimStart": "2008-08-02T22:30:00+02:00", "md": "1584", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Not able to access leakage point. Changed DP elevator.", "dTimEnd": "2008-08-02T23:30:00+02:00", "dTimStart": "2008-08-02T23:00:00+02:00", "md": "1594", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "RIH with cleaning assemblies on 5 1/2\" DP from 1594 m to 1748 m MD.", "dTimEnd": "2008-08-03T00:00:00+02:00", "dTimStart": "2008-08-02T23:30:00+02:00", "md": "1748", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_08_04
NO 15/9-F-5
NO 15/9-F-5
name
2008-08-03T00:00:00+02:00
2008-08-04T00:00:00+02:00
normal
2018-05-03T13:53:02+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-08-04T00:00:00+02:00", "dTimDiaHoleStart": "2008-08-02T01:15:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "POOH with cleaning string from 3011 m MD to surface. Set VMB plug at 640 m MD. Pull wearbushing. Set 10 3/4\" casing hanger lock down sub.", "hpht": "0", "md": "3792", "mdCsgLast": "3790.1", "mdDiaHoleStart": "3792", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3754", "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "35", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Drilled/scraped cement to 3735 m MD. Tagged TOL at 2809,5 m MD. Dressed off PBR. Inflow tested well using well commissioner and base oil. Pumped displacement train. Cleaned well with SW and displaced to packer fluid. Tested well to 345 bar. POOH with cleaning assemblies to 3011 m MD.", "tightWell": "0", "tvd": "3247", "tvdCsgLast": "3245.3", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-08-03T11:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "3972", "mudClass": "other", "presBopRating": "345", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" }, { "dTim": "2008-08-03T14:00:00+02:00", "density": "1.44", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3792", "mudClass": "oil based", "presBopRating": "345", "pv": "25", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "10" } ]
[]
[]
[ { "comments": "RIH with cleaning assemblies on 5 1/2\" DP from 1748 m to 2804 m MD.", "dTimEnd": "2008-08-03T01:45:00+02:00", "dTimStart": "2008-08-03T00:00:00+02:00", "md": "2804", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Took up/down weights 147/121 MT. Free rotating weight 132 MT. Free rotating torque at 20 rpm was 9 kNm. Circulated 50 m3 OBM at 1900 lpm / 285 bar to condition mud.", "dTimEnd": "2008-08-03T02:15:00+02:00", "dTimStart": "2008-08-03T01:45:00+02:00", "md": "2804", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Entered PBR with 6\" bit while rotating 20 rpm and circulating at 500 lpm / SPP 37 bar. No obstruction observed.", "dTimEnd": "2008-08-03T02:30:00+02:00", "dTimStart": "2008-08-03T02:15:00+02:00", "md": "2815", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with cleaning assemblies on 5 1/2\" DP from 2815 m to 2868 m MD.", "dTimEnd": "2008-08-03T03:00:00+02:00", "dTimStart": "2008-08-03T02:30:00+02:00", "md": "2868", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Elevator not functioning correctly on given commands. Changed back to original elevator which had been fixed.", "dTimEnd": "2008-08-03T03:45:00+02:00", "dTimStart": "2008-08-03T03:00:00+02:00", "md": "2868", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued to RIH with cleaning assemblies on 5 1/2\" DP from 2868 m to 3131 m MD.", "dTimEnd": "2008-08-03T04:00:00+02:00", "dTimStart": "2008-08-03T03:45:00+02:00", "md": "3131", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up and made up 2 x 5 1/2\" DP singles. Picked up and made up cleaning assy #5 - 10 3/4\" razor back / posi drift / well sweep magnets / well patroller.", "dTimEnd": "2008-08-03T04:30:00+02:00", "dTimStart": "2008-08-03T04:00:00+02:00", "md": "3170", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with cleaning assemblies on 5 1/2\" DP from 3170 m MD to 3654 m MD.", "dTimEnd": "2008-08-03T06:00:00+02:00", "dTimStart": "2008-08-03T04:30:00+02:00", "md": "3654", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up 5 1/2\" singel. Took weight at 3656 m MT. Scraped cement from 3656 m to 3668 m MD. Parameters : Flow 1640 lpm / 270 bar SPP / 50 rpm / torque 15 kNm.", "dTimEnd": "2008-08-03T07:15:00+02:00", "dTimStart": "2008-08-03T06:00:00+02:00", "md": "3668", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up full stand of 5 1/2\" to scrape cement. Scraped cement from 3668 m MD to 3708. Parameters : Flow 1640 lpm / 260 bar SPP / 50 rpm / torque 15 kNm.", "dTimEnd": "2008-08-03T09:00:00+02:00", "dTimStart": "2008-08-03T07:15:00+02:00", "md": "3708", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Set back stand and replaced with 3 x 5 1/2\" singles picked up from deck. Ran back to 3708 m MD.", "dTimEnd": "2008-08-03T09:45:00+02:00", "dTimStart": "2008-08-03T09:00:00+02:00", "md": "3708", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Scraped cement from 3708 m to 3735 m MD. Parameters : Flow 1640 lpm / 256 bar SPP / 50 rpm / torque 15 kNm.", "dTimEnd": "2008-08-03T11:15:00+02:00", "dTimStart": "2008-08-03T09:45:00+02:00", "md": "3735", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Entered PBR while rotatiing 40 rpm and circulating at 1000 lpm. TOL tagged at 2809,5 m MD. Dressed off PBR with 30 rpm, torqued up to 17 kNm.", "dTimEnd": "2008-08-03T11:45:00+02:00", "dTimStart": "2008-08-03T11:15:00+02:00", "md": "3739", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up to place polish mill ~5 m above PBR. Circulated 2,5 x liner volume at 1800 lpm / SPP 295 bar / 60 rpm.", "dTimEnd": "2008-08-03T12:30:00+02:00", "dTimStart": "2008-08-03T11:45:00+02:00", "md": "3727", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Entered PBR while rotating 30 rpm. Sheared MFCT open by setting down 30 MT.", "dTimEnd": "2008-08-03T12:45:00+02:00", "dTimStart": "2008-08-03T12:30:00+02:00", "md": "3739", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Circulated 1.5 x well volume above TOL at 4000 lpm / SPP 270 bar / 60 rpm / torque 10 kNm.", "dTimEnd": "2008-08-03T13:30:00+02:00", "dTimStart": "2008-08-03T12:45:00+02:00", "md": "3739", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cycled MFCT to closed position according to SPS instructions. Confirmed closed MFCT by pumping 1600 lpm / SPP 230 bar - ok.", "dTimEnd": "2008-08-03T13:45:00+02:00", "dTimStart": "2008-08-03T13:30:00+02:00", "md": "3739", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Set well commissioner packer by setting down 20 MT. Closed MPR. Tested packer to 70 bar-using rig pumps - ok.", "dTimEnd": "2008-08-03T14:15:00+02:00", "dTimStart": "2008-08-03T13:45:00+02:00", "md": "3739", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up weight to unset packer. Pumped 1640 lpm / SPP 230 bar to confirm MFCT still closed.", "dTimEnd": "2008-08-03T14:45:00+02:00", "dTimStart": "2008-08-03T14:15:00+02:00", "md": "3735", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Displaced choke and kill line to base oil through standpipe #1.", "dTimEnd": "2008-08-03T15:30:00+02:00", "dTimStart": "2008-08-03T14:45:00+02:00", "md": "3735", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pumped 33,9 m3 base oil through one standpipe and down the DP at 340 lpm. Circulated welll on trip tank to confirm stable. U-tube pressure 153 bar before setting well commissioner.", "dTimEnd": "2008-08-03T17:30:00+02:00", "dTimStart": "2008-08-03T15:30:00+02:00", "md": "3739", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Set well commissioner by setting down 20 MT. Lined up to cement unit and bled off well in stages to 12 bar. Bled back 750 liter.", "dTimEnd": "2008-08-03T18:15:00+02:00", "dTimStart": "2008-08-03T17:30:00+02:00", "md": "3739", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Inflow tested well. Pressure rose 6,6 bar in 30 min. Bled down pressure again and held test for another 45 min, test levelled out towards end, dropped 0,2 bar last 10 min. Equalised well commissioner by pressuring up to 153 bar. Picked up 7 m and unset well commissioner packer.", "dTimEnd": "2008-08-03T19:45:00+02:00", "dTimStart": "2008-08-03T18:15:00+02:00", "md": "3733", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Displaced lines and manifolds to seawater using cement unit. Filled soap in trip tanks.", "dTimEnd": "2008-08-03T21:00:00+02:00", "dTimStart": "2008-08-03T19:45:00+02:00", "md": "3732", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held tolbox meeting prior to pumping displacement train.", "dTimEnd": "2008-08-03T21:15:00+02:00", "dTimStart": "2008-08-03T21:00:00+02:00", "md": "3732", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pumped well cleaning fluids : 10 m3 dope cleaning pill, 30 m3 hi-vis push pill, 15 m3 hi-vis soap pill, 10 m3 hi-vis soap pill, 10 m3 seawater and 15 m3 hi-vis soap pill. Routed OBM returns to pits. Pump rate 1500-3000 lpm / SPP 270-290 bar. Rotated at 50 rpm and reciporcated string while pumping. Observed torque values up to 27 kNm when baseoil travelled up annulus.", "dTimEnd": "2008-08-03T22:30:00+02:00", "dTimStart": "2008-08-03T21:15:00+02:00", "md": "3732", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Reset stroke counter. Pumped 20 m3 seawater, 20 m3 packer fluid and 31 m3 seawater to place the packer fluid in the 7\" liner. Pump rate 2600-3500 lpm / SPP 270-290 bar.", "dTimEnd": "2008-08-03T23:00:00+02:00", "dTimStart": "2008-08-03T22:30:00+02:00", "md": "3733", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Ran in while rotating and opened MFCT / set well commissioner by setting down 20 MT on the liner top.", "dTimEnd": "2008-08-03T23:15:00+02:00", "dTimStart": "2008-08-03T23:00:00+02:00", "md": "3733", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Maintained 20 MT on MFCT / well commisioner and continued pumping. Pumped seawater at 3100-4000 lpm / SPP 80-130 bar / 60 rpm.", "dTimEnd": "2008-08-04T00:00:00+02:00", "dTimStart": "2008-08-03T23:15:00+02:00", "md": "3739", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_08_05
NO 15/9-F-5
NO 15/9-F-5
name
2008-08-04T00:00:00+02:00
2008-08-05T00:00:00+02:00
normal
2018-05-03T13:53:02+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-08-05T00:00:00+02:00", "dTimDiaHoleStart": "2008-08-02T01:15:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Test VMB plug from above to 345 bar. Set wearbushing. Set 10 3/4\" lock down sub. Nipple down diverter and BOP. Make up claxton tool. Remove tensioner assy on Centralizer deck.", "hpht": "0", "md": "3792", "mdCsgLast": "3790.1", "mdDiaHoleStart": "3792", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3754", "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "36", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "POOH with cleaning string to 920 m MD. Laid down cleaning assy#4 and #3. Not able to rack 3 1/2\" DP. Troubleshot situation with FWD/AFT PRS. POOH with 3 1/2\" DP and racked back in derrick. Laid down cleaning assy #2 and #1. RIH and set 9 5/8\" VMB plug at 637 m MD. Tested below plug to 380 bar. Spotted hi-vis and POOH with running tool.", "tightWell": "0", "tvd": "3247", "tvdCsgLast": "3245.3", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-08-04T19:30:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3792", "mudClass": "other", "presBopRating": "345", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" }, { "dTim": "2008-08-04T12:30:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "3972", "mudClass": "other", "presBopRating": "345", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" }, { "dTim": "2008-08-04T15:00:00+02:00", "density": "1.45", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "3790", "mudClass": "oil based", "presBopRating": "345", "pv": "26", "tempHthp": "120", "type": "OBM-Standard", "visFunnel": "-999.99", "yp": "9.5" }, { "dTim": "2008-08-04T00:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3792", "mudClass": "other", "presBopRating": "345", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[]
[]
[ { "comments": "Pumped seawater at 3100-4000 lpm / SPP 80-130 bar / 60 rpm. Took consecutive NTU readings on seawater returns: 398/317/224/166/411/580/491/799/1000+/780. Pumped a total of 180 m3 seawater.", "dTimEnd": "2008-08-04T00:15:00+02:00", "dTimStart": "2008-08-04T00:00:00+02:00", "md": "3739", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Stopped rotation. Pumped packer fluid at 3800 lpm / SPP 118 bar. Took consecutive NTU reading on packer fluid returns: 106/89/80/121/250/130/111/115/125/115. Pumped a total of 270 m3 packer fluid.", "dTimEnd": "2008-08-04T01:30:00+02:00", "dTimStart": "2008-08-04T00:15:00+02:00", "md": "3739", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up to unset well commissioner and operated MFCT to closed position. Spaced out and closed MPR. Lined up cement unit.", "dTimEnd": "2008-08-04T01:45:00+02:00", "dTimStart": "2008-08-04T01:30:00+02:00", "md": "3733", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressure tested casing/liner to 345 bar / 10 min. Observed 0,5 bar drop / 10 min (0,15%) towards end of test - ok. Pumped and bled back 2280 liter.", "dTimEnd": "2008-08-04T02:45:00+02:00", "dTimStart": "2008-08-04T01:45:00+02:00", "md": "3733", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Flowchecked well on trip tanks - well static. Meanwhile terminated building 7\" tubing stands and prepared for laying out singles / pulling DP.", "dTimEnd": "2008-08-04T03:15:00+02:00", "dTimStart": "2008-08-04T02:45:00+02:00", "md": "3733", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke out and set back 5 1/2\" DP stand. Pulled, broke and laid out 4 x 5 1/2\" DP singles.", "dTimEnd": "2008-08-04T04:15:00+02:00", "dTimStart": "2008-08-04T03:15:00+02:00", "md": "3647", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with cleaning assemblies on 5 1/2\" DP from 3647 m to 3170 m MD.", "dTimEnd": "2008-08-04T05:15:00+02:00", "dTimStart": "2008-08-04T04:15:00+02:00", "md": "3170", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke out an laid down cleaning assy #5 - 10 3 /4\" razor back / posi drift / wellsweep magnets / well patroller.", "dTimEnd": "2008-08-04T05:45:00+02:00", "dTimStart": "2008-08-04T05:15:00+02:00", "md": "3749", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke and laid out 2 x 5 1/2\" DP singles. POOH with cleaning assemblies on 5 1/2\" DP from 3131 m to 3011 m MD.", "dTimEnd": "2008-08-04T06:00:00+02:00", "dTimStart": "2008-08-04T05:45:00+02:00", "md": "3011", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with cleaning assemblies on 5 1/2\" DP from 3011 m to 2201 m MD. Got problems with HPU indicating hydraulic leakage.", "dTimEnd": "2008-08-04T08:00:00+02:00", "dTimStart": "2008-08-04T06:00:00+02:00", "md": "2201", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Troubleshot HPU. Found leakage on hose to PS-21 slips. Removed slips. Installed masterbushing to continue pulling pipe using manual slips.", "dTimEnd": "2008-08-04T09:15:00+02:00", "dTimStart": "2008-08-04T08:00:00+02:00", "md": "2201", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "POOH with cleaning assemblies on 5 1/2 DP from 2201 to 2000 m MD. Used manual slips.", "dTimEnd": "2008-08-04T09:30:00+02:00", "dTimStart": "2008-08-04T09:15:00+02:00", "md": "2000", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed masterbushing. Installed PS-21 automatic slips and function tested same.", "dTimEnd": "2008-08-04T10:00:00+02:00", "dTimStart": "2008-08-04T09:30:00+02:00", "md": "2000", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "POOH with cleaning assemblies on 5 1/2\" DP from 2000 m to 950 m MD.", "dTimEnd": "2008-08-04T12:00:00+02:00", "dTimStart": "2008-08-04T10:00:00+02:00", "md": "950", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke out and laid out cleaning assy#4 - MFCT / well patroller / wellsweep magnet and cleaning assy #3 - polish/top-dress mill / well commissioner / wellsweep magnets. Recovered 4 kg swarf on magnets. Nothing recovered in well patrollers.", "dTimEnd": "2008-08-04T13:15:00+02:00", "dTimStart": "2008-08-04T12:00:00+02:00", "md": "920", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Set up AFT PRS for racking 3 1/2\" DP stands. Not able to rack stands using AFT PRS.", "dTimEnd": "2008-08-04T13:30:00+02:00", "dTimStart": "2008-08-04T13:15:00+02:00", "md": "920", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Troubleshot racking problem. Calibrated fwd PRS. Attempted to rack pipe with FWD PRS - negative. Calibrated AFT PRS, not able to rack pipe. Had problems with anti-collission system and pipe clashed with racking fingers. Fixed hydraulic leakge on HPU which may have caused malfunction on anti-collision system. Had problems with \"pipe set down\" function, system not registering when pipe set down. Parked AFT PRS. Continued to troubleshot FWD PRS. Attempted to rack stand of pipe - ok.", "dTimEnd": "2008-08-04T20:30:00+02:00", "dTimStart": "2008-08-04T13:30:00+02:00", "md": "920", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "POOH with cleaning assemblies on 3 1/2\" DP from 920 m to 30 m MD. Racked back 3 1/2\" DP in foldable fingerboard using FWD PRS. Removed automatic slips and installed masterbushings.", "dTimEnd": "2008-08-04T23:15:00+02:00", "dTimStart": "2008-08-04T20:30:00+02:00", "md": "30", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled and laid out 2 x 3 1/2\" DP singles. Broke and laid out cleaning assy #2 - 7\" razor back / wellsweep magnets. Broke and laid out cleaning assy #1 - 6 \" PDC bit.", "dTimEnd": "2008-08-04T23:45:00+02:00", "dTimStart": "2008-08-04T23:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- circulating conditioning", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Changed to 5 1/2\" handling equipment. Lifted VMB plug onto HTS.", "dTimEnd": "2008-08-05T00:00:00+02:00", "dTimStart": "2008-08-04T23:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_08_06
NO 15/9-F-5
NO 15/9-F-5
name
2008-08-05T00:00:00+02:00
2008-08-06T00:00:00+02:00
normal
2018-05-03T13:53:02+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-08-06T00:00:00+02:00", "dTimDiaHoleStart": "2008-08-05T21:30:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Transfer weight from tensioners to block. Dismantle tensioner assembly. Disconnect TBC. Pull HPDR.", "hpht": "0", "md": "3792", "mdCsgLast": "3790.1", "mdDiaHoleStart": "3792", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3754", "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "37", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "POOH with VMB setting tool. Tested VMB plug to 345 bar / 10 min from above. Retrieved wear bushing. RIH with lock down sub on PADPRT. Not able to set lock down sub. Washed/jetted wellhead. Set lock down sub. Pulled diverter and nippled down BOP. Picked up and landed claxton tool on BOP joint. Made up claxton tool.", "tightWell": "0", "tvd": "3247", "tvdCsgLast": "3245.3", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-08-05T21:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Active pit", "md": "3792", "mudClass": "other", "presBopRating": "345", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[]
[]
[ { "comments": "Picked up and hung off VMB plug / setting tool in rotary.", "dTimEnd": "2008-08-05T00:15:00+02:00", "dTimStart": "2008-08-05T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with VBM plug / setting tool on 5 1/2\" DP from surface to 608 m MD.", "dTimEnd": "2008-08-05T02:15:00+02:00", "dTimStart": "2008-08-05T00:15:00+02:00", "md": "608", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH on last stand to 638 m MD while circualting packer fluid at 800 lpm / SPP 2 bar. Stopped pumping. Took up/down weights 95/89 MT.", "dTimEnd": "2008-08-05T02:30:00+02:00", "dTimStart": "2008-08-05T02:15:00+02:00", "md": "638", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rotated pipe clockwise at 15 rpm and slacked off weight. Stopped rotation and set down to 60 MT. Took 30 MT overpull to confirm plug set. Confirmed plug set with packer element at 636,5 m MD and top of plug at 634 m MD.", "dTimEnd": "2008-08-05T02:45:00+02:00", "dTimStart": "2008-08-05T02:30:00+02:00", "md": "638", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Set down to 87 m MT in block. Made 3 attempts to shear sleeve for closing ball vavle (3/4, 1,5 and 2 lefthand turns)- nogo. On 4th attempt the shear sleeve sheared out just after 2 turn and 3100 Nm applied torque. Pressured up to 30 bar on string above plug. Rotated string righthand to re-open ball valve and observed pressure dropping to 16 bar.", "dTimEnd": "2008-08-05T03:15:00+02:00", "dTimStart": "2008-08-05T02:45:00+02:00", "md": "638", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up cement unit. Pressured up to 280 bar, observed losing ~10 MT weight on plug. Picked up weight to 82 MT on block. Continued pressuring up to 380 bar, observed losing ~4 MT on plug. Held test for 20 min, last 10 min 0,5 bar drop (0,13%). Pumped and bled back 1880/1800 liter.", "dTimEnd": "2008-08-05T04:15:00+02:00", "dTimStart": "2008-08-05T03:15:00+02:00", "md": "638", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rotated DP lefthand to close ball valve. Applied 30 bar on DP to check that ball valve closed.", "dTimEnd": "2008-08-05T04:30:00+02:00", "dTimStart": "2008-08-05T04:15:00+02:00", "md": "638", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up 5 m to get free of plug. Spotted 5 m3 hi-vis pill on top of plug at 1500 lpm / SPP 4 bar. Chased hi-vis with packer fluid.", "dTimEnd": "2008-08-05T05:00:00+02:00", "dTimStart": "2008-08-05T04:30:00+02:00", "md": "633", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with VMB plug setting tool on 5 1/2\" DP from 628 m to 130 m MD.", "dTimEnd": "2008-08-05T05:45:00+02:00", "dTimStart": "2008-08-05T05:00:00+02:00", "md": "130", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed PS-30 slips. Installed masterbushing.", "dTimEnd": "2008-08-05T06:00:00+02:00", "dTimStart": "2008-08-05T05:45:00+02:00", "md": "130", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with VMB plug setting tool on 5 1/2\" HWDP from 130 m MD to surface.", "dTimEnd": "2008-08-05T06:15:00+02:00", "dTimStart": "2008-08-05T06:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Laid down VMB plug setting tool. Prepared WBRRT for retrieveing wearbushing. Held toolbox talk and handover meeting. Meanwhile closed shear ram and lined up cement unit to pump down kill line. Pressure tested VMB plug from above to 345 bar / 10 min (0,2% drop).", "dTimEnd": "2008-08-05T07:30:00+02:00", "dTimStart": "2008-08-05T06:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Reset WBRRT according to Vetco instructions. RIH to 140 m MD on 5 1/2\" DP and engaged tool. Pulled free wearbushing with 34 MT overpull.", "dTimEnd": "2008-08-05T08:15:00+02:00", "dTimStart": "2008-08-05T07:30:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with WBRRT and wear bushing.", "dTimEnd": "2008-08-05T08:45:00+02:00", "dTimStart": "2008-08-05T08:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Released and laid out wearbushing. Reset WBRRT according to Vetco instructions. Laid down WBRRT.", "dTimEnd": "2008-08-05T09:15:00+02:00", "dTimStart": "2008-08-05T08:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up jetting sub to stand of 5 1/2\" HWDP. RIH on 2 x stands of 5 1/2\" HWDP to 115 m MD.", "dTimEnd": "2008-08-05T10:15:00+02:00", "dTimStart": "2008-08-05T09:15:00+02:00", "md": "115", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up PADPRT to 18 3/4\" lock down sub. Landed PADPRT on 10 3/4\" casing hanger at 139 m MD. Set down 7 MT on PADPRT and rotated 4 1/4\" turns to initiate locking sequence.", "dTimEnd": "2008-08-05T11:45:00+02:00", "dTimStart": "2008-08-05T10:15:00+02:00", "md": "254", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Performed line test from cement unit to kill lline HCR. 35/345 bar 5/10 min - ok. Closed LPR.", "dTimEnd": "2008-08-05T12:30:00+02:00", "dTimStart": "2008-08-05T11:45:00+02:00", "md": "254", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made 4 attempts to set lock down sub by pressuring up between LPR and PADPRT. Observed too high volumes pumped and no pressure building up. Repeated setting procedure 3 times but obtained same negative result.", "dTimEnd": "2008-08-05T14:00:00+02:00", "dTimStart": "2008-08-05T12:30:00+02:00", "md": "254", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with PADPRT and lockdown sub from 139 m MD to surface. Inspected lockdown sub and found score marks indicating junk preventing proper landing. Broke out and set back PADPRT.", "dTimEnd": "2008-08-05T15:30:00+02:00", "dTimStart": "2008-08-05T14:00:00+02:00", "md": "115", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up stand. Made up TDS and RIH with jet sub to +/- 140 m MD. Made 3 passes and jetted across wellhead at 4100 lpm / SPP 65 bar. Pumped a total of 45 m3 packer fluid.", "dTimEnd": "2008-08-05T16:45:00+02:00", "dTimStart": "2008-08-05T15:30:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Racked back stand used for jetting. Picked up and made up PADPRT. RIH on 5 1/2\" HWDP and landed PADPRT at 139 m MD. Rotated string and set down weight as instructed by Vetco.", "dTimEnd": "2008-08-05T17:45:00+02:00", "dTimStart": "2008-08-05T16:45:00+02:00", "md": "254", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Closed LPR and lined up from cement unit to pump in BOP kill line. Pressurised above PADPRT in 35 bar increments up to 207 bar to set lock down sub - ok.", "dTimEnd": "2008-08-05T18:30:00+02:00", "dTimStart": "2008-08-05T17:45:00+02:00", "md": "254", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Disengaged from lock down sub. POOH on 5 1/2\" HWDP from surface. Laid out PADRT tool and jet sub.", "dTimEnd": "2008-08-05T20:15:00+02:00", "dTimStart": "2008-08-05T18:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Ran in with stand of 5 1/2\" DP. Closed annular. Purged air in kill line in atttempt to empty riser and BOP. POOH with stand of DP. The BOP was accidentally left closed when pulling.stand, weight came up rapidly and the last tooljoint slipped through the annular causing a shock.", "dTimEnd": "2008-08-05T21:00:00+02:00", "dTimStart": "2008-08-05T20:15:00+02:00", "md": "35", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Inspected drill line and crown block for damage - none found.", "dTimEnd": "2008-08-05T21:30:00+02:00", "dTimStart": "2008-08-05T21:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Cleared and tidied drillfloor before removing diverter.", "dTimEnd": "2008-08-05T22:00:00+02:00", "dTimStart": "2008-08-05T21:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed elevator and installed sling for pulling diverter. Remove master bushing and outer ring.", "dTimEnd": "2008-08-05T22:30:00+02:00", "dTimStart": "2008-08-05T22:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled diverter and set back on drillfloor.", "dTimEnd": "2008-08-05T23:00:00+02:00", "dTimStart": "2008-08-05T22:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Attached sling to diverter slick joint, pulled and laid out slickjoint.", "dTimEnd": "2008-08-05T23:30:00+02:00", "dTimStart": "2008-08-05T23:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged down slings. Installed outer ring, masterbushing and hole cover.", "dTimEnd": "2008-08-06T00:00:00+02:00", "dTimStart": "2008-08-05T23:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_08_07
NO 15/9-F-5
NO 15/9-F-5
name
2008-08-06T00:00:00+02:00
2008-08-07T00:00:00+02:00
normal
2018-05-03T13:53:02+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-08-07T00:00:00+02:00", "dTimDiaHoleStart": "2008-08-05T21:30:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Lay out 4th and 5th HPDR doubles. Transfer F-5 flow hose from main deck to XMT deck. Run production riser from surface to 95 m. ", "hpht": "0", "md": "3792", "mdCsgLast": "3790.1", "mdDiaHoleStart": "3792", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3754", "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "38", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Transferd tension from tensioners to block. Disconnected TBC. Pulled HPDR to 24 m.", "tightWell": "0", "tvd": "3247", "tvdCsgLast": "3245.3", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-08-06T23:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "3790", "mudClass": "other", "presBopRating": "345", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[]
[]
[ { "comments": "Removed BOP tension cylinders. Nippled down BOP. Removed/rebuilt scaffolding. Moved BOP to starboard setback area in moonpool. Meanwhile made up PR tension joint handling flange to stand of DP. Ran guidewire for hotstab. ROV engaged hotstab in TBC receptacle.", "dTimEnd": "2008-08-06T03:00:00+02:00", "dTimStart": "2008-08-06T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox / short change handover meeting.", "dTimEnd": "2008-08-06T03:15:00+02:00", "dTimStart": "2008-08-06T03:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up claxton tool. Removed outer ring and master bushing and ran claxton tool through RT. Installed outer ring and master bushing. Hung off claxton tool on pup joint. Made up 5 1/2\" DP stand, ran in and landed Claxton tool on top of HPDR BOP joint.", "dTimEnd": "2008-08-06T04:30:00+02:00", "dTimStart": "2008-08-06T03:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up studs on claxton tool to 4500 Nm using Hy-torq tool and torque plate.", "dTimEnd": "2008-08-06T06:00:00+02:00", "dTimStart": "2008-08-06T04:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cleared tools and equipment from scaffolding in moonpool.", "dTimEnd": "2008-08-06T06:30:00+02:00", "dTimStart": "2008-08-06T06:00:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Took 5 MT overpull on riser. Bled down pressure on tension cylinders and transferred tenison to block until 60 MT in block. Meanwhile brought riser spider to drillfoor and function tested same.", "dTimEnd": "2008-08-06T08:00:00+02:00", "dTimStart": "2008-08-06T06:30:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Ran cylinders and lowered tensioner assembly. Disconnected tension cylinders and pulled aside. Dismanteled tensioner assembly. Dismanteled contact ring. Hoisted up contact ring. Removed centralizer and boat collision stool. Lowered tension ring onto the protector guide.", "dTimEnd": "2008-08-06T12:30:00+02:00", "dTimStart": "2008-08-06T08:00:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk prior to unlacthing TBC. Confirmed injection well F-4 shut down for heavylift operation.", "dTimEnd": "2008-08-06T12:45:00+02:00", "dTimStart": "2008-08-06T12:30:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressured up through minireel/hotstab to 3000 psi to unlock the TBC connector.", "dTimEnd": "2008-08-06T14:30:00+02:00", "dTimStart": "2008-08-06T12:45:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed hotstab in TBC connector and installed dummy stab using ROV.", "dTimEnd": "2008-08-06T14:45:00+02:00", "dTimStart": "2008-08-06T14:30:00+02:00", "md": "140", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lifted off TBC connector and came free from wellhead in on continuos stroke. Pulled claxton tool / HPDR to just under rotary table for setting slips. Set slips. Broke out and set back 5 1/2\" DP stand.", "dTimEnd": "2008-08-06T15:15:00+02:00", "dTimStart": "2008-08-06T14:45:00+02:00", "md": "130", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk for installing riser spider.", "dTimEnd": "2008-08-06T16:00:00+02:00", "dTimStart": "2008-08-06T15:15:00+02:00", "md": "130", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed master bushing and outer ring. Pulled 1st HPDR double - BOP joint and tension joint - through rotary. Installed riser spider in well center. Hung off HPDR in riser spider.", "dTimEnd": "2008-08-06T16:45:00+02:00", "dTimStart": "2008-08-06T16:00:00+02:00", "md": "100", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed fairings. Broke connection using bolt tensioner tools. Laid out 1st double with simulatneous lift by deck crane and TDS. Installed handling flange type C on 2nd double - upper pup joint and splash zone joint.", "dTimEnd": "2008-08-06T19:45:00+02:00", "dTimStart": "2008-08-06T16:45:00+02:00", "md": "100", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with HPDR to 77 m. Removed fairings. Hung off HPDR in riser spider.", "dTimEnd": "2008-08-06T20:15:00+02:00", "dTimStart": "2008-08-06T19:45:00+02:00", "md": "77", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke connection using bolt tensioner tools. 2 bolt tensioner tools got jammed on bolts. Meanwhile installed VX ring, guide funnel and hole cover on F-5 subsea wellhead.", "dTimEnd": "2008-08-06T22:15:00+02:00", "dTimStart": "2008-08-06T20:15:00+02:00", "md": "77", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Freed bolt tensioner tools that jammed/malfunctioned. Traced back up tools.", "dTimEnd": "2008-08-06T22:45:00+02:00", "dTimStart": "2008-08-06T22:15:00+02:00", "md": "77", "phase": "fixed", "proprietaryCode": "interruption -- repair", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Continued breaking connection using bolt tensioner tools. Installed handling flange type C on 3rd double - std joint#4 and std joint#5.", "dTimEnd": "2008-08-07T00:00:00+02:00", "dTimStart": "2008-08-06T22:45:00+02:00", "md": "77", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_08_08
NO 15/9-F-5
NO 15/9-F-5
name
2008-08-07T00:00:00+02:00
2008-08-08T00:00:00+02:00
normal
2018-05-03T13:53:02+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-08-08T00:00:00+02:00", "dTimDiaHoleStart": "2008-08-05T21:30:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Remove RLGF and move same to F-9. Land TBC/production riser. Lock TBC. Install tensioner assembly on Centralizer deck and transfer tension to tensioner cylinders. Cut riser at wellhead deck. Rig down riser running equipment. Install 13 5/8\" wellhead.", "hpht": "0", "md": "3792", "mdCsgLast": "3790.1", "mdDiaHoleStart": "3792", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3754", "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "39", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Laid out 2 ea HPDR joints. Transferred F-5 coflex hose to XMT deck. Prepared for running production riser. Ran production riser and entered riser guide funnel with TBC.", "tightWell": "0", "tvd": "3247", "tvdCsgLast": "3245.3", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-08-07T22:30:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "3790", "mudClass": "other", "presBopRating": "345", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[]
[]
[ { "comments": "Laid out 2nd double with simultaneous lift by deck crane and TDS", "dTimEnd": "2008-08-07T00:30:00+02:00", "dTimStart": "2008-08-07T00:00:00+02:00", "md": "77", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with HPDR double to 49 m. Removed fairings. Hung off HPDR in riser spider.", "dTimEnd": "2008-08-07T01:00:00+02:00", "dTimStart": "2008-08-07T00:30:00+02:00", "md": "49", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke connection using bolt tensioner tools. Installed handling flange type C on 4th double - std joint#2 and lower pup joint.", "dTimEnd": "2008-08-07T02:45:00+02:00", "dTimStart": "2008-08-07T01:00:00+02:00", "md": "49", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH with HPDR to 24 m. Checked zink anodes. Checked inside TBC for VX ring - none. Removed fairings. Hung off HPDR in riser spider.", "dTimEnd": "2008-08-07T04:15:00+02:00", "dTimStart": "2008-08-07T02:45:00+02:00", "md": "24", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke connection using bolt tensioner tools. Installed handling flange type C on 5th double - std joint#1, lower pup joint and TBC. Meanwhile removed tension ring 002 and installed tension ring for PR riser (10008802) on Centralizer deck.", "dTimEnd": "2008-08-07T06:00:00+02:00", "dTimStart": "2008-08-07T04:15:00+02:00", "md": "24", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Laid out 4th double with simultaneous lift by deck crane and TDS.", "dTimEnd": "2008-08-07T07:00:00+02:00", "dTimStart": "2008-08-07T06:00:00+02:00", "md": "24", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk / handover meeting prior to laying out 5th double.", "dTimEnd": "2008-08-07T07:15:00+02:00", "dTimStart": "2008-08-07T07:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "POOH 5th double - std joint #1, lower pup and TBC to surface. Laid out 5th double with simultaneous lift by deck crane and TDS.", "dTimEnd": "2008-08-07T08:30:00+02:00", "dTimStart": "2008-08-07T07:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cleaned and tided drillfloor.", "dTimEnd": "2008-08-07T09:00:00+02:00", "dTimStart": "2008-08-07T08:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk for transfering F-5 production coflex hose to XMT deck.", "dTimEnd": "2008-08-07T09:15:00+02:00", "dTimStart": "2008-08-07T09:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Transferred production coflex hose from drillfloor to XMT deck using tuggers.", "dTimEnd": "2008-08-07T10:15:00+02:00", "dTimStart": "2008-08-07T09:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "completion -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk for picking up production riser and re-arranging hatches in wellherad module.", "dTimEnd": "2008-08-07T10:30:00+02:00", "dTimStart": "2008-08-07T10:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed hatches on slot F-10. Re-arranged/built scaffolding barriers around F-5 and F-10. Configured riser spider for running production riser.", "dTimEnd": "2008-08-07T11:00:00+02:00", "dTimStart": "2008-08-07T10:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up 1st joint - TBC and stress joint, with simultaneous lift by deck crane and TDS. Chekcked / re-arranged guidwire clamp.", "dTimEnd": "2008-08-07T11:30:00+02:00", "dTimStart": "2008-08-07T11:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with TBC stress joint and hung off in riser spider. Picked up 1st double - lower pup joint and std joint #1 with simulatneous lift by deck crane and TDS. Removed handling flange on 1 st joint. Made up connection using bolt tensioner tools. Tested flange to 3000 psi through test port - ok. Installed bolt caps and fairings. Attached guidewire slings and fore-runner on TBC / stress joint.", "dTimEnd": "2008-08-07T15:00:00+02:00", "dTimStart": "2008-08-07T11:30:00+02:00", "md": "12", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with production riser to 20 m. Function trested TBC and performed pre-operational checks according to Vetco procedure.", "dTimEnd": "2008-08-07T17:15:00+02:00", "dTimStart": "2008-08-07T15:00:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with production riser to put guidewire clamp in convenient working height at Centealizer deck. Caught guidewires and attached to ROV hooks/slings on guidewire clamp. Ran guidewires indivdually to 2 m above riser guide funnel at seabed. RIH to 37 m and hung off production riser in riser spider.", "dTimEnd": "2008-08-07T18:15:00+02:00", "dTimStart": "2008-08-07T17:15:00+02:00", "md": "37", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up 2nd double - 2 ea standard joints with simulatneous lift by deck crane and TDS. Removed handling tool type E from 1st double.", "dTimEnd": "2008-08-07T18:45:00+02:00", "dTimStart": "2008-08-07T18:15:00+02:00", "md": "37", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up connection using bolt tensioner tools. Tested flange to 3000 psi through test port - ok. Installed bolt caps and fairings.", "dTimEnd": "2008-08-07T20:45:00+02:00", "dTimStart": "2008-08-07T18:45:00+02:00", "md": "37", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with production riser to 66 m. Hung off production riser in riser spider. Removed handling flange type E. Exhaust fumes on drillfloor.", "dTimEnd": "2008-08-07T21:30:00+02:00", "dTimStart": "2008-08-07T20:45:00+02:00", "md": "66", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Recessed operations due to exhaust fumes on drillfloor.", "dTimEnd": "2008-08-07T22:00:00+02:00", "dTimStart": "2008-08-07T21:30:00+02:00", "md": "66", "phase": "fixed", "proprietaryCode": "interruption -- waiting on weather", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up 3rd double - lower std joint #2 and splash zone jnt with simulatneous lift by deck crane and TDS.", "dTimEnd": "2008-08-07T22:30:00+02:00", "dTimStart": "2008-08-07T22:00:00+02:00", "md": "66", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up connection using bolt tensioner tools. Tested flange to 3000 psi through test port - ok. Installed bolt caps and fairings.", "dTimEnd": "2008-08-08T00:00:00+02:00", "dTimStart": "2008-08-07T22:30:00+02:00", "md": "66", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_08_09
NO 15/9-F-5
NO 15/9-F-5
name
2008-08-08T00:00:00+02:00
2008-08-09T00:00:00+02:00
normal
2018-05-03T13:53:03+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-08-09T00:00:00+02:00", "dTimDiaHoleStart": "2008-08-05T21:30:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Install and test 13 3/8\" multibowl. Install annulus valves. Install surface riser. Nipple up BOP and diverter. Install bowl protector in wellhead. Retrieve annulus insert.", "hpht": "0", "md": "3792", "mdCsgLast": "3790.1", "mdDiaHoleStart": "3792", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3754", "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "40", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Oriented TBC panels. Landed and locked TBC. Installed tensioner assembly on Centralizer deck. Transferred tension from block to tension cylinders. Pressure tested production riser to 20/345 bar 5/20 min. Cut tensioner joint on Tensioner deck. Transferred annulus valves to Centralizer deck. Installed and oriented 13 3/8\" surface wellhead.", "tightWell": "0", "tvd": "3247", "tvdCsgLast": "3245.3", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-08-08T22:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "3790", "mudClass": "other", "presBopRating": "345", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[]
[]
[ { "comments": "RIH with production riser to 95 m. Hung off production riser in riser spider. Removed handling flange type E.", "dTimEnd": "2008-08-08T00:30:00+02:00", "dTimStart": "2008-08-08T00:00:00+02:00", "md": "95", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Picked up 4th double - upper pup joint and tensioner joint with simultaneous lift by deck crane and TDS.", "dTimEnd": "2008-08-08T00:45:00+02:00", "dTimStart": "2008-08-08T00:30:00+02:00", "md": "95", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up connection using bolt tensioner tools. Tested flange to 3000 psi through test port - ok. Installed bolt caps and fairings.", "dTimEnd": "2008-08-08T02:45:00+02:00", "dTimStart": "2008-08-08T00:45:00+02:00", "md": "95", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with production riser to 118 m. Hung off production riser with hang off plate in riser spider.", "dTimEnd": "2008-08-08T03:30:00+02:00", "dTimStart": "2008-08-08T02:45:00+02:00", "md": "118", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed handling flange. Picked up stand with premade running flange. Made up flange to tensioner joint. Picked up weight and removed hang off plate.", "dTimEnd": "2008-08-08T04:45:00+02:00", "dTimStart": "2008-08-08T03:30:00+02:00", "md": "118", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH on 5 1/2\" DP stand to land TBC on wellhead. Observed with ROV and used pusher tool to help TBC to enter riser guide funnel. Observed in riser guide funnel window while coming down. Ran TBC to +/- 10 cm above bottom of window.", "dTimEnd": "2008-08-08T05:15:00+02:00", "dTimStart": "2008-08-08T04:45:00+02:00", "md": "138", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Released 6 MT guidewire from template and ROV hook on riser guidewire clamp. Retrieved guidewire to surface. Released 10 MT guidewire.", "dTimEnd": "2008-08-08T06:00:00+02:00", "dTimStart": "2008-08-08T05:15:00+02:00", "md": "138", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Hooked 10 MT guidewire on funnel. Removed RLGF. Oriented TBC ROV panels by rotating 1/8\" turn counterclokwise. Ran and established hotstab in TBC receptacle.", "dTimEnd": "2008-08-08T09:00:00+02:00", "dTimStart": "2008-08-08T06:00:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Landed TBC/production riser on wellhead and set down 15 MT. Verified TBC fullly landed by oserving marker/band on TBC. Locked TBC connector by pressurising port A1 to 2500-3000 psi. Observed upwards movement on TBC upper body when locking TBC.", "dTimEnd": "2008-08-08T09:15:00+02:00", "dTimStart": "2008-08-08T09:00:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Took 10 MT overpull on TBC to verify locked.", "dTimEnd": "2008-08-08T09:30:00+02:00", "dTimStart": "2008-08-08T09:15:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Moved hotstab to port B1 and flushed lower dog cavity and upper piston cavity according to Vetco procedure.", "dTimEnd": "2008-08-08T10:00:00+02:00", "dTimStart": "2008-08-08T09:30:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Measured and marked groves on tensioner joint. Installed centralizer and boat collision stool in Centralizer deck. Made up contact ring. Made up tensioner assembly half hubs. Raised tensioner assembly to contact ring using tensioner cylinders. Adjusted pressure to 90 bar and transferred tension from block to tension cylinders. Installed centralizer in Tensioner deck.", "dTimEnd": "2008-08-08T16:00:00+02:00", "dTimStart": "2008-08-08T10:00:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up TDS to landing strand. Filled production riser with seawater pumping from cement unit.", "dTimEnd": "2008-08-08T16:15:00+02:00", "dTimStart": "2008-08-08T16:00:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressure tested production riser against VMB plug to 20/345 bar 5/10 min - ok.", "dTimEnd": "2008-08-08T16:45:00+02:00", "dTimStart": "2008-08-08T16:15:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Measured and marked tensioner joint 141,4 cm above Tensioner deck. Rigged up, adjusted and dressed Norse cutting equipment on tensioner joint. Barriered off area. Adjusted block weight to put slight overpull at cut height. Drained riser through port on running flange.", "dTimEnd": "2008-08-08T20:00:00+02:00", "dTimStart": "2008-08-08T16:45:00+02:00", "md": "139", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Cut riser according to Norse cutting procedure. Retrieved cut part of tensioner joint. Removed riser spider. Installed outer ring and masterbushing. Broke out landing stand. Laid out cut part of tensioner joint. Installed hole cover in RT.", "dTimEnd": "2008-08-09T00:00:00+02:00", "dTimStart": "2008-08-08T20:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_08_10
NO 15/9-F-5
NO 15/9-F-5
name
2008-08-09T00:00:00+02:00
2008-08-10T00:00:00+02:00
normal
2018-05-03T13:53:03+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-08-10T00:00:00+02:00", "dTimDiaHoleStart": "2008-08-05T21:30:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Install diverter. Run test plug and test BOP connection. Set bowl protector. Run jet-sub, clean wellhead and displace riser to packer fluid. Pull bowl protector. Clean surface wellhead. Make up 10 3/4\" spear and rack back. Make up adjustable sub setting tool and rack back. Rig up for running 10 3/4\" casing. Make up handling tool to adjustable sub / 10 3/4\" casing hanger. Run tie-back adapter and 10 3/4\" tie-back casing. ", "hpht": "0", "md": "3792", "mdCsgLast": "3790.1", "mdDiaHoleStart": "3792", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3754", "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "41", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Pressure tested multibowl seals. Broke and pulled WH running tool. Made up DP stand and pull tested multibowl. Installed VR plugs, blind flanges and annulus valves on wellhead and tested same. Ran and landed BOP riser joint with dual lift. Made up BOP riser joint. Built scaffolding on Weather deck. Nippled up BOP. Installed BOP overshot joint.", "tightWell": "0", "tvd": "3247", "tvdCsgLast": "3245.3", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-08-09T23:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "3970", "mudClass": "other", "presBopRating": "345", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[]
[]
[ { "comments": "Put debris barrier inside tensioner joint. Re-configured cutting jig for making bevel. Cut bevel. Used handtools to dress cut and bevel. Removed cutting jig, cleared and tided Tensioner deck.", "dTimEnd": "2008-08-09T03:45:00+02:00", "dTimStart": "2008-08-09T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- casing", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pulled master bushing and outer ring. Transferred 2 x annulus valves to Tensioner deck using tugger.", "dTimEnd": "2008-08-09T04:30:00+02:00", "dTimStart": "2008-08-09T03:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed lift cap and single joint elevator on 13 3/8\" multibowl. Attached 2 tuggers for dual lift in order to avoid F-4 shut in. Lowered 13 3/8\" multibowl from drillfloor to well head. Slipped multibowl over tension joint and adjusted to correct orientation 45 deg aft stb.", "dTimEnd": "2008-08-09T05:15:00+02:00", "dTimStart": "2008-08-09T04:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Retrieved tuggers. Installed F-5 hatch on Weather deck.", "dTimEnd": "2008-08-09T06:00:00+02:00", "dTimStart": "2008-08-09T05:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Pressure tested BT seals in multibowl to 35 bar - ok. Injejected and energized plastic in upper and lower BT-seals. Tested BT seals to 3000 psi / 10 min - ok. Locked in 1000 psi between BT seals. Energized multibowl slips by torquing up cap srews to 600 ft-lbs.", "dTimEnd": "2008-08-09T10:15:00+02:00", "dTimStart": "2008-08-09T06:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed outer ring and master bushing. Removed hatch on Weather deck.", "dTimEnd": "2008-08-09T10:45:00+02:00", "dTimStart": "2008-08-09T10:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 5 1/2\" stand and made up to multibowl running tool. Performed overpull test of 5 MT on multibowl - ok.", "dTimEnd": "2008-08-09T11:00:00+02:00", "dTimStart": "2008-08-09T10:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Broke multibowl running tool with chain tong. Pulled running tool on 5 1/2\" stand. Broke out and laid out running tool. Racked back 5 1/2\" stand.", "dTimEnd": "2008-08-09T11:45:00+02:00", "dTimStart": "2008-08-09T11:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Confirmed measurement from RT to 13 3/8\" wellhead to 19,955 m using laser.", "dTimEnd": "2008-08-09T12:00:00+02:00", "dTimStart": "2008-08-09T11:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed hatch on Weatherdeck.", "dTimEnd": "2008-08-09T12:15:00+02:00", "dTimStart": "2008-08-09T12:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed slings for installing BOP riser. Prepared for dual lift in order to avoid shut in of F-4/F-14. Attached 75 MT shackle in each bail. Primary lift sling 30 MT shackles + 10 m / 10 MT sling attached to 7,5 MT pad eyes with 25 MT shackles. Secondary lift sling in each bail - 12 MT shackle + 11 MT sling + 8,5 MT sling + 11 MT sling choked around neck of BOP/NT-2 connector.", "dTimEnd": "2008-08-09T13:00:00+02:00", "dTimStart": "2008-08-09T12:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Installed VR plugs, blind flange and annulus valves on wellhead outlets and tested each component accordingly.", "dTimEnd": "2008-08-09T16:45:00+02:00", "dTimStart": "2008-08-09T13:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Inspected TDS for loose items after maintenance.", "dTimEnd": "2008-08-09T17:45:00+02:00", "dTimStart": "2008-08-09T16:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk for lifting and installing BOP joint.", "dTimEnd": "2008-08-09T18:00:00+02:00", "dTimStart": "2008-08-09T17:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Removed hatch on Weatherdeck. Removed outer ring and master bushing in RT.", "dTimEnd": "2008-08-09T19:00:00+02:00", "dTimStart": "2008-08-09T18:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Ran surface riser with TDS and dual lift to 0,5 m above 13 3/8\" wellhead. Removed hole cover and cleaned seal surface. Installed seal ring. Alligned connector and landed NT-2 connector.", "dTimEnd": "2008-08-09T20:45:00+02:00", "dTimStart": "2008-08-09T19:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up NT-2 connector according to Vetco procedure. Took 2,5 MT overpull on connector.", "dTimEnd": "2008-08-09T21:15:00+02:00", "dTimStart": "2008-08-09T20:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Barriered off wellhead module. Installed split hatch on Weatherdeck. Built scaffolding on Weatherdeck for access to BOP connection.", "dTimEnd": "2008-08-10T00:00:00+02:00", "dTimStart": "2008-08-09T21:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" } ]
[]
15_9_F_5_2008_08_11
NO 15/9-F-5
NO 15/9-F-5
name
2008-08-10T00:00:00+02:00
2008-08-11T00:00:00+02:00
normal
2018-05-03T13:53:03+02:00
{ "name": "15/9-F-5", "namingSystem": "NPD code" }
[ { "name": "15/9-F-5", "namingSystem": "NPD code" }, { "name": "5769", "namingSystem": "NPD number" } ]
[ { "dTimSpud": "2007-11-11T00:00:00+01:00", "dateDrillComplete": "2008-07-30", "daysBehind": null, "operator": "StatoilHydro", "rigAlias": [ { "name": "MÆRSK INSPIRER", "namingSystem": "NPD Name" }, { "name": "369304", "namingSystem": "NPD code" } ] } ]
[ { "avgPresBH": null, "avgTempBH": null, "dTim": "2008-08-11T00:00:00+02:00", "dTimDiaHoleStart": "2008-08-05T21:30:00+02:00", "diaHole": null, "diaPilot": null, "distDrill": "-999.99", "elevKelly": "54.9", "fixedRig": "false", "forecast24Hr": "Set bowl protector. Run jet-sub, clean wellhead and displace riser to TSW. Pull bowl protector. Clean surface wellhead. Make up 10 3/4\" spear and rack back. Make up adjustable sub setting tool and rack back. Rig up for running 10 3/4\" casing. Make up handling tool to adjustable sub / 10 3/4\" casing hanger. Run tie-back adapter and 10 3/4\" tie-back casing. Make up tie-back adapter.", "hpht": "0", "md": "3792", "mdCsgLast": "3790.1", "mdDiaHoleStart": "3792", "mdKickoff": null, "mdPlanned": "-999.99", "mdPlugTop": "3754", "mdStrengthForm": "2921", "presTestType": "formation integrity test", "reportNo": "42", "ropCurrent": "-999.99", "strengthForm": "1.65", "sum24Hr": "Ran diverter. Nippled up overshot joint. Ran BOP test plug. Tested BOP connection to 20/345 bar 5/10 min. POOH with test plug and strapped DP. Lost part of holecover in hole. Drained BOP and opened BOP bonnet to catch fish which was resting on top of BOP test plug. Caught fish with magnet. POOH and replaced and ran BOP test plug. Closed ram doors and atttempted to test BOP - observed leakage visually. Opened BSR ram doors. Re-tested BOP to 345 bar - found leakage to be hydraulic fluid. POOH with test plug and strapped pipe for surface WH datum.", "tightWell": "0", "tvd": "3247", "tvdCsgLast": "3245.3", "tvdStrengthForm": "2610", "waterDepth": "91", "wellheadElevation": "138.9" } ]
[ { "dTim": "2008-08-10T23:00:00+02:00", "density": "1.03", "filterCakeLtlp": null, "filtrateLtlp": null, "locationSample": "Reserve pit", "md": "3790", "mudClass": "other", "presBopRating": "345", "pv": "-999.99", "tempHthp": null, "type": "Packer fluid", "visFunnel": "-999.99", "yp": "-999.99" } ]
[]
[]
[ { "comments": "Covered scaffolding with canvas. Covered gap between riser and Weatherdeck with aluminum cover. Released BOP stump connector.", "dTimEnd": "2008-08-10T00:45:00+02:00", "dTimStart": "2008-08-10T00:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Skidded BOP from STB setback area and landed on BOP riser.", "dTimEnd": "2008-08-10T01:15:00+02:00", "dTimStart": "2008-08-10T00:45:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up BOP connection. Meanwhile made up swadge to TDS and tested upper/lower IBOP and standpipe to 20/345 bar 5 /10 min.", "dTimEnd": "2008-08-10T03:30:00+02:00", "dTimStart": "2008-08-10T01:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Hooked up up BOP tension cylinders to BOP. Made up bell nipple spool. Installed and made up overshot joint to BOP. Prepared for installing diverter.", "dTimEnd": "2008-08-10T06:00:00+02:00", "dTimStart": "2008-08-10T03:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Rigged up slings for installing diverter. Ran diverter.", "dTimEnd": "2008-08-10T07:00:00+02:00", "dTimStart": "2008-08-10T06:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Held toolbox talk / shift hanover meeting.", "dTimEnd": "2008-08-10T07:15:00+02:00", "dTimStart": "2008-08-10T07:00:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Continued making up overshot joint and diverter.", "dTimEnd": "2008-08-10T09:15:00+02:00", "dTimStart": "2008-08-10T07:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Made up 13 3/8\" BOP testplug. Cleaned drains inside/outside drillers cabin due to bad smell.", "dTimEnd": "2008-08-10T09:45:00+02:00", "dTimStart": "2008-08-10T09:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "RIH with 13 3/8\" BOP test plug on 5 1/2 DP stand and landed in surface wellhead at 20 m MD.", "dTimEnd": "2008-08-10T10:00:00+02:00", "dTimStart": "2008-08-10T09:45:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Lined up cement unit to BOP kill inlet and filled prodcution riser and BOP with seawater prior to pressure test.", "dTimEnd": "2008-08-10T10:30:00+02:00", "dTimStart": "2008-08-10T10:00:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Closed MPR. Pressure tested BOP connection 35/345 bar 5/10 min - ok.", "dTimEnd": "2008-08-10T11:30:00+02:00", "dTimStart": "2008-08-10T10:30:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- bop activities", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Strapped pipe according to Vetco instructions. Strapped RT to landing point to 20,46 m MD, but questioned value.", "dTimEnd": "2008-08-10T11:45:00+02:00", "dTimStart": "2008-08-10T11:30:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "drilling -- bop activities", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Function tested BOP pipe rams and annular.", "dTimEnd": "2008-08-10T12:15:00+02:00", "dTimStart": "2008-08-10T11:45:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- bop activities", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Re-strapped pipe according to Vetco instructions. When puttig on hole cover the hinged lid came loose and was lost into the riser/well.", "dTimEnd": "2008-08-10T12:30:00+02:00", "dTimStart": "2008-08-10T12:15:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "drilling -- bop/wellhead equipment", "state": "ok", "stateDetailActivity": "success" }, { "comments": "Item lost in hole was a steel plate of 18 x 20 cm. Discussed situation and made plan for attempting to fish. Found that clearance (6 mm) between the riser and the 13 3/8\" BOP test plug would make it impossible for the lid to pass the plug. Drained BOP to get dry access to BOP through ram door. Prepared fishing magnet on rope.", "dTimEnd": "2008-08-10T16:15:00+02:00", "dTimStart": "2008-08-10T12:30:00+02:00", "md": "20", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Opened LPR ram doors. Drained riser. Picked up to 11,5 m MD in order to get pictures of fish. Got pictures showing lid resting on top of 13 3/8\" test plug.", "dTimEnd": "2008-08-10T19:00:00+02:00", "dTimStart": "2008-08-10T16:15:00+02:00", "md": "11.5", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Picked up in steps to +/- 10 m and took pictures through bonnet door for each incremental movment to observe position of fish. Observed lid leaning over into the larger 18 3/4\" ID close to the BOP, i.e. in position to attmept fishing with magnet. Put magnet on rope into riser through ram door. Latched fish with magnet and caught through ram door.", "dTimEnd": "2008-08-10T20:45:00+02:00", "dTimStart": "2008-08-10T19:00:00+02:00", "md": "10", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Inspected fish and found that the pin in the broken hinge was still missing. Estimated missing pin to be 26 mm x 9 mm OD. Discussed situation. Decided to continue picking up in small increments in case pin was caught in the lip seal of the 13 3/8\" test plug.", "dTimEnd": "2008-08-10T21:15:00+02:00", "dTimStart": "2008-08-10T20:45:00+02:00", "md": "10", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "Picked up in steps of 1-2\" and took pictures through bonnet door accordingly. Picked up to lips seal was visible in larger riser ID, but found no evidence of pin being trapped in lip seal.", "dTimEnd": "2008-08-10T23:15:00+02:00", "dTimStart": "2008-08-10T21:15:00+02:00", "md": "9.5", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" }, { "comments": "POOH with 13 3/8\" test plug. Observed for lost pin through ram doors when passing LPR with 13 3/8\" test plug. Pulled 13 3/8\" test plug to surface. Found small brass washer originating from the broken hinge on top of the plug. No pin recovered (later found missing pin trapped behind lip seal). Closed doors on LPR.", "dTimEnd": "2008-08-11T00:00:00+02:00", "dTimStart": "2008-08-10T23:15:00+02:00", "md": "0", "phase": "fixed", "proprietaryCode": "interruption -- other", "state": "ok", "stateDetailActivity": "equipment failure" } ]
[]